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Well ID: 34-133-22263 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Palmyra Township | |
Operator Name: DIVERSIFIED PRODUCTION LLC | |
Well Pad ID: | |
Farm/Lease Name: LANZA | |
License Status: Producing | |
License Date: 1980-06-25 | |
Spud Date: 1980-06-22 | |
Spud Drilling Contractor: | |
Final Drill Date: 1980-06-27 | |
Well Total Depth: 4850.00 ft | |
Configuration: Vertical | |
Latitude: 41.080000 | |
Longitude: -81.060000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1980-06-22 | |
CO | 1980-06-25 | 198 VIKING RESOURCES CORP GeoDate 6/25/80 |
Completed | 1980-06-27 | |
Reached Total Depth | 1980-06-27 | |
Change of Owner | 2017-10-17 | Operator changed from 198, VIKING RESOURCES LLC to 8685, M & R INVESTMENTS OHIO LLC |
Record Last Modified | 2019-06-04 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4678 | 4714 | 8 |
4678 | 4714 | 8 | |
4678 | 4714 | 8 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 98900 Gal | 50000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | POMINEX INC | 677.00 | 603.00 | 0 |
1985 | JERRY MOORE INC | 19.00 | 0.00 | 0 |
1986 | POMINEX INC | 787.00 | 599.00 | 365 |
1987 | VIKING RESOURCES LLC | 6579.00 | 1538.00 | 362 |
1988 | POMINEX INC | 1009.00 | 459.00 | 365 |
1989 | CGAS EXPLORATION | 759.00 | 342.00 | 365 |
1990 | VIKING RESOURCES LLC | 2549.00 | 617.00 | 365 |
1992 | VIKING RESOURCES LLC | 1818.00 | 515.00 | 365 |
1993 | CGAS EXPLORATION | 526.00 | 250.00 | 366 |
1994 | VIKING RESOURCES LLC | 2497.00 | 533.00 | 365 |
1995 | VIKING RESOURCES LLC | 1592.00 | 431.00 | 0 |
1996 | VIKING RESOURCES LLC | 1335.00 | 444.00 | 0 |
1997 | VIKING RESOURCES LLC | 1864.00 | 392.00 | 0 |
1998 | VIKING RESOURCES LLC | 1647.00 | 371.00 | 365 |
2000 | RESOURCE AMERICA INC | 2234.00 | 358.00 | 365 |
2001 | VIKING RESOURCES LLC | 1973.00 | 311.00 | 365 |
2002 | VIKING RESOURCES LLC | 2109.00 | 311.00 | 365 |
2003 | VIKING RESOURCES LLC | 1829.00 | 316.00 | 365 |
2004 | VIKING RESOURCES LLC | 1779.00 | 272.00 | 365 |
2005 | VIKING RESOURCES LLC | 1772.00 | 257.00 | 365 |
2006 | VIKING RESOURCES LLC | 1699.00 | 226.00 | 365 |
2007 | VIKING RESOURCES LLC | 1567.00 | 226.00 | 365 |
2008 | VIKING RESOURCES LLC | 1839.00 | 271.00 | 366 |
2009 | VIKING RESOURCES LLC | 1580.00 | 237.00 | 365 |
2010 | VIKING RESOURCES LLC | 1285.00 | 139.00 | 365 |
2011 | VIKING RESOURCES LLC | 1388.00 | 247.00 | 0 |
2012 | VIKING RESOURCES LLC | 1228.00 | 160.00 | 366 |
2013 | VIKING RESOURCES LLC | 1744.00 | 247.00 | 365 |
2014 | VIKING RESOURCES LLC | 1138.00 | 184.00 | 365 |
2015 | VIKING RESOURCES LLC | 1063.00 | 160.00 | 365 |
2016 | VIKING RESOURCES LLC | 1157.00 | 200.00 | 366 |
2017 | VIKING RESOURCES LLC | 566.00 | 57.00 | 182 |
2018 | M & R INVESTMENTS OHIO LLC | 858.00 | 112.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | POMINEX INC | Brine | 0 | 0 |
1985 | JERRY MOORE INC | Brine | 0 | 0 |
1986 | POMINEX INC | Brine | 549 | 365 |
1987 | VIKING RESOURCES LLC | Brine | 200 | 362 |
1988 | POMINEX INC | Brine | 427 | 365 |
1989 | CGAS EXPLORATION | Brine | 446 | 365 |
1990 | VIKING RESOURCES LLC | Brine | 140 | 365 |
1992 | VIKING RESOURCES LLC | Brine | 120 | 365 |
1993 | CGAS EXPLORATION | Brine | 365 | 366 |
1994 | VIKING RESOURCES LLC | Brine | 140 | 365 |
1995 | VIKING RESOURCES LLC | Brine | 120 | 0 |
1996 | VIKING RESOURCES LLC | Brine | 135 | 0 |
1997 | VIKING RESOURCES LLC | Brine | 115 | 0 |
1998 | VIKING RESOURCES LLC | Brine | 80 | 365 |
2000 | RESOURCE AMERICA INC | Brine | 0 | 365 |
2001 | VIKING RESOURCES LLC | Brine | 0 | 365 |
2002 | VIKING RESOURCES LLC | Brine | 100 | 365 |
2003 | VIKING RESOURCES LLC | Brine | 0 | 365 |
2004 | VIKING RESOURCES LLC | Brine | 40 | 365 |
2005 | VIKING RESOURCES LLC | Brine | 40 | 365 |
2006 | VIKING RESOURCES LLC | Brine | 40 | 365 |
2007 | VIKING RESOURCES LLC | Brine | 40 | 365 |
2008 | VIKING RESOURCES LLC | Brine | 40 | 366 |
2009 | VIKING RESOURCES LLC | Brine | 40 | 365 |
2010 | VIKING RESOURCES LLC | Brine | 40 | 365 |
2011 | VIKING RESOURCES LLC | Brine | 40 | |
2012 | VIKING RESOURCES LLC | Brine | 160 | 366 |
2013 | VIKING RESOURCES LLC | Brine | 120 | 365 |
2014 | VIKING RESOURCES LLC | Brine | 160 | 365 |
2015 | VIKING RESOURCES LLC | Brine | 190 | 365 |
2016 | VIKING RESOURCES LLC | Brine | 160 | 366 |
2017 | VIKING RESOURCES LLC | Brine | 80 | 182 |
2018 | M & R INVESTMENTS OHIO LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1746848672 | 2010-8-9 0:00:0 | PW | No Violations | |
1281703487 | 2010-08-05 | Production Wells | Violations Noted | Rusty with Atlas America called and reported a flowline leak south of the wellhead that has impacted approximately 800 of an unnamed streambed. OEPA-DERR was also notified and Bart Raye responded. Atlas estimated 5 to 10 bbl of oil/brine were lost. Atlas responded with personnel, sorbent materials and a minihoe. A vac truck was enroute. Crude oil congregated in three main areas in the stream and Atlas planned to recover this product with either the vac truck or with sorbent materials. Several booms were placed downstream and a siphon dam was placed in the stream. Future planned remediation includes washing the stream with hot water and recovering the product with the vac truck. |
1418442942 | 2010-08-17 | Production Wells | No Violations | The affected creek bed has been remediated and the siphon dams and booms have been removed. The violation is corrected. |
1476192352 | 2016-10-11 | Production Wells | No Violations
-door. A locked chain link fence surrounds the well. The load line is secure with a lock and plug. The access road is in good repair with a locked gate at the entrance for the well. The well shares tank battery with 2-2264. The equipment on the site consists of the following:
| |
1746848672 | 2010-08-09 | Production Wells | No Violations | A majority of the cleanup has been completed. The impacted soil has been removed to Atlas Deerfield yard and the heaviest concentrations of oil have been recovered. Sorbent booms and pads will continue to be changed as necessary and the siphon dam will remain in place. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1281703487 | US-OH-107829 | 2010-08-13 | Inadequate pipeline strength | |
1281703487 | US-OH-107830 | 2010-08-13 | Well operation causing pollution and contamination |
For data sources see[9]