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Well ID: 34-133-22803 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Franklin Township | |
Operator Name: BECK ENERGY CORPORATION | |
Well Pad ID: | |
Farm/Lease Name: HAYDEN UNIT | |
License Status: Producing | |
License Date: 2008-10-31 | |
Spud Date: 1983-01-11 | |
Spud Drilling Contractor: CUBBY DRLG | |
Final Drill Date: 1983-01-15 | |
Well Total Depth: 4172.00 ft | |
Configuration: Vertical | |
Latitude: 41.180000 | |
Longitude: -81.360000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1982-12-08 | Issued Date 12/8/82 Expired Date 6/6/83 Acres 0086730 Tool Type RTA Proposed Formation CLINTON Proposed Depth 04172 Proposed Drill Depth 04172 |
Original Spud | 1983-01-11 | |
Completed | 1983-01-15 | |
Reached Total Depth | 1983-01-15 | |
CO | 1983-02-02 | 1888 BECK ENERGY CORP GeoDate 12/8/82 |
Completion Report Received | 1983-02-09 | |
APP | 2008-10-31 | Proposed Formations:CLINTON, Issued Date:10/31/2008, Expired Date:10/31/2009 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Construction Permit Expires | 2009-10-31 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 4012 | 4123 | 0 |
4012 | 4123 | 0 | |
2006-09-11 | 4050 | 4089 | 15 |
4050 | 4089 | 15 | |
4012 | 4123 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 35000 Gal | 40000 | FRAC;35MG H2O,40M# SAND |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-395140003 | 2008-11-18 0:00 | PW | No Violations | |
0000PL6324 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0388465243 | 2009-10-21 | Production Wells | No Violations | Mr. Hayden requested this insepction. He was concerned that Beck was venting the gas to atmosphere. I found that there was a meter run and meter and Beck was selling gas. I relayed this to Mr. Hayden. |
0395140003 | 2008-11-18 | Production Wells | No Violations | Beck applied for and received a plugging permit to abandon this well. While pulling rods, the well kicked off and Beck decided to place the well back in production. The tank battery will need to be rebuilt. |
2011318272 | 2009-11-10 | Production Wells | No Violations | I received a call from Mr. Hayden (330-678-1094) reporting that Beck Energy was venting natural gas out of the stock tank. The well is connected to the Dominion system and has a new rotary meter in the tank battery. I contacted Beck and met the pumper on site. He told me that they have had problems with the separator sticking open and that he has been experimenting with it to correct the problem. I told him that he could not vent the gas to atmosphere and if the separator could not be fixed, then it must be replaced. |
388465243 | 2009-10-21 0:00 | PW | No Violations | |
PL6324 | PL | No Violations |
For data sources see[9]