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34-121-21850

Well Details

Well ID: 34-121-21850
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Country: United States
State: Ohio
County: Noble
Municipality: Sharon Township
Operator Name: JADCO ENERGY INC
Well Pad ID:
Farm/Lease Name: WILEY N
License Status: Producing
License Date: 1980-11-01
Spud Date: 1976-05-20
Spud Drilling Contractor:
Final Drill Date: 1976-07-01
Well Total Depth: 5511.00 ft
Configuration: Vertical
Latitude: 39.710000
Longitude: -81.630000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1976-05-20
Completed 1976-07-01
Reached Total Depth 1976-07-01
CO 1980-11-01 295 DAVID OIL CO GeoDate 11/1/80
Record Last Modified 2013-10-03

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5397 5438 19
5397 5438 19
5397 5438 19

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1450 Bbl 35000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1987 DAVID OIL CO 2005.00 0.00 365
1988 DAVID OIL CO 2274.00 0.00 365
1989 DAVID OIL CO 1959.00 0.00 365
1990 DAVID OIL CO 1517.00 0.00 365
1991 DAVID OIL CO 1881.00 0.00 365
1992 DAVID OIL CO 1984.00 0.00 365
1993 DAVID OIL CO 1801.00 0.00 365
1994 DAVID OIL CO 1838.00 0.00 365
1995 DAVID OIL CO 1525.00 0.00 365
1996 DAVID OIL CO 1385.00 0.00 365
1997 JADCO ENERGY INC 1453.00 0.00 365
1998 JADCO ENERGY INC 1512.00 0.00 365
1999 JADCO ENERGY INC 1984.00 0.00 365
2000 JADCO ENERGY INC 1855.00 0.00 365
2001 JADCO ENERGY INC 3037.00 0.00 365
2002 JADCO ENERGY INC 2860.00 0.00 365
2003 JADCO ENERGY INC 2837.00 0.00 365
2004 JADCO ENERGY INC 2762.00 0.00 365
2005 JADCO ENERGY INC 2042.00 0.00 365
2006 JADCO ENERGY INC 913.00 0.00 365
2007 JADCO ENERGY INC 2655.00 0.00 365
2008 JADCO ENERGY INC 2013.00 0.00 365
2009 JADCO ENERGY INC 2426.00 0.00 365
2010 JADCO ENERGY INC 1926.00 0.00 365
2011 JADCO ENERGY INC 1754.00 0.00 365
2012 JADCO ENERGY INC 1320.00 0.00 366
2013 JADCO ENERGY INC 1582.00 0.00 365
2014 JADCO ENERGY INC 1379.00 0.00 365
2015 JADCO ENERGY INC 1414.00 0.00 365
2016 JADCO ENERGY INC 1130.00 0.00 365
2017 JADCO ENERGY INC 1241.00 0.00 365
2018 JADCO ENERGY INC 2101.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1987 DAVID OIL CO Brine 0 365
1988 DAVID OIL CO Brine 0 365
1989 DAVID OIL CO Brine 0 365
1990 DAVID OIL CO Brine 0 365
1991 DAVID OIL CO Brine 0 365
1992 DAVID OIL CO Brine 0 365
1993 DAVID OIL CO Brine 0 365
1994 DAVID OIL CO Brine 0 365
1995 DAVID OIL CO Brine 0 365
1996 DAVID OIL CO Brine 0 365
1997 JADCO ENERGY INC Brine 0 365
1998 JADCO ENERGY INC Brine 0 365
1999 JADCO ENERGY INC Brine 0 365
2000 JADCO ENERGY INC Brine 0 365
2001 JADCO ENERGY INC Brine 0 365
2002 JADCO ENERGY INC Brine 68 365
2003 JADCO ENERGY INC Brine 0 365
2004 JADCO ENERGY INC Brine 0 365
2005 JADCO ENERGY INC Brine 0 365
2006 JADCO ENERGY INC Brine 0 365
2007 JADCO ENERGY INC Brine 30 365
2008 JADCO ENERGY INC Brine 0 365
2009 JADCO ENERGY INC Brine 0 365
2010 JADCO ENERGY INC Brine 0 365
2011 JADCO ENERGY INC Brine 0 365
2012 JADCO ENERGY INC Brine 0 366
2013 JADCO ENERGY INC Brine 0 365
2014 JADCO ENERGY INC Brine 37 365
2015 JADCO ENERGY INC Brine 0 365
2016 JADCO ENERGY INC Brine 0 365
2017 JADCO ENERGY INC Brine 0 365
2018 JADCO ENERGY INC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-230622763 2011-9-21 0:00: PW No Violations
0230622763 2011-09-21 Production Wells No Violations FOLLOW UP TO NOV # 1316647724 Received complaint from land owner, Connie Stack, of leaking well on property. I inspected site and found well leaking from production casing. It has a repair clamp on it but it is not sealed properly. Well is equipped with 8 surface casing, 4.5 production casing and 1.5 tubing. There is one 210 barrel holding tank on-site. Properly seal leakage on casing whether by new clamp or have service rig pull stretch on casing and repair faulty pipe. Failure to comply may result in bond forfieture.
1083459954 2016-05-11 Production Wells No Violations My inspection today finds the well is equipped with 2 tubing and a plunger lift system. The tank battery is comprised of one100 barrel tank, a horizontal separator and a meter with a current chart. A domestic gas assembly is located at the separator. The production equipment is located in an earthen dike.
1316647724 2011-09-21 Production Wells Violations Noted Received complaint from land owner, Connie Stack, of leaking well on property. I inspected site and found well leaking from production casing. It has a repair clamp on it but it is not sealed properly. Well is equipped with 8 surface casing, 4.5 production casing and 1.5 tubing. There is one 210 barrel holding tank on-site. Properly seal leakage on casing whether by new clamp or have service rig pull stretch on casing and repair faulty pipe. Failure to comply may result in bond forfieture.
1881292555 2011-12-14 Production Wells No Violations Well has been repaired, resolving the previous compliance notice issued on 9/21/2011.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1316647724 US-OH-109020 2011-09-21 Well insufficiently equipped to prevent escape of oil and gas
1316647724 US-OH-109021 2011-09-21 Defective casing, leaking well

For data sources see[9]

References