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34-121-21818

Well Details

Well ID: 34-121-21818
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Country: United States
State: Ohio
County: Noble
Municipality: Olive Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: MORRIS R
License Status: Final Restoration
License Date: 2015-02-05
Spud Date: 1976-06-08
Spud Drilling Contractor:
Final Drill Date: 1976-06-14
Well Total Depth: 5951.00 ft
Configuration: Vertical
Latitude: 39.710000
Longitude: -81.500000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1975-12-26 2143 CARLESS RESOURCES INC GeoDate 12/26/75
Original Spud 1976-06-08
Completed 1976-06-14
Reached Total Depth 1976-06-14
Change of Owner 1998-07-06 Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC
Change of Owner 2009-12-14 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
APP 2015-02-05 Proposed Formations:CLINTON, Issued Date:2/5/2015, Expired Date:2/4/2017 12:00:00 PM, Drilling unit acres:44, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2015-06-15
Construction Permit Expires 2017-02-04
Record Last Modified 2017-02-10

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5738 5782 13
5738 5782 13
5738 5782 13

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1410 Bbl 50000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 ZILKHA ENERGY INC 2073.00 111.00 292
1987 ZILKHA ENERGY INC 1455.00 36.00 181
1988 CARLESS RESOURCES INC 1475.00 92.00 330
1989 CARLESS RESOURCES INC 1382.00 0.00 355
1990 CARLESS RESOURCES INC 2482.00 73.00 365
1991 CARLESS RESOURCES INC 2191.00 173.00 365
1992 CARLESS RESOURCES INC 2287.00 95.00 365
1993 CARLESS RESOURCES INC 1885.00 99.00 365
1994 CARLESS RESOURCES INC 1641.00 0.00 365
1995 CARLESS RESOURCES INC 1678.00 155.00 365
1996 CARLESS RESOURCES INC 1720.00 0.00 365
1997 CARLESS RESOURCES INC 1816.00 101.00 365
1998 EXCO - NORTH COAST ENERGY INC 1800.00 0.00 365
1999 EXCO - NORTH COAST ENERGY INC 2243.00 52.00 365
2000 EXCO - NORTH COAST ENERGY INC 1031.00 0.00 365
2001 EXCO - NORTH COAST ENERGY INC 853.00 0.00 365
2002 EXCO - NORTH COAST ENERGY INC 669.00 0.00 365
2003 EXCO - NORTH COAST ENERGY INC 570.00 0.00 365
2004 EXCO - NORTH COAST ENERGY INC 804.00 0.00 365
2005 EXCO - NORTH COAST ENERGY INC 673.00 78.00 365
2006 EXCO - NORTH COAST ENERGY INC 820.00 0.00 365
2007 EXCO - NORTH COAST ENERGY INC 666.00 56.00 365
2008 EXCO - NORTH COAST ENERGY INC 472.00 54.00 366
2009 EXCO - NORTH COAST ENERGY INC 448.00 0.00 365
2010 ENERVEST OPERATING LLC 810.00 114.00 365
2011 ENERVEST OPERATING LLC 661.00 0.00 0
2012 ENERVEST OPERATING LLC 685.00 0.00 366
2013 ENERVEST OPERATING LLC 471.00 0.00 365
2014 ENERVEST OPERATING LLC 529.00 6.00 365
2015 ENERVEST OPERATING LLC 0.00 0.00 303

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 ZILKHA ENERGY INC Brine 98 292
1987 ZILKHA ENERGY INC Brine 107 181
1988 CARLESS RESOURCES INC Brine 17 330
1989 CARLESS RESOURCES INC Brine 0 355
1990 CARLESS RESOURCES INC Brine 57 365
1991 CARLESS RESOURCES INC Brine 20 365
1992 CARLESS RESOURCES INC Brine 129 365
1993 CARLESS RESOURCES INC Brine 62 365
1994 CARLESS RESOURCES INC Brine 41 365
1995 CARLESS RESOURCES INC Brine 63 365
1996 CARLESS RESOURCES INC Brine 0 365
1997 CARLESS RESOURCES INC Brine 0 365
1998 EXCO - NORTH COAST ENERGY INC Brine 2 365
1999 EXCO - NORTH COAST ENERGY INC Brine 14 365
2000 EXCO - NORTH COAST ENERGY INC Brine 0 365
2001 EXCO - NORTH COAST ENERGY INC Brine 0 365
2002 EXCO - NORTH COAST ENERGY INC Brine 0 365
2003 EXCO - NORTH COAST ENERGY INC Brine 40 365
2004 EXCO - NORTH COAST ENERGY INC Brine 24 365
2005 EXCO - NORTH COAST ENERGY INC Brine 84 365
2006 EXCO - NORTH COAST ENERGY INC Brine 120 365
2007 EXCO - NORTH COAST ENERGY INC Brine 108 365
2008 EXCO - NORTH COAST ENERGY INC Brine 43 366
2009 EXCO - NORTH COAST ENERGY INC Brine 43 365
2010 ENERVEST OPERATING LLC Brine 61 365
2011 ENERVEST OPERATING LLC Brine 0
2012 ENERVEST OPERATING LLC Brine 0 366
2013 ENERVEST OPERATING LLC Brine 0 365
2014 ENERVEST OPERATING LLC Brine 0 365
2015 ENERVEST OPERATING LLC Brine 0 303

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1422786378 2012-4-18 0:00: PW No Violations
-1514027759 2015-9-1 0:00:0 FR No Violations 1.00
-1516789880 2014-12-29 0:00 PW No Violations 2.00
1258663680 2009-11-17 Production Wells No Violations Inspection revealed that well is equipped with pumping unit and tubing and rods and 1-210 bbl tank located in dike area.
1422786378 2012-04-18 Production Wells No Violations Inspection of well found the following equipment -8.625 surface casing -4.5 production casing -2.375 tubing with the production valves open and the well being produced by means of a pumping unit , 210 tank and separator located in a shared dike with other wells in area ,identification present on well and tank .
1434478631 2015-06-15 Plug / Plug Back No Violations My inspection today finds Berry Well Service pulled the casing up to 1760 where Petroset spotted a 50 sack class A 2% gel plug. The casing was then pulled up to 200 and Petroset pumped a 60 sack plug to surface. The cement was topped off and the cement stayed at surface.
1510864169 2015-06-22 Plug / Plug Back No Violations The well has been plugged resolving the previous violation.
1514027759 2015-09-01 Final Restoration No Violations My inspection today finds the well site meets the requirements of 1509.072(B).
1516789880 2014-12-29 Production Wells Violations Noted I received a telephone call from the landowner Lamar Dowling indicating that the well casing failed and he was forced to disconnect from the well due to H2S. I called the well tender David Williams and he corroborated the landowners statements. Upon arrival I found the well was equipped with 4.5 casing with a 4.5 ball valve in the closed position. All valves were closed at the time of inspection. Upon the discovery that the casing in a well is defective or that a well was not adequately constructed, the owner of the well shall notify the Chief of the Division of Oil and Gas Resources Management within twenty-four hours of discovery, and the owner shall immediately repair the casing, correct the construction inadequacies, or plug the well. The well shall be repaired or plugged within 180 days.
1578471921 2015-06-12 Plug / Plug Back No Violations On site to witness rig crew rip pipe and set lime plug they cut pipe off at 4010 and pulled one joint of casing and set 200 plug and pipe became stuck in the well bore had to work hard to get pipe freed up and they pulled 32 joints today and will resume plugging operation on Monday 6/15/15.
1629458513 2015-06-10 Production Wells No Violations I received a voice mail from Donnie with Barry Well Service indicating that the company was preparing to plug the well. My inspection of the site finds Barry Well Service has moved a service rig onto location. Upon arrival I was given twenty four hour notice of intent to plug.
1813578794 2015-06-11 Plug / Plug Back No Violations My inspection today finds the service contractor, Barry Well Service, ran 5729 of 1.5 tubing into the well. Petroset pumped a 30 sack class A plug to 5738 and displaced with 14.2 barrels of water.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1516789880 US-OH-114395 2015-06-22 Defective casing, leaking well

For data sources see[9]

References