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34-121-22064

Well Details

Well ID: 34-121-22064
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Country: United States
State: Ohio
County: Noble
Municipality: Sharon Township
Operator Name: STONEBRIDGE OPERATING CO LLC
Well Pad ID:
Farm/Lease Name: MORRISON ETAL
License Status: Producing
License Date: 1978-10-30
Spud Date: 1979-03-15
Spud Drilling Contractor:
Final Drill Date: 1979-03-01
Well Total Depth: 5962.00 ft
Configuration: Vertical
Latitude: 39.710000
Longitude: -81.560000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1978-10-30 2098 OPI INC GeoDate 10/30/78
Unknown 1978-10-30 Issued Date 10/30/78 Expired Date 10/30/79 Acres 0000000 Tool Type Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000
Completed 1979-03-01
Reached Total Depth 1979-03-01
Original Spud 1979-03-15
Construction Permit Expires 1979-10-30
CO 1994-06-28 631 BT ENERGY CORP GeoDate 10/30/78
Change of Owner 2007-10-12 Operator changed from 631, BT ENERGY CORP to 2070, STONEBRIDGE OPERATING CO
Record Last Modified 2013-10-03

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5792 5914 18
5792 5914 18
5792 5914 18

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1500 Bbl 40000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 BT ENERGY CORP 4533.00 40.00 365
1985 BT ENERGY CORP 5639.00 0.00 365
1986 BT ENERGY CORP 5639.00 0.00 365
1987 BT ENERGY CORP 3070.00 0.00 365
1988 BT ENERGY CORP 2142.00 0.00 365
1989 BT ENERGY CORP 2766.00 0.00 365
1990 BT ENERGY CORP 1383.00 0.00 365
1991 BT ENERGY CORP 1647.00 0.00 365
1993 BT ENERGY CORP 917.00 0.00 365
1994 BT ENERGY CORP 1134.00 0.00 365
1995 BT ENERGY CORP 913.00 0.00 365
1996 BT ENERGY CORP 1112.00 0.00 238
1997 BT ENERGY CORP 432.00 0.00 238
1998 STONEBRIDGE OPERATING CO LLC 1671.00 0.00 266
1999 BT ENERGY CORP 0.00 0.00 196
2000 STONEBRIDGE OPERATING CO LLC 636.00 0.00 366
2001 STONEBRIDGE OPERATING CO LLC 551.00 0.00 91
2002 BT ENERGY CORP 2563.00 0.00 364
2003 BT ENERGY CORP 1904.00 0.00 365
2004 BT ENERGY CORP 2318.00 0.00 357
2005 BT ENERGY CORP 2012.00 0.00 357
2006 BT ENERGY CORP 517.00 0.00 252
2007 STONEBRIDGE OPERATING CO LLC 926.00 0.00 364
2008 STONEBRIDGE OPERATING CO LLC 1273.00 0.00 365
2009 STONEBRIDGE OPERATING CO LLC 273.00 0.00 63
2010 STONEBRIDGE OPERATING CO LLC 63.00 0.00 140
2011 STONEBRIDGE OPERATING CO LLC 106.00 0.00 0
2012 STONEBRIDGE OPERATING CO LLC 101.00 0.00 0
2013 STONEBRIDGE OPERATING CO LLC 93.00 0.00 0
2014 STONEBRIDGE OPERATING CO LLC 37.00 0.00 0
2015 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2016 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2017 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2018 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 BT ENERGY CORP Brine 0 365
1985 BT ENERGY CORP Brine 0 365
1986 BT ENERGY CORP Brine 40 365
1987 BT ENERGY CORP Brine 0 365
1988 BT ENERGY CORP Brine 0 365
1989 BT ENERGY CORP Brine 50 365
1990 BT ENERGY CORP Brine 0 365
1991 BT ENERGY CORP Brine 0 365
1993 BT ENERGY CORP Brine 0 365
1994 BT ENERGY CORP Brine 0 365
1995 BT ENERGY CORP Brine 0 365
1996 BT ENERGY CORP Brine 0 238
1997 BT ENERGY CORP Brine 0 238
1998 STONEBRIDGE OPERATING CO LLC Brine 0 266
1999 BT ENERGY CORP Brine 0 196
2000 STONEBRIDGE OPERATING CO LLC Brine 0 366
2001 STONEBRIDGE OPERATING CO LLC Brine 0 91
2002 BT ENERGY CORP Brine 0 364
2003 BT ENERGY CORP Brine 0 365
2004 BT ENERGY CORP Brine 0 357
2005 BT ENERGY CORP Brine 0 357
2006 BT ENERGY CORP Brine 5 252
2007 STONEBRIDGE OPERATING CO LLC Brine 0 364
2008 STONEBRIDGE OPERATING CO LLC Brine 0 365
2009 STONEBRIDGE OPERATING CO LLC Brine 0 63
2010 STONEBRIDGE OPERATING CO LLC Brine 0 140
2011 STONEBRIDGE OPERATING CO LLC Brine 0
2012 STONEBRIDGE OPERATING CO LLC Brine 0 0
2013 STONEBRIDGE OPERATING CO LLC Brine 0 0
2014 STONEBRIDGE OPERATING CO LLC Brine 0 0
2015 STONEBRIDGE OPERATING CO LLC Brine 0 0
2016 STONEBRIDGE OPERATING CO LLC Brine 0 0
2017 STONEBRIDGE OPERATING CO LLC Brine 0 0
2018 STONEBRIDGE OPERATING CO LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1544951314 2012-5-23 0:00: PW No Violations
-1573783216 2011-9-14 0:00: PW No Violations
-1803115401 2015-8-10 0:00: PW No Violations 1.00
-1968593535 2011-12-8 0:00: PW No Violations
-602138854 2014-2-25 0:00: PW No Violations 1.50
-725588477 2011-9-14 0:00: PW No Violations
0419944218 2018-12-10 Production Wells No Violations The purpose of my inspection was a follow up on a compliance notice numbered 725588477. On the day of my inspection the well appeared to be idle and I witnessed that the well was equipped with 8.625-inch diameter surface casing 4.5-inch diameter production casing, 1.5-inch diameter tubing equipped with a plunger lift system. Production equipment included a 100-barrel steel production fluid storage tank and horizontal separator. Production was reported as 0 since 2015. All production valves were closed at the time of my inspection and 2-inch diameter flow line had been disconnected. At the time of my inspection the tubing head was leaking.
0602138854 2014-02-25 Production Wells No Violations My inspection finds the well is equipped to be produced by a plunger lift system (rabbit). All valves are shut in at the well. The tank battery consists of one 100 bbl tank and a production unit. The production unit is locked. At 12:06 pm I called and left a message for the production manager to call me to discuss this well.
0725588477 2011-09-14 Production Wells Violations Noted Received complaint from landowner of idle well on property. I inspected well and found it to be shut in with last production reported in 2009, Well is equipped with 8 surface casing, 4.5 production casing and tubing string. There is one - 100 barrel tank and seperator located at lease road entrance. Noted a slight sulfur odor at wellhead. PLUG OR PRODUCE WELL OR FILE FOR TMPORARY INACTIVE STATUS. FAILURE TO COMPLY MAY RESULT IN BOND FORFIETURE.
1110088829 2020-1-6 0:00:0 PW No Violations
1323899762 2011-12-14 Production Wells No Violations Inspection revealed that there has been no change in status of well. It still remains idle and waiting on a gas meter too be set. I called the company rep and left a message for a call back with an update on getting the meter in place.
1331877329 2014-02-28 Administrative Inspection No Violations I called Mr. John Snyder of Stonebridge Operating at 11:17 am. I discussed the outstanding violation against the well with Mr. Snyder. Mr. Snyder stated that the company is trying to reach an agreement with a land owner to set a master meter. The well does not have a commercial outlet.
1389814169 2014-01-15 Production Wells No Violations My inspection today finds the well is shut in. All production valves are closed. The production unit has been pad locked.
1457533870 2016-03-02 Production Wells No Violations My inspection today finds the well is not in production. A valve on the wellhead where the flow line ties in is shut. The tank battery is comprised of one 100 barrel tank and a production unit. The production unit has a lock on it. The tank battery is overgrown with vegetation.
1465216744 2016-06-06 Production Wells No Violations My inspection today finds the well is shut in. The 4.5 to 1.5 tubing wellhead is leaking natural gas around the top of the packing ring. The tank battery is comprised of one 100 barrel tank and a production unit. Additionally, the tank battery is overgrown with vegetation and there are no signs of activity in or around the production equipment.
1500903677 2017-07-24 Production Wells No Violations The purpose of my inspection was a follow up on a compliance notice numbered -725588477. During my inspection the well was equipped with 8.625 inch diameter surface casing with a casing head, 4.5 inch diameter production casing with a tubing head, 1.5 inch diameter tubing, and a plunger lift system. All production valves were in the closed position. The packing ring on the tubing head was leaking natural gas that could be heard 300 feet away. Zero production had been reported by Stonebridge Operating Company for the year 2016. All original violations still exist. Pictures were taken to assist this inspection.
1515621542 2018-01-10 Production Wells No Violations The purpose of my inspection was a follow up on a compliance notice numbered -725588477. During my inspection the well was equipped with 8.625 inch diameter surface casing with a casing head, 4.5 inch diameter production casing with a tubing head, 1.5 inch diameter tubing, and a plunger lift system. All production valves were in the closed position. The packing ring on the tubing head was leaking natural gas. The production equipment consisted of one 100 barrel tank and a horizontal separator. Stonebridge Operating reported zero for production for the years 2015 and 2016. Well remains noncompliant. Pictures were taken to assist this inspection.
1544951314 2012-05-23 Production Wells No Violations Inspection of the well found the well still shut in and unresolved NOV from 2011,will refer to Lead inspector making initial NOV -Dave Ball .
1565622749 2019-8-12 0:00: PW No Violations 1.00
1573783216 2011-09-14 Production Wells No Violations FOLLOW UP TO NOV # -725588477 Received complaint from landowner of idle well on property. I inspected well and found it to be shut in with last production reported in 2009, Well is equipped with 8 surface casing, 4.5 production casing and tubing string. There is one - 100 barrel tank and seperator located at lease road entrance. Noted a slight sulfur odor at wellhead. PLUG OR PRODUCE WELL OR FILE FOR TMPORARY INACTIVE STATUS. FAILURE TO COMPLY MAY RESULT IN BOND FORFIETURE.
1586357827 2020-4-8 0:00:0 PW No Violations 1.00
1803115401 2015-08-10 Production Wells No Violations My inspection today finds the well is not in production. A valve on the wellhead where the flow line ties in is shut. The tank battery is comprised of one 100 barrel tank and a production unit. The production unit has a lock on it. The tank battery is overgrown with vegetation and there are no paths to the production equipment indicative of foot traffic.
1968593535 2011-12-08 Production Wells No Violations Inspection revealed that the well still remains idle. The well owner stated that they were waiting on a gas meter to be set so they could begin selling gas off of said well.
419944218 2018-12-10 0:00 PW No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0725588477 US-OH-128258 2011-09-14 Well insufficiently equipped to prevent escape of oil and gas
0725588477 US-OH-128259 2011-09-14 Well shall be plugged
0725588477 US-OH-128260 2011-09-14 Nonproduction; well shall be plugged or placed in temporary inactive status
0725588477 US-OH-128261 2011-09-14 Defective casing, leaking well
0725588477 US-OH-128262 2011-09-14 Statement of annual production not filed

For data sources see[9]

References