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Well ID: 34-121-23826 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Brookfield Township | |
Operator Name: ATLAS NOBLE LLC | |
Well Pad ID: | |
Farm/Lease Name: NAGIT (OHIO POWER) | |
License Status: Final Restoration | |
License Date: 2008-12-12 | |
Spud Date: 1991-07-08 | |
Spud Drilling Contractor: MATTMARK DRILLING | |
Final Drill Date: 1991-07-13 | |
Well Total Depth: 5667.00 ft | |
Configuration: Vertical | |
Latitude: 39.800000 | |
Longitude: -81.620000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1991-06-20 | 3071 KINGSTON OIL CORP GeoDate 6/20/91 |
Oil and Gas | 1991-06-20 | Issued Date 6/20/91 Expired Date 6/19/92 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05667 Proposed Drill Depth 05667 |
Original Spud | 1991-07-08 | |
Completed | 1991-07-13 | |
Reached Total Depth | 1991-07-13 | |
Completion Report Received | 1991-09-05 | |
Change of Owner | 2001-01-12 | Operator changed from 3071, KINGSTON OIL CORP to 6867, ATLAS AMERICA INC |
Change of Owner | 2004-03-23 | Operator changed from 6867, ATLAS AMERICA INC to 6866, ATLAS NOBLE INC |
APP | 2008-12-12 | Proposed Formations:CLINTON/MEDINA, Issued Date:12/12/2008, Expired Date:12/12/2009 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2009-02-13 | |
Construction Permit Expires | 2009-12-12 | |
Record Last Modified | 2015-09-24 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5354 | 5377 | 12 |
5318 | 5432 | 0 | |
2006-09-11 | 5334 | 5339 | 4 |
5334 | 5339 | 4 | |
5318 | 5432 | 0 | |
1997-06-29 | 5318 | 5432 | 0 |
2006-09-11 | 5477 | 5481 | 6 |
2006-09-11 | 5420 | 5422 | 2 |
2006-09-11 | 5394 | 5396 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 15 | 0 | 0 | BKDN FM, FE | ||
H2O | 0 | 2400 Bbl | 35000 | FRAC W/2400 BW & 350 SX SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1991 | KINGSTON OIL CORP | 813.00 | 0.00 | 365 |
1992 | KINGSTON OIL CORP | 6247.00 | 32.00 | 350 |
1993 | KINGSTON OIL CORP | 5334.00 | 0.00 | 350 |
1994 | KINGSTON OIL CORP | 5200.00 | 0.00 | 350 |
1995 | KINGSTON OIL CORP | 3757.00 | 0.00 | 350 |
1996 | KINGSTON OIL CORP | 2812.00 | 0.00 | 350 |
1997 | KINGSTON OIL CORP | 1155.00 | 0.00 | 350 |
1998 | KINGSTON OIL CORP | 2875.00 | 0.00 | 350 |
1999 | KINGSTON OIL CORP | 1975.00 | 0.00 | 0 |
2000 | KINGSTON OIL CORP | 1630.00 | 0.00 | 0 |
2001 | CHEVRON APPALACHIA LLC | 911.00 | 0.00 | 365 |
2002 | CHEVRON APPALACHIA LLC | 987.00 | 0.00 | 365 |
2003 | ATLAS NOBLE LLC | 564.00 | 23.00 | 365 |
2004 | ATLAS NOBLE LLC | 1187.00 | 0.00 | 365 |
2005 | ATLAS NOBLE LLC | 3540.00 | 0.00 | 365 |
2006 | ATLAS NOBLE LLC | 3657.00 | 0.00 | 365 |
2007 | ATLAS NOBLE LLC | 3386.00 | 0.00 | 365 |
2008 | ATLAS NOBLE LLC | 325.00 | 0.00 | 366 |
2009 | ATLAS NOBLE LLC | 0.00 | 40.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1991 | KINGSTON OIL CORP | Brine | 70 | 365 |
1992 | KINGSTON OIL CORP | Brine | 263 | 350 |
1993 | KINGSTON OIL CORP | Brine | 114 | 350 |
1994 | KINGSTON OIL CORP | Brine | 100 | 350 |
1995 | KINGSTON OIL CORP | Brine | 118 | 350 |
1996 | KINGSTON OIL CORP | Brine | 59 | 350 |
1997 | KINGSTON OIL CORP | Brine | 0 | 350 |
1998 | KINGSTON OIL CORP | Brine | 67 | 350 |
1999 | KINGSTON OIL CORP | Brine | 31 | |
2000 | KINGSTON OIL CORP | Brine | 0 | |
2001 | CHEVRON APPALACHIA LLC | Brine | 0 | 365 |
2002 | CHEVRON APPALACHIA LLC | Brine | 0 | 365 |
2003 | ATLAS NOBLE LLC | Brine | 0 | 365 |
2004 | ATLAS NOBLE LLC | Brine | 66 | 365 |
2005 | ATLAS NOBLE LLC | Brine | 53 | 365 |
2006 | ATLAS NOBLE LLC | Brine | 47 | 365 |
2007 | ATLAS NOBLE LLC | Brine | 54 | 365 |
2008 | ATLAS NOBLE LLC | Brine | 16 | 366 |
2009 | ATLAS NOBLE LLC | Brine | 13 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000008799 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 9/17/92 INSPECTOR TED DOBBIN DATE 09/1719/92 DATA FROM OLD VAX INFO | |
0140395724 | 2009-02-13 | Production Wells | No Violations | Well has been properly plugged resolving previous Notice of Violation. |
0249900804 | 2015-11-05 | Final Restoration | No Violations | I inspected this former well location as an evaluation of current site conditions and well status. Reportedly, the well was initially permitted, drilled, and plugged and abandoned in 1984 without being completed or placed into production. The former well location is located along a NE-SW-trending ridge. The surrounding areas are comprised of lands being cultivated for feed grasses. At the time of this inspection, there is no visible surface expression of the well, former pits, or other production appurtenances. The site grade matches the surrounding area. |
1299501648 | 2009-10-22 | Final Restoration | No Violations | Final restoration work at site satisfactory pit has been filled in and site restored and vegatation has been established. |
140395724 | 2009-2-13 0:00: | PW | No Violations | |
1441383787 | 2009-01-23 | Production Wells | No Violations | Follow-up inspection revealed that well is still idle&incapable of producing in its present state of repair,talked to company rep and he stated they will have service rig on hole within the next 2 weeks to plug said well. |
1471396976 | 2008-10-20 | Production Wells | No Violations | Inspection revealed that well is shut in and has hole in casing according to field supervisor,well is equipped with 11 conductor pipe and 8 surface casing and 4.5 production casing and 2.375 tubing well was worked on a couple years ago after pulling tubing and replacing it soon after casing became defected,well also is equipped with 1-100 bbl tank in need of properr dike construction if placed back into production. |
1638095284 | 2009-02-10 | Production Wells | No Violations | On site to possibly witness setting of bottom hole plug,operator failed to call and inform inspector of postponing of plugging operation ,will set plug 2/11/09 they had to pull tubing and remove bottom joint of tubing and run it back into well. |
249900804 | 2015-11-5 0:00: | FR | No Violations | 1.00 |
8799 | PL | No Violations |
For data sources see[9]