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Well ID: 34-121-21825 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Olive Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: AKE M | |
License Status: Final Restoration | |
License Date: 2012-12-06 | |
Spud Date: 1976-05-26 | |
Spud Drilling Contractor: | |
Final Drill Date: 1976-06-03 | |
Well Total Depth: 5991.00 ft | |
Configuration: Vertical | |
Latitude: 39.720000 | |
Longitude: -81.490000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1976-03-03 | 2143 CARLESS RESOURCES INC GeoDate 3/3/76 |
Original Spud | 1976-05-26 | |
Completed | 1976-06-03 | |
Reached Total Depth | 1976-06-03 | |
Change of Owner | 1998-07-06 | Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2012-12-06 | Proposed Formations:CLINTON, Issued Date:12/6/2012, Expired Date:12/6/2014 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2013-08-15 | |
Record Last Modified | 2014-07-25 | |
Construction Permit Expires | 2014-12-06 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5760 | 5822 | 14 |
5760 | 5822 | 14 | |
5760 | 5822 | 14 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1560 Bbl | 42000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1194025532 | 2013-8-13 0:00: | PB | No Violations | |
-1968177457 | 2013-11-19 0:00 | FR | No Violations | 2.00 |
-2119301293 | 2013-8-12 0:00: | PB | No Violations | 4.00 |
-613763804 | 2013-8-14 0:00: | PB | No Violations | 11.50 |
0240037874 | 2013-08-15 | Plug / Plug Back | No Violations | Chipco set the surface plug. The plug stayed at surface. |
0311663859 | 2012-10-22 | Production Wells | Violations Noted | My inspection today finds the well is equipped with 4.5 casing and 1.5 tubing with a plunger lift system. All valves at the well are shut. There is a slight H2S odor at the well head. No production has been reported since 2004. PLACE THE WELL BACK IN PRODUCTION OR PLUG. Failure comply may result in forfeiture of bond. |
0613763804 | 2013-08-14 | Plug / Plug Back | No Violations | Appalachian made five attempts to cut the tubing. They cut it at 3060 on the fifth run. Chipco pulled the tubing. The rig crew ripped the casing at 3022 and set an 86 sack plug. The casing pulled tight and would not move at 2822. |
0707872023 | 2009-11-17 | Production Wells | No Violations | Rabbit well equipped with tubing and 1-210 bbl tank shared with three other wells on lease. |
0839710414 | 2013-08-15 | Plug / Plug Back | No Violations | On site to witness setting of cement plugs in well, they cut casing off@2260 and then they set a 250 plug from1788-1
1538 and then they pulled casing up to 200 and then they set 200 plug to ground level. Chipco Cementing used 72 sacks of class A cement on first plug and 62 sacks on surface plug. |
1036003769 | 2013-08-13 | Plug / Plug Back | No Violations | The rig crew continued to try and free the tubing. They could not free the pipe. They spotted a 30 sk plug at 3940. |
1194025532 | 2013-08-13 | Plug / Plug Back | No Violations | On site to witness Chipco rig crew set plug in said well. |
1365700524 | 2013-04-10 | Production Wells | No Violations | Follow up to Compliance notice #311663859. The status of the well has not changed. The operator was issued a permit to plug on 12/06/2012 |
1375996031 | 2013-08-08 | Plug / Plug Back | No Violations | Inspection revealed that Chipco was moving service rig in on site preparing to plug said well. |
1376338032 | 2013-08-12 | Plug / Plug Back | No Violations | Chipco on site trying to work tubing free. |
1968177457 | 2013-11-19 | Final Restoration | No Violations | My inspection today finds the final restoration is complete. The pit has been filled, and vegetation has been established. Production equipment has been removed. |
2119301293 | 2013-08-12 | Plug / Plug Back | No Violations | The rig crew has tried for two days to free the tubing and get to bottom. They have worked down to 3940 inside the tubing. Appalachian cut the tubing at 3940. The rig crew tried to pump the tubing free but could not. |
240037874 | 2013-8-15 0:00: | PB | No Violations | 2.00 |
311663859 | 2012-10-22 0:00 | PW | No Violations | 1.00 |
707872023 | 2009-11-17 0:00 | PW | No Violations | |
839710414 | 2013-8-15 0:00: | PB | No Violations | 3.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0311663859 | US-OH-123245 | 2013-12-11 | Nonproduction; well shall be plugged or placed in temporary inactive status |
For data sources see[9]