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Well ID: 34-133-21496 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: | |
Operator Name: DIVERSIFIED PRODUCTION LLC | |
Well Pad ID: | |
Farm/Lease Name: WOODARD | |
License Status: Producing | |
License Date: 1978-06-08 | |
Spud Date: 1978-06-23 | |
Spud Drilling Contractor: | |
Final Drill Date: 1978-07-01 | |
Well Total Depth: 4280.00 ft | |
Configuration: Vertical | |
Latitude: 41.250000 | |
Longitude: -81.330000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1978-06-08 | 277 ATWOOD ENERGY INC GeoDate 6/8/78 |
Original Spud | 1978-06-23 | |
Completed | 1978-07-01 | |
Reached Total Depth | 1978-07-01 | |
CO | 1995-07-18 | 4205 TRANSFUEL RESOURCES CO GeoDate 6/8/78 |
CO | 1995-10-27 | 213 LOMAK OPERATING CO GeoDate 6/8/78 |
Change of Owner | 2000-06-27 | Operator changed from 213, RANGE OPERATING COMPANY to 6674, GREAT LAKES ENERGY PTNSHP LLC |
Change of Owner | 2010-04-08 | Operator changed from 6674, RANGE RESOURCES-APPALACHIA LLC to 7578, ENERVEST OPERATING LLC |
Change of Owner | 2017-05-01 | Operator changed from 7578, ENERVEST OPERATING LLC, to 8685, M & R INVESTMENTS OHIO LLC |
Record Last Modified | 2019-06-04 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4132 | 4188 | 19 |
4132 | 4188 | 19 | |
4132 | 4188 | 19 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 80000 Gal | 60000 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | ATWOOD ENERGY INC | 2742.00 | 278.00 | 0 |
1985 | ATWOOD ENERGY INC | 1987.00 | 89.00 | 0 |
1986 | ATWOOD ENERGY INC | 1412.00 | 187.00 | 365 |
1987 | ATWOOD ENERGY INC | 1846.00 | 184.00 | 365 |
1988 | ATWOOD ENERGY INC | 1855.00 | 175.00 | 365 |
1989 | ATWOOD ENERGY INC | 1099.00 | 255.00 | 365 |
1990 | ATWOOD ENERGY INC | 1297.00 | 98.00 | 365 |
1991 | ATWOOD ENERGY INC | 1238.00 | 83.00 | 365 |
1992 | ATWOOD RESOURCES INC | 919.00 | 96.00 | 365 |
1993 | ATWOOD RESOURCES INC | 805.00 | 290.00 | 365 |
1995 | TRANSFUEL RESOURCES CO | 272.00 | 0.00 | 270 |
1996 | RANGE OPERATING COMPANY | 885.00 | 0.00 | 365 |
1997 | RANGE OPERATING COMPANY | 589.00 | 0.00 | 365 |
1998 | RANGE OPERATING COMPANY | 543.00 | 0.00 | 365 |
1999 | RANGE OPERATING COMPANY | 1.00 | 0.00 | 28 |
2010 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2011 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2012 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2013 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 365 |
2014 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2015 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2016 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 0 |
2017 | ENERVEST OPERATING LLC | 0.00 | 0.00 | 44 |
2018 | M & R INVESTMENTS OHIO LLC | 0.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | ATWOOD ENERGY INC | Brine | 0 | 0 |
1985 | ATWOOD ENERGY INC | Brine | 130 | 0 |
1986 | ATWOOD ENERGY INC | Brine | 95 | 365 |
1987 | ATWOOD ENERGY INC | Brine | 250 | 365 |
1988 | ATWOOD ENERGY INC | Brine | 140 | 365 |
1989 | ATWOOD ENERGY INC | Brine | 155 | 365 |
1990 | ATWOOD ENERGY INC | Brine | 150 | 365 |
1991 | ATWOOD ENERGY INC | Brine | 0 | 365 |
1992 | ATWOOD RESOURCES INC | Brine | 0 | 365 |
1993 | ATWOOD RESOURCES INC | Brine | 170 | 365 |
1995 | TRANSFUEL RESOURCES CO | Brine | 0 | 270 |
1996 | RANGE OPERATING COMPANY | Brine | 0 | 365 |
1997 | RANGE OPERATING COMPANY | Brine | 140 | 365 |
1998 | RANGE OPERATING COMPANY | Brine | 365 | |
1999 | RANGE OPERATING COMPANY | Brine | 0 | 28 |
2010 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2011 | ENERVEST OPERATING LLC | Brine | 0 | |
2012 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2013 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2014 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2015 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2016 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2017 | M & R INVESTMENTS OHIO LLC | Brine | 0 | 0 |
2018 | M & R INVESTMENTS OHIO LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1086251760 | 2019-2-25 0:00: | UP | No Violations | 0.80 |
1374748141 | 2019-03-27 | UrbanProduction Wells | No Violations | Status check inspection of this Clinton Sandstone well that I requested the annular space between the 8-5/8 surface casing and 4-1/2 production casing be exposed and gauged. My inspection today found that a gauge has been installed on the annular port. I opened the needle gauge and found a pressure reading of 98psi and it is below the maximum allowable pressure of 123psi (.303 X 407) based on OAC 1501:9-1-08(N)(2). I am waiting on M&R to determine if the well will be placed back into production. |
1543507855 | 2018-11-29 | UrbanProduction Wells | No Violations | Status check inspection of this Clinton Sandstone well. My inspection found the wellhead fenced and locked and a Diversified (M&R) identification sign posted on the fencing. The required well information was not filled in on the ID signage. The wellhead is equipped with 2.375 tubing and a plunger lift system. The main valve on the tubing is closed and the flow line valves on the tubing and 4.5 production casing are closed. The former tank battery is located along the east side of the lease road and does not contain any surface production equipment (tanks or separators). The inlet and outlet risers are present, the valves are closed, and they are fitted with bull plugs. The sales line riser is present as well as the old dump lines. The area is fenced and diked, the man door has been removed, and the fence panel is splayed open (no post). There are two (2) Diversified (M&R) ID stickers on the main gate post and the well information is still legible on the old Great Lakes Energy ID sign. Production records indicate that this well has not produced commercially since the 1998 reporting period and the well is not capable of production as it is currently equipped. I spoke with Rusty Morrison (M&R) and informed him of my findings. Rusty told me he has not had a chance to look at this well and evaluate its viability since it was acquired by M&R Investments. I asked him to make a determination within the next three (3) months at which time they will need to work towards placing the well back into production or a compliance notice will be issued to plug the well. |
1580916834 | 2020-2-5 0:00:0 | UP | No Violations |
For data sources see[9]