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34-121-21994

Well Details

Well ID: 34-121-21994
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Country: United States
State: Ohio
County: Noble
Municipality: Jackson Township
Operator Name: NORTHWOOD ENERGY CORP
Well Pad ID:
Farm/Lease Name: OHIO POWER CO
License Status: Producing
License Date: 2005-04-08
Spud Date: 1977-08-14
Spud Drilling Contractor:
Final Drill Date: 1977-09-22
Well Total Depth: 5878.00 ft
Configuration: Vertical
Latitude: 39.660000
Longitude: -81.580000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1977-06-06 213 LOMAK OPERATING CO GeoDate 6/6/77
Original Spud 1977-08-14 OTD: 5876' IN CLINTON GL=982.84
Completed 1977-09-22 OTD: 5876' IN CLINTON GL=982.84
Reached Total Depth 1977-09-22 OTD: 5876' IN CLINTON GL=982.84
CO 1992-10-13 1634 NORTHWOOD ENERGY CORP GeoDate 6/6/77
APP 2004-05-04 Proposed Formations:CLINTON, Issued Date:5/4/2004, Expired Date:5/4/2005 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
APP 2005-04-08 Proposed Formations:BEREA THRU GORDON, Issued Date:4/8/2005, Expired Date:4/8/2006 6:00:00 AM, Drilling unit acres:114.68, Proposed Well Type:OG, Proposed Well Class:POOL
Plugged Back 2005-07-27 OTD: 5876' IN CLINTON GL=982.84
Completion Report Received 2006-01-06 OTD: 5876' IN CLINTON GL=982.84
Construction Permit Expires 2006-04-08 OTD: 5876' IN CLINTON GL=982.84
Record Last Modified 2017-02-15 OTD: 5876' IN CLINTON GL=982.84

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-03-06 1801 1820 20
2006-03-06 1890 2024 24
1801 1820 20
1890 2024 24
5629 5730 16
1801 1820 20
2006-09-11 5629 5730 16

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 42000 Gal 20000 GANTZ & THIRTY FOOT
H2O 0 40000 Gal 9000
0 0 0 R.P. 40 HRS.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 ALAMCO 2060.00 0.00 0
1986 ALMCO INC 1047.00 0.00 341
1987 ALMCO INC 1565.00 0.00 352
1988 ALMCO INC 1400.00 0.00 357
1990 RANGE OPERATING COMPANY 521.00 0.00 92
1991 RANGE OPERATING COMPANY 1495.00 0.00 365
1992 RANGE OPERATING COMPANY 1027.00 0.00 274
1993 NORTHWOOD ENERGY CORP 1261.00 0.00 365
1994 NORTHWOOD ENERGY CORP 986.00 0.00 365
1995 NORTHWOOD ENERGY CORP 865.00 0.00 365
1996 NORTHWOOD ENERGY CORP 826.00 0.00 365
1997 NORTHWOOD ENERGY CORP 727.00 0.00 365
1998 NORTHWOOD ENERGY CORP 242.00 0.00 365
1999 NORTHWOOD ENERGY CORP 0.00 0.00 365
2000 NORTHWOOD ENERGY CORP 0.00 0.00 365
2001 NORTHWOOD ENERGY CORP 0.00 0.00 365
2002 NORTHWOOD ENERGY CORP 0.00 0.00 365
2003 NORTHWOOD ENERGY CORP 0.00 0.00 365
2004 NORTHWOOD ENERGY CORP 0.00 0.00 0
2005 NORTHWOOD ENERGY CORP 1647.00 0.00 365
2006 NORTHWOOD ENERGY CORP 3699.00 0.00 365
2007 NORTHWOOD ENERGY CORP 2195.00 0.00 365
2008 NORTHWOOD ENERGY CORP 1553.00 0.00 365
2009 NORTHWOOD ENERGY CORP 868.00 22.00 365
2010 NORTHWOOD ENERGY CORP 716.00 25.00 365
2011 NORTHWOOD ENERGY CORP 930.00 0.00 0
2012 NORTHWOOD ENERGY CORP 376.00 0.00 366
2013 NORTHWOOD ENERGY CORP 1870.00 0.00 365
2014 NORTHWOOD ENERGY CORP 1355.00 0.00 365
2015 NORTHWOOD ENERGY CORP 2036.00 42.00 365
2016 NORTHWOOD ENERGY CORP 2052.00 16.00 365
2017 NORTHWOOD ENERGY CORP 828.00 0.00 365
2018 NORTHWOOD ENERGY CORP 1067.00 48.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 ALAMCO Brine 0 0
1986 ALMCO INC Brine 45 341
1987 ALMCO INC Brine 40 352
1988 ALMCO INC Brine 55 357
1990 RANGE OPERATING COMPANY Brine 0 92
1991 RANGE OPERATING COMPANY Brine 71 365
1992 RANGE OPERATING COMPANY Brine 0 274
1993 NORTHWOOD ENERGY CORP Brine 0 365
1994 NORTHWOOD ENERGY CORP Brine 0 365
1995 NORTHWOOD ENERGY CORP Brine 35 365
1996 NORTHWOOD ENERGY CORP Brine 0 365
1997 NORTHWOOD ENERGY CORP Brine 35 365
1998 NORTHWOOD ENERGY CORP Brine 0 365
1999 NORTHWOOD ENERGY CORP Brine 365
2000 NORTHWOOD ENERGY CORP Brine 365
2001 NORTHWOOD ENERGY CORP Brine 365
2002 NORTHWOOD ENERGY CORP Brine 365
2003 NORTHWOOD ENERGY CORP Brine 0 365
2004 NORTHWOOD ENERGY CORP Brine 0 0
2005 NORTHWOOD ENERGY CORP Brine 1060 365
2006 NORTHWOOD ENERGY CORP Brine 127 365
2007 NORTHWOOD ENERGY CORP Brine 1275 365
2008 NORTHWOOD ENERGY CORP Brine 1205 365
2009 NORTHWOOD ENERGY CORP Brine 1194 365
2010 NORTHWOOD ENERGY CORP Brine 605 365
2011 NORTHWOOD ENERGY CORP Brine 1060
2012 NORTHWOOD ENERGY CORP Brine 1001 366
2013 NORTHWOOD ENERGY CORP Brine 853 365
2014 NORTHWOOD ENERGY CORP Brine 150 365
2015 NORTHWOOD ENERGY CORP Brine 497 365
2016 NORTHWOOD ENERGY CORP Brine 644 365
2017 NORTHWOOD ENERGY CORP Brine 495 365
2018 NORTHWOOD ENERGY CORP Brine 103 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1643764736 2004-10-14 0:00 PW No Violations
1076840373 2004-02-13 Production Wells Violations Noted Upon inspecting well site found well to be idle no I.D.posted ,no production reported on well since1999.100bbl production tank leaking on bottom seam causing a kill area approximatly4x20area.

All valves at wellhead are closed,doesnt appear that anyone has been to site in sometime.

1121527260 2005-07-12 Plug / Plug Back No Violations Stopped by service rig for update for possible plug back operation still fishing for concoil it stuck inside casing at 3500 needs to be fished out or driven to bottom to place required plugs.
1122680785 2005-07-27 Plug / Plug Back No Violations Well has been plugged back to the Ohio shale,operator ran 2100 of tested 4.5 casing back into well and cemented in place with 200 sks.
1341314888 2012-07-03 Production Wells No Violations Inspection of the well head found the following equipment , 4.5 production casing ,1.5 tubing & rods with the production valves open and the well being produced by the means of a pumping unit. 2 100 barrel tanks along with a separator and gas meter are present in an established dike .
1643764736 2004-10-14 Production Wells Violations Noted No change in status of well, conversation with Bill Arnold concerning well he stated they were planning plug back procedures later this fall or early winter depending on availability of service rig.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1076840373 US-OH-101658 2004-02-15 Well operation causing pollution and contamination
1076840373 US-OH-101659 2004-02-15 Failure to legibly identify well
1076840373 US-OH-101660 2004-02-15 Well shall be plugged
1643764736 US-OH-116190 2004-02-15 Well operation causing pollution and contamination
1643764736 US-OH-116191 2004-02-15 Failure to legibly identify well
1643764736 US-OH-116192 2004-02-15 Well shall be plugged

For data sources see[9]

References