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Well ID: 34-133-20368 | Loading map...
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Country: United States | |
State: Ohio | |
County: Portage | |
Municipality: Randolph Township | |
Operator Name: VANGUARD OIL & GAS LLC | |
Well Pad ID: | |
Farm/Lease Name: CHUDANOV JELENA COMM | |
License Status: Producing | |
License Date: 1995-05-16 | |
Spud Date: 1965-02-07 | |
Spud Drilling Contractor: | |
Final Drill Date: 1965-02-13 | |
Well Total Depth: 4454.00 ft | |
Configuration: Vertical | |
Latitude: 41.060000 | |
Longitude: -81.270000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1965-02-07 | |
Completed | 1965-02-13 | |
Reached Total Depth | 1965-02-13 | |
CO | 1995-04-20 | 182 BELDEN & BLAKE CO |
Construction Permit Expires | 1996-05-15 | |
Change of Owner | 2001-04-05 | Operator changed from 457, ALSID OIL & GAS to 6970, VANGUARD OIL & GAS LLC |
Record Last Modified | 2016-07-14 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4372 | 4375 | 6 |
2006-09-11 | 4353 | 4363 | 2 |
4353 | 4363 | 2 | |
4353 | 4363 | 2 | |
2006-09-11 | 4412 | 4422 | 2 |
2006-09-11 | 4402 | 4412 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 999 Bbl | 30000 | R.P. 48 HRS. |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | DOMINION EAST OHIO | 1205.00 | 58.00 | 0 |
1985 | DOMINION EAST OHIO | 1610.00 | 0.00 | 365 |
1986 | DOMINION EAST OHIO | 52.00 | 1075.00 | 365 |
1987 | DOMINION EAST OHIO | 1412.00 | 0.00 | 371 |
1988 | DOMINION EAST OHIO | 1491.00 | 0.00 | 291 |
1989 | DOMINION EAST OHIO | 870.00 | 36.00 | 337 |
1990 | DOMINION EAST OHIO | 654.00 | 0.00 | 365 |
1991 | DOMINION EAST OHIO | 529.00 | 31.00 | 365 |
1992 | DOMINION EAST OHIO | 627.00 | 0.00 | 365 |
1993 | DOMINION EAST OHIO | 760.00 | 0.00 | 365 |
1994 | DOMINION EAST OHIO | 760.00 | 0.00 | 365 |
1995 | BELDEN & BLAKE CORPORATION | 346.00 | 0.00 | 151 |
1996 | BELDEN & BLAKE CORPORATION | 396.00 | 60.00 | 366 |
1997 | BELDEN & BLAKE CORPORATION | 258.00 | 0.00 | 85 |
1998 | ALSID OIL & GAS | 573.00 | 0.00 | 365 |
1999 | ALSID OIL & GAS | 706.00 | 48.00 | 365 |
2000 | VANGUARD OIL & GAS LLC | 1384.00 | 0.00 | 365 |
2001 | VANGUARD OIL & GAS LLC | 1273.00 | 38.00 | 365 |
2002 | VANGUARD OIL & GAS LLC | 906.00 | 0.00 | 365 |
2003 | VANGUARD OIL & GAS LLC | 259.00 | 27.00 | 365 |
2004 | VANGUARD OIL & GAS LLC | 553.00 | 0.00 | 365 |
2005 | VANGUARD OIL & GAS LLC | 548.00 | 0.00 | 365 |
2006 | VANGUARD OIL & GAS LLC | 410.00 | 0.00 | 365 |
2007 | VANGUARD OIL & GAS LLC | 458.00 | 0.00 | 365 |
2009 | VANGUARD OIL & GAS LLC | 388.00 | 0.00 | 365 |
2010 | VANGUARD OIL & GAS LLC | 0.00 | 0.00 | 365 |
2011 | VANGUARD OIL & GAS LLC | 925.00 | 0.00 | 0 |
2012 | VANGUARD OIL & GAS LLC | 0.00 | 38.00 | 366 |
2013 | VANGUARD OIL & GAS LLC | 545.00 | 0.00 | 365 |
2014 | VANGUARD OIL & GAS LLC | 166.00 | 0.00 | 365 |
2015 | VANGUARD OIL & GAS LLC | 78.00 | 0.00 | 365 |
2016 | VANGUARD OIL & GAS LLC | 225.00 | 0.00 | 365 |
2017 | VANGUARD OIL & GAS LLC | 164.00 | 0.00 | 365 |
2018 | VANGUARD OIL & GAS LLC | 142.00 | 0.00 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-423628705 | 2012-10-23 0:00 | PW | No Violations | |
0423628705 | 2012-10-23 | Production Wells | No Violations | I performed this status check inspection to follow up on the events detailed in inspection report #1351260822 from 10/22/12. I met with inspector Bob Roush on location to inspect the well. During my inspection I found that the ID sign on the well was worn away and not legible. The tank pad contained a 100 barell stock tank and a vertical separator. The tank battery was completely overgrown by trees and brush. The wellhead was being operated as a swab well and the gate valve on the right side of the wellhead was leaking slightly after being knocked off the previous evening. The wellhead area was also overgrown with brush. The well had 118 psi on the gauge and a domestic hook-up. Bob told me he spoke with the pumper the previous evening about the ID sign and the heavy brush growing around the equipment. I will follow-up in several weeks to see if the issues have been addressed. |
1351260822 | 2012-10-22 | Production Wells | No Violations | I received a call fro Randy with the Randolph Township Fire Department at 10:06 P.M. on 10/22/12 about a gas well leak near the intersections of Saxe and Johnny Cake Roads. He told me the landowner was disking his field this evening and ran into the well head causing it to leak. I asked Randy if he could identify the permit number or owner of the well and he said that there was no information anywhere. I told Randy I would try and figure out what well it was and call him back. I determined the well was owned by Vanguard Oil & Gas. I called Randy back at 10:20 and he had me call the Fire Chief, Marty Jenior. I called Marty and told him that myself or another inspector would be out shortly to assess the situation. I called Vanguard and left a message detailing the situation at 10:29. I spoke with inspector Bob Roush and he indicated that he could get to the location quickly. Bob called me at 11:18 to inform me that the well pumper was on location and that the well had been shut-in and was no longer venting gas. I told Bob that I would meet him there in the morning to inspect the well. |
1353956871 | 2012-11-16 | Production Wells | No Violations | During this status check inspection, I found that the proper ID sign had been posted on the tank battery. The trees and brush that were overgrowing the equipment had been chopped down and removed from around the wellhead and from the tank battery. Both of the old gate valves had been removed and replaced with ball valves and the well was no longer leaking. No violations. |
476947137 | 2019-10-8 0:00: | UP | No Violations | 0.40 |
For data sources see[9]