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34-133-23953

Well Details

Well ID: 34-133-23953
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Country: United States
State: Ohio
County: Portage
Municipality: Randolph Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: WISE D & L COMM
License Status: Plugged and Abandoned
License Date: 2017-10-23
Spud Date: 1993-06-02
Spud Drilling Contractor: CO TOOLS
Final Drill Date: 1993-06-15
Well Total Depth: 7207.00 ft
Configuration: Vertical
Latitude: 41.010000
Longitude: -81.280000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1993-04-19 182 BELDEN & BLAKE CO GeoDate 4/19/93
Oil and Gas 1993-04-19 Issued Date 4/19/93 Expired Date 4/19/94 Acres 0111130 Tool Type RTA Proposed Formation CL/COPPER RIDGE Proposed Depth 07207 Proposed Drill Depth 07207
Original Spud 1993-06-02 UPDATE LOCATION PER DOGRM SURVEYOR ALE 12-11-17.
Completed 1993-06-15 UPDATE LOCATION PER DOGRM SURVEYOR ALE 12-11-17.
Reached Total Depth 1993-06-15 UPDATE LOCATION PER DOGRM SURVEYOR ALE 12-11-17.
Completion Report Received 1993-06-18 UPDATE LOCATION PER DOGRM SURVEYOR ALE 12-11-17.
Change of Owner 2007-04-27 Operator changed from 182, BELDEN & BLAKE CORPORATION to 7578, ENERVEST OPERATING LLC
APP 2017-10-23 Proposed Formations:ROSE RUN SANDSTONE, Issued Date:10/23/2017, Expired Date:10/23/2019 12:00:00 PM, Drilling unit acres:111, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2018-05-18 UPDATE LOCATION PER DOGRM SURVEYOR ALE 12-11-17.
Record Last Modified 2019-01-31 UPDATE LOCATION PER DOGRM SURVEYOR ALE 12-11-17.
Construction Permit Expires 2019-10-23 UPDATE LOCATION PER DOGRM SURVEYOR ALE 12-11-17.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 7044 7099 120
7046 0
1997-06-29 7046 0
7044 7099 120
7044 7099 120

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 22000 Gal 10000 FRAC W/22M GAL WATER & 100 SX SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1993 BELDEN & BLAKE CORPORATION 34173.00 1522.00 171
1994 BELDEN & BLAKE CORPORATION 56583.00 1450.00 346
1995 BELDEN & BLAKE CORPORATION 16434.00 487.00 347
1996 BELDEN & BLAKE CORPORATION 3533.00 187.00 350
1997 BELDEN & BLAKE CORPORATION 1903.00 92.00 351
1998 BELDEN & BLAKE CORPORATION 268.00 128.00 113
2000 BELDEN & BLAKE CORPORATION 3.00 0.00 366
2001 BELDEN & BLAKE CORPORATION 0.00 0.00 48
2002 BELDEN & BLAKE CORPORATION 0.00 25.00 102
2003 BELDEN & BLAKE CORPORATION 0.00 10.00 230
2004 BELDEN & BLAKE CORPORATION 0.00 0.00 3
2005 BELDEN & BLAKE CORPORATION 0.00 0.00 309
2006 BELDEN & BLAKE CORPORATION 0.00 0.00 309
2007 ENERVEST OPERATING LLC 0.00 0.00 0
2008 ENERVEST OPERATING LLC 0.00 0.00 0
2009 ENERVEST OPERATING LLC 0.00 0.00 0
2010 ENERVEST OPERATING LLC 0.00 0.00 0
2011 ENERVEST OPERATING LLC 0.00 0.00 0
2012 ENERVEST OPERATING LLC 0.00 0.00 0
2013 ENERVEST OPERATING LLC 0.00 0.00 365
2014 ENERVEST OPERATING LLC 0.00 0.00 0
2015 ENERVEST OPERATING LLC 0.00 0.00 0
2016 ENERVEST OPERATING LLC 0.00 0.00 0
2017 ENERVEST OPERATING LLC 0.00 0.00 0
2018 ENERVEST OPERATING LLC 0.00 0.00 3

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1993 BELDEN & BLAKE CORPORATION Brine 120 171
1994 BELDEN & BLAKE CORPORATION Brine 121 346
1995 BELDEN & BLAKE CORPORATION Brine 64 347
1996 BELDEN & BLAKE CORPORATION Brine 0 350
1997 BELDEN & BLAKE CORPORATION Brine 14 351
1998 BELDEN & BLAKE CORPORATION Brine 28 113
2000 BELDEN & BLAKE CORPORATION Brine 0 366
2001 BELDEN & BLAKE CORPORATION Brine 0 48
2002 BELDEN & BLAKE CORPORATION Brine 98 102
2003 BELDEN & BLAKE CORPORATION Brine 18 230
2004 BELDEN & BLAKE CORPORATION Brine 0 3
2005 BELDEN & BLAKE CORPORATION Brine 0 309
2006 BELDEN & BLAKE CORPORATION Brine 0 309
2007 ENERVEST OPERATING LLC Brine 0 0
2008 ENERVEST OPERATING LLC Brine 0 0
2009 ENERVEST OPERATING LLC Brine 0 0
2010 ENERVEST OPERATING LLC Brine 0 0
2011 ENERVEST OPERATING LLC Brine 0
2012 ENERVEST OPERATING LLC Brine 0 0
2013 ENERVEST OPERATING LLC Brine 0 365
2014 ENERVEST OPERATING LLC Brine 0 0
2015 ENERVEST OPERATING LLC Brine 0 0
2016 ENERVEST OPERATING LLC Brine 0 0
2017 ENERVEST OPERATING LLC Brine 0 0
2018 ENERVEST OPERATING LLC Brine 0 3

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1788474079 2018-5-17 0:00: PB No Violations 11.70
-2113376191 2018-5-15 0:00: PB No Violations 2.40
-355767128 2014-3-27 0:00: UP No Violations 0.50
-720846938 2017-7-21 0:00: UP No Violations 0.60
0000003997 Preliminary Restoration No Violations PASSED Y WITNESSED 11/12/93 INSPECTOR KEITH WHITE DATE 11/1219/93 DATA FROM OLD VAX INFO
0355767128 2014-03-27 UrbanProduction Wells No Violations Status check inspection of this Rose Run Well. My inspection found the well equipped with a concoil lift system and the well is currently shut-in. The wellhead is fenced and contains a domestic hook up that is not in service. The tank battery is fenced and diked and contains 1-210 barrel tank and a 50 barrel tank. The proper ID is posted at the tank battery and wellhead. The separator/gas production unit has been removed from the fenced area 90 north of the tank battery and there is no associated production equipment on location. Enervest acquired the well in 2007 from Belden & Blake and there has been no commercial production reported for this well since 2002. I will speak with Enervest about the status of this well.
0720846938 2017-07-21 UrbanProduction Wells No Violations I inspected this Rose Run Sandstone well in regards to Non-Producing Well Complaint #5555 filed on 3/17/17 by the current landowner of the property where the well and equipment are located. The last commercial production reported from this well was by Belden & Blake for the 1998 production year and has not produced commercially since that time. Enervest Operating acquired the well in 2007 and has reported zero (0) barrels of oil and zero (0) Mcf of natural gas production from 2007 through 2016. The wellhead consists of 4.5 production casing equipped with a 4 plunger (Concoyl) lift system. The wellhead was fenced with the ID posted and the valves on the flanged casing head and flow line were open. There is a partially fenced area to the north east that is overgrown and contains an old domestic meter, regulator, and a one (1) inch supply line. The tank battery was found badly overgrown with weeds and small trees and the fencing is missing on the north and west sides. The tank battery was diked and contained one (1) 210 barrel tank and one (1) 70 barrel tank. I found no gas production unit or separator on this location. I spoke with Joe Teppert (Enervest) to inquire about the status of this well. Joe told me that he would look into it and get back to me. I will wait for Enervest to respond.
0854761838 2017-05-22 Production Wells No Violations I inspected this Rose Run Sandstone well in regards to Non-Producing Well Complaint #5555 filed on 3/17/17 by the current landowner of the property where the well and equipment are located. The last commercial production reported from this well was by Belden & Blake for the 1998 production year and has not produced commercially since that time. Enervest Operating acquired the well in 2007 and has reported zero (0) barrels of oil and zero (0) Mcf of natural gas production from 2007 through 2016. The wellhead consists of 4.5 production casing equipped with a 4 plunger (Concoyl) lift system. The wellhead was fenced with the ID posted and the valves on the flanged casing head and flow line were open. Partial fencing remains around the former location of separator (removed) and the area is overgrown and contains an old domestic meter. The tank battery was found badly overgrown with weeds and small trees and the fencing is missing on the north and west sides. The tank battery was diked and contained one (1) 210 barrel tank and one (1) 70 barrel tank. I spoke with Joe Teppert (Enervest) to inquire about the status of this well. Joe told me that would need to speak with management to see if they plan on placing the well back into production. I will wait on a response from the company before taking further enforcement action.
0865126894 2018-06-18 Final Restoration No Violations Status check inspection of progress towards Final Restoration of this former Rose Run Sandstone well that was plugged and abandoned on 5/18/18 under Compliance Notice #1504209622. The fencing around the tank battery and area of the heated separator has been removed as well as the line heater. There is a two (2) inch flow line riser at the location of the separator and several pieces of one (1) inch plastic line exposed between the former separator location and the tank battery. The 210 barrel tank and 50 barrel tank remain on location, have been moved, and the dike walls have been knocked down. Trees and brush have been pushed into the tree line and there is a pile of debris containing stone, dirt, and cement from the former post holes to the south of the tanks. Final Restoration is due by mid-August. This Compliance Notice will be closed when Final Restoration is achieved.
1039571264 2018-05-14 Plug / Plug Back No Violations Status check inspection of this Rose Run Sandstone well that will be plugged and abandoned this week. I arrived on location and Chipco, LLC has spotted Rig #5 on the south side of the wellhead. The tubing trailer was spotted on the north side of the wellhead in preparation to run tubing tomorrow (5/15/18). No violations.
1150385778 2018-07-26 Final Restoration No Violations Status check inspection of Final Restoration progress which is due by August 18th, 2018. My inspection found that the tanks and surface equipment have been removed from location. There are several short pieces of one (1) inch, domestic, plastic line on the ground near the former separator. The area of the former tank battery is roughly graded and it appears the landowner has shoved some small trees and debris into the tree line. Enervest Operating will be required to submit an executed landowner waiver (Form 5) to leave the flow and sales lines buried, and for the lease road to remain. No violations.
1442575566 2018-05-18 Plug / Plug Back No Violations I was on location to witness the plugging and abandonment of this Rose Run Sandstone well. Chipco, LLC ran inside the 4.5 production casing with the knife tool and parted the casing at a depth of 3,133. Plugs were spotted through the casing to cover and isolate the top of the Big Lime, the Berea Sandstone/Ohio Shale interval, and the Glacial Deposits. See plugging report for more details on this job. No violations.
1504209622 2017-08-31 UrbanProduction Wells No Violations I inspected this Rose Run Sandstone well in regards to Non-Producing Well Complaint #5555 filed on 3/17/17 by the current landowner of the property where the well and equipment are located. The last commercial production reported from this well was by Belden & Blake for the 1998 production year and has not produced commercially since that time. Enervest Operating acquired the well in 2007 and has reported zero (0) barrels of oil and zero (0) Mcf of natural gas production from 2007 through 2016. The wellhead consists of 4.5 production casing equipped with a 4 plunger (Concoyl) lift system. The wellhead was fenced with the ID posted and the valves on the flanged casing head and flow line were open. There is a partially fenced area to the north that is overgrown and contains an old domestic meter, regulator, and a one (1) inch supply line. The tank battery was found overgrown with weeds and small, 2 diameter trees and the fencing is missing on the north and west sides. The tank battery was diked and contained one (1) 210 barrel tank and one (1) 70 barrel tank. I found no gas production unit or separator on this location. I inquired with Joe Teppert (Enervest) about the status of this well. Joe got back to me and told me that Enervest has no plans to repair the well or place it back in production. It is determined that the well is currently incapable of production. The well owner/operator shall submit a written plugging schedule to Michael Dinsmore at 3575 Forest Lake Drive, Suite 150, Uniontown, Ohio 44685-8116 within 30 days, per OAC 1501:9-11-05(B), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied.
1526927502 2018-05-21 Plug / Plug Back No Violations Status check inspection following the conclusion of plugging operations on 5/18/18. My inspection found the circulating pit has been closed and the entire work area has been graded. Final Restoration is due in three (3) months (urbanized township) by mid August. No violations.
1528206752 2018-05-16 Plug / Plug Back No Violations I was on location to witness the plugging and abandonment of this Rose Run Sandstone well. The bottom plug was spotted from 7100-6700 with 6.3 barrels of Class A cement by Chipco, LLC. The tubing was pulled to 6140 and Appalachian Well Surveys ran inside the tubing with a perforating string. They were unable to get past 6000 and pulled the perforating string. The tubing was pulled and the last six (6) joint were full of set cement. Operations will continue tomorrow (5/17/18). See plugging report for more details on this job. No violations.
1788474079 2018-05-17 Plug / Plug Back No Violations I was on location to witness the plugging and abandonment of this Rose Run Sandstone well. Chipco, LLC ran inside the 4.5 production casing and tagged the top of the bottom plug at a depth of 6819. The casing was perforated by Appalachian Well Surveys and plugs were squeezed across the Point Pleasant Formation and the Clinton Sandstone in two (2) separate stages. The tubing was pulled from the well and operations were shut down for the day. See plugging report for more details on this job. No violations.
2113376191 2018-05-15 Plug / Plug Back No Violations I was on location to check the status of plugging operations. Chipco was the plugging contractor and Tim McConaha was on location to supervise operations for Enervest Operating. Chipco ran in the hole with the ripping tool (no knife) to verify total depth of the hole and that no obstructions were present. They tagged the bottom of the hole at 7,200 and the perforations are open (7,099-7,044). The intervals to plug were reviewed and agreed upon and Chipco rigged up and began running 4.7lb/ft., 2.375 tubing into the hole in preparations to set the bottom plug tomorrow (5/16/18). No violations.
3997 PL No Violations
854761838 2017-5-22 0:00: PW No Violations 0.50
865126894 2018-6-18 0:00: FR No Violations 1.30

For data sources see[9]

References