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34-121-22109

Well Details

Well ID: 34-121-22109
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Country: United States
State: Ohio
County: Noble
Municipality: Center Township
Operator Name: NORTHWOOD ENERGY CORP
Well Pad ID:
Farm/Lease Name: MURREY
License Status: Producing
License Date: 2010-09-08
Spud Date: 2010-08-12
Spud Drilling Contractor: DAVIS DRLG
Final Drill Date: 2010-08-18
Well Total Depth: 5840.00 ft
Configuration: Vertical
Latitude: 39.750000
Longitude: -81.500000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1978-10-03 213 LOMAK OPERATING CO GeoDate 10/3/78
Original Spud 1978-10-31 OTD: 5840' IN CLINTON PB to DEVONIAN SHALE IP 20 MCF
Completed 1978-11-12 OTD: 5840' IN CLINTON PB to DEVONIAN SHALE IP 20 MCF
Change of Owner 2000-06-27 Operator changed from 213, RANGE OPERATING COMPANY to 6674, GREAT LAKES ENERGY PTNSHP LLC
Change of Owner 2000-10-12 Operator changed from 6674, GREAT LAKES ENERGY PTNSHP LLC to 5815, JADCO ENERGY INC.
Plugged Back 2010-08-17 OTD: 5840' IN CLINTON PB to DEVONIAN SHALE IP 20 MCF
Reached Total Depth 2010-08-18 OTD: 5840' IN CLINTON PB to DEVONIAN SHALE IP 20 MCF
APP 2010-09-08 Proposed Formations:BEREA/30 FOOT/GORDON/SHALE, Issued Date:9/8/2010, Expired Date:9/7/2012 12:00:00 PM, Drilling unit acres:86.54, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 2012-09-07 OTD: 5840' IN CLINTON PB to DEVONIAN SHALE IP 20 MCF
Change of Owner 2014-06-16 Operator changed from 5815, JADCO ENERGY INC to 1634, NORTHWOOD ENERGY CORP
Completion Report Received 2015-11-20 OTD: 5840' IN CLINTON PB to DEVONIAN SHALE IP 20 MCF
Record Last Modified 2015-11-23 OTD: 5840' IN CLINTON PB to DEVONIAN SHALE IP 20 MCF

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2015-11-23 2432 2921 18
2011-06-06 5623 5673 17
5623 5673 17
2432 2921 18
2432 2921 18

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 PLUG BACK TO OHIO SHALE/L HURON. DID NOT TREAT
0 0 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 ALAMCO 2836.00 0.00 0
1986 ALMCO INC 1593.00 0.00 320
1987 ALMCO INC 1587.00 0.00 334
1988 ALMCO INC 967.00 0.00 332
1990 RANGE OPERATING COMPANY 132.00 0.00 61
1991 RANGE OPERATING COMPANY 823.00 0.00 365
1992 RANGE OPERATING COMPANY 602.00 0.00 335
1993 RANGE OPERATING COMPANY 596.00 0.00 365
1994 RANGE OPERATING COMPANY 534.00 0.00 334
1995 RANGE OPERATING COMPANY 487.00 0.00 365
1996 RANGE OPERATING COMPANY 255.00 0.00 304
1997 RANGE OPERATING COMPANY 614.00 0.00 365
2000 JADCO ENERGY INC 0.00 0.00 365
2001 JADCO ENERGY INC 0.00 0.00 0
2002 JADCO ENERGY INC 0.00 0.00 0
2003 JADCO ENERGY INC 0.00 0.00 0
2004 JADCO ENERGY INC 0.00 0.00 0
2005 JADCO ENERGY INC 160.00 0.00 365
2006 JADCO ENERGY INC 456.00 0.00 365
2007 JADCO ENERGY INC 143.00 0.00 365
2008 JADCO ENERGY INC 0.00 0.00 365
2009 JADCO ENERGY INC 0.00 0.00 0
2010 JADCO ENERGY INC 0.00 0.00 365
2011 JADCO ENERGY INC 0.00 0.00 0
2012 JADCO ENERGY INC 0.00 0.00 0
2013 JADCO ENERGY INC 0.00 0.00 0
2014 NORTHWOOD ENERGY CORP 0.00 0.00 0
2015 NORTHWOOD ENERGY CORP 1376.00 0.00 365
2016 NORTHWOOD ENERGY CORP 809.00 0.00 365
2017 NORTHWOOD ENERGY CORP 211.00 0.00 365
2018 NORTHWOOD ENERGY CORP 72.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 ALAMCO Brine 0 0
1986 ALMCO INC Brine 62 320
1987 ALMCO INC Brine 55 334
1988 ALMCO INC Brine 28 332
1990 RANGE OPERATING COMPANY Brine 0 61
1991 RANGE OPERATING COMPANY Brine 70 365
1992 RANGE OPERATING COMPANY Brine 66 335
1993 RANGE OPERATING COMPANY Brine 0 365
1994 RANGE OPERATING COMPANY Brine 67 334
1995 RANGE OPERATING COMPANY Brine 0 365
1996 RANGE OPERATING COMPANY Brine 67 304
1997 RANGE OPERATING COMPANY Brine 0 365
2000 JADCO ENERGY INC Brine 0 365
2001 JADCO ENERGY INC Brine 0 0
2002 JADCO ENERGY INC Brine 0 0
2003 JADCO ENERGY INC Brine 0 0
2004 JADCO ENERGY INC Brine 0 0
2005 JADCO ENERGY INC Brine 0 365
2006 JADCO ENERGY INC Brine 41 365
2007 JADCO ENERGY INC Brine 0 365
2008 JADCO ENERGY INC Brine 0 365
2009 JADCO ENERGY INC Brine 0 0
2010 JADCO ENERGY INC Brine 30 365
2011 JADCO ENERGY INC Brine 0 0
2012 JADCO ENERGY INC Brine 0 0
2013 JADCO ENERGY INC Brine 0 0
2014 NORTHWOOD ENERGY CORP Brine 0 0
2015 NORTHWOOD ENERGY CORP Brine 1728 365
2016 NORTHWOOD ENERGY CORP Brine 293 365
2017 NORTHWOOD ENERGY CORP Brine 0 365
2018 NORTHWOOD ENERGY CORP Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1608673291 2010-8-16 0:00: PB No Violations
0009481758 2014-07-31 Plug / Plug Back No Violations My inspection today finds Davis Well Service has pulled the tubing and rods out of the well and they are now attempting to pull the casing out of the well. The casing is hung in the hole.
0368868607 2014-09-23 Production Wells No Violations My inspection today finds Northwood Energy is preparing to perform hydraulic stimulation on the well and return it to production soon after.
1281884187 2010-08-13 Production Wells No Violations Company rep called and stated they were moving service rig in on site to possibly repair well, they suspect casing has hole in it and they might want to possibly plug well back to Ohio Shale told them to apply for plug back permit ASAP.
1552059902 2014-11-19 Production Wells No Violations My inspection today finds the well has been plugged back. The well is equipped with tubing and rods and is awaiting a pump jack to be set. The tank battery has yet to be built. The pit that was used for the plug back has been filled in and the surface has been rough graded.
1608673291 2010-08-16 Plug / Plug Back No Violations On site to witness perf job on casing in preparation for plugback operation.
1773646201 2014-07-14 Administrative Inspection No Violations The well has been sold to Northwood Energy. I spoke to Bill Arnholt with Northwood Energy about the well on 7-11-2014. Mr. Arnholt stated that the company would be recompleting the well in the next few weeks and returning it to production.
1858441776 2012-02-27 Preliminary Restoration No Violations Upon inspection of well site found the plug back pit filled and vegetation established, at well head the following equipment is present 8.625 surface casing, 4.5 production casing, 1.5tubing with the well being produced by the means of a pumping unit, inspector will note only the tubing and surface casing are hooked up at this time 4.5 production casing is not hooked up, 100 barrel tank on well site also.
2018862229 2014-03-18 Production Wells Violations Noted My inspection finds the well is equipped to be produced by a pump jack. The casing valves are shut. The tank battery is comprised of one 100 bbl tank located in a dike. A separator is located out of the dike with the inlet valve closed. The owner has reported zero production on the well since 2007. THE WELL SHALL BE PLUGGED WITHIN 180 DAYS.
368868607 2014-9-23 0:00: PW No Violations
9481758 2014-7-31 0:00: PB No Violations 1.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
2018862229 US-OH-120515 2014-12-03 Well shall be plugged

For data sources see[9]

References