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34-133-23289

Well Details

Well ID: 34-133-23289
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Country: United States
State: Ohio
County: Portage
Municipality: Freedom Township
Operator Name: BECK ENERGY CORPORATION
Well Pad ID:
Farm/Lease Name: SHIFLETT
License Status: Final Restoration
License Date: 2010-12-16
Spud Date: 1984-10-26
Spud Drilling Contractor: CUBBY DRLG
Final Drill Date: 1984-10-30
Well Total Depth: 4550.00 ft
Configuration: Vertical
Latitude: 41.210000
Longitude: -81.180000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1984-09-24 1888 BECK ENERGY CORP GeoDate 9/24/84
Oil and Gas 1984-09-24 Issued Date 9/24/84 Expired Date 3/23/85 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 04550 Proposed Drill Depth 04550
Original Spud 1984-10-27
Completed 1984-10-30
Reached Total Depth 1984-10-30
Completion Report Received 1984-12-24
APP 2010-12-16 Proposed Formations:CLINTON, Issued Date:12/16/2010, Expired Date:12/15/2012 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2011-02-16
Construction Permit Expires 2012-12-15
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 4356 4474 0
4356 4474 0
2006-09-11 4376 4468 41
4376 4468 41
4356 4474 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 79000 Gal 50000 FRAC: H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 BECK ENERGY CORPORATION 1738.00 1150.00 230
1986 BECK ENERGY CORPORATION 1779.00 759.00 230
1987 BECK ENERGY CORPORATION 1440.00 641.00 365
1988 BECK ENERGY CORPORATION 701.00 456.00 365
1989 BECK ENERGY CORPORATION 175.00 97.00 365
1990 BECK ENERGY CORPORATION 0.00 0.00 365
1991 BECK ENERGY CORPORATION 291.00 98.00 365
1992 BECK ENERGY CORPORATION 0.00 0.00 0
1993 BECK ENERGY CORPORATION 0.00 0.00 0
1994 BECK ENERGY CORPORATION 0.00 0.00 0
1995 BECK ENERGY CORPORATION 0.00 0.00 0
1996 BECK ENERGY CORPORATION 0.00 0.00 0
1997 BECK ENERGY CORPORATION 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 BECK ENERGY CORPORATION Brine 3300 230
1986 BECK ENERGY CORPORATION Brine 1407 230
1987 BECK ENERGY CORPORATION Brine 1045 365
1988 BECK ENERGY CORPORATION Brine 685 365
1989 BECK ENERGY CORPORATION Brine 80 365
1990 BECK ENERGY CORPORATION Brine 0 365
1991 BECK ENERGY CORPORATION Brine 567 365
1992 BECK ENERGY CORPORATION Brine 0 0
1993 BECK ENERGY CORPORATION Brine 0 0
1994 BECK ENERGY CORPORATION Brine 0 0
1995 BECK ENERGY CORPORATION Brine 0 0
1996 BECK ENERGY CORPORATION Brine 0 0
1997 BECK ENERGY CORPORATION Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1161384182 2010-7-28 0:00: PW No Violations
0000PL6058 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
1161384182 2010-07-28 Production Wells Violations Noted In 1998, ODNR entered into a consent agreement with Beck Energy that required this well to be placed in production, plugged and abandoned or transferred to the landowner by October 30, 1998. According to the bonding section, Mr. Shiflett did not apply for an owner number and the well was never transferred. At this time, the tank battery has been dismantled and the equipment has been removed. The well consists of 4-1/2 casing with a swedge and ball valve. The well must be plugged and abandoned.
1421773099 2012-08-03 Final Restoration No Violations FOLLOW UP TO NOV # -1161384182. This well was plugged and abandoned on 2/16/11. All equipment has been removed and the landowner has large piles of dirt stored on the location. Final Restoration is approved.
1673844546 2010-07-28 Production Wells No Violations FOLLOW UP TO NOV # -1161384182 In 1998, ODNR entered into a consent agreement with Beck Energy that required this well to be placed in production, plugged and abandoned or transferred to the landowner by October 30, 1998. According to the bonding section, Mr. Shiflett did not apply for an owner number and the well was never transferred. At this time, the tank battery has been dismantled and the equipment has been removed. The well consists of 4-1/2 casing with a swedge and ball valve. The well must be plugged and abandoned.
1794514502 2011-02-15 Plug / Plug Back No Violations Nicks Well Plugging (NWP) is on site to plug and abandon the well as required by the Beck Consent Agreement. NWP will be running a string of tubing in the well today in order to set the bottom plug tomorrow morning.
1862579509 2010-11-01 Production Wells No Violations No change in the status or condition of this well. There is no identification and no tank battery.
PL6058 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1161384182 US-OH-104288 2010-08-02 Failure to legibly identify well
1161384182 US-OH-104289 2010-08-02 Well shall be plugged

For data sources see[9]

References