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34-133-23059

Well Details

Well ID: 34-133-23059
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Country: United States
State: Ohio
County: Portage
Municipality: Ravenna Township
Operator Name: BECK ENERGY CORPORATION
Well Pad ID:
Farm/Lease Name: WENDT
License Status: Final Restoration
License Date: 2010-09-08
Spud Date: 1983-07-17
Spud Drilling Contractor: CUBBY DRLG
Final Drill Date: 1983-07-21
Well Total Depth: 4352.00 ft
Configuration: Vertical
Latitude: 41.180000
Longitude: -81.290000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1983-04-21 Issued Date 4/21/83 Expired Date 10/18/83 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 04352 Proposed Drill Depth 04352
Original Spud 1983-07-17
Completed 1983-07-21
Reached Total Depth 1983-07-21
CO 1983-09-21 1888 BECK ENERGY CORP GeoDate 4/21/83
Completion Report Received 1984-08-02
APP 2010-09-08 Proposed Formations:CLINTON, Issued Date:9/8/2010, Expired Date:9/7/2012 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2010-11-10
Construction Permit Expires 2012-09-07
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 4174 4268 0
4174 4268 0
2006-09-11 4189 4259 13
4189 4259 13
4174 4268 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 68000 Gal 50000 FRAC;H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 BEARDMORE OIL & GAS CO 14808.00 388.00 0
2001 BECK ENERGY CORPORATION 0.00 0.00 0
2002 BECK ENERGY CORPORATION 0.00 0.00 0
2003 BECK ENERGY CORPORATION 0.00 0.00 0
2004 BECK ENERGY CORPORATION 0.00 0.00 0
2005 BECK ENERGY CORPORATION 0.00 0.00 0
2006 BECK ENERGY CORPORATION 0.00 0.00 0
2007 BECK ENERGY CORPORATION 0.00 0.00 0
2008 BECK ENERGY CORPORATION 0.00 0.00 0
2009 BECK ENERGY CORPORATION 0.00 0.00 0
2010 BECK ENERGY CORPORATION 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 BEARDMORE OIL & GAS CO Brine 0 0
2001 BECK ENERGY CORPORATION Brine 0 0
2002 BECK ENERGY CORPORATION Brine 0 0
2003 BECK ENERGY CORPORATION Brine 0 0
2004 BECK ENERGY CORPORATION Brine 0 0
2005 BECK ENERGY CORPORATION Brine 0 0
2006 BECK ENERGY CORPORATION Brine 0 0
2007 BECK ENERGY CORPORATION Brine 0 0
2008 BECK ENERGY CORPORATION Brine 0 0
2009 BECK ENERGY CORPORATION Brine 75 0
2010 BECK ENERGY CORPORATION Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1192991699 2010-11-10 0:00 PB No Violations
-931479920 2012-8-1 0:00:0 FR No Violations
0000PL6187 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0406050449 2010-11-09 Plug / Plug Back No Violations J-Well service rig is on site to start plugging operations on 11/10. Petroset will provide cement.
0931479920 2012-08-01 Final Restoration No Violations FOLLOW UP TO NOV # 1769939611. This well was plugged and abandoned on 11/10/2010. All equipment has been removed and the location has been restored and is being cultivated. Final Restoration is approved.
1192991699 2010-11-10 Plug / Plug Back No Violations The well was plugged to abandon. The plugging operation was witnessed, except the bottom hole plug.
1280755162 2010-07-27 Production Wells Violations Noted The well was drilled in 1983. The last reported production from this rabbit well was in 1984. The well must be placed back in production or properly plugged and abandoned. The tank battery consists of one 210 bbl stock tank. There is no separator or meter in or near the tank battery. The required identification is posted at the tank battery.
1288728038 2010-11-01 Production Wells No Violations Beck applied for and received a permit to plug and abandon this well. According to Beck personnel, the well is scheduled to be plugged the week of 11/08.
1769939611 2010-07-27 Production Wells No Violations FOLLOW UP TO NOV # 1280755162 The well was drilled in 1983. The last reported production from this rabbit well was in 1984. The well must be placed back in production or properly plugged and abandoned. The tank battery consists of one 210 bbl stock tank. There is no separator or meter in or near the tank battery. The required identification is posted at the tank battery.
406050449 2010-11-9 0:00: PB No Violations
PL6187 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1280755162 US-OH-107783 2010-08-02 Well shall be plugged

For data sources see[9]

References