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Well ID: 34-121-21361 | Loading map...
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Country: United States | |
State: Ohio | |
County: Noble | |
Municipality: Brookfield Township | |
Operator Name: GREEN GAS CO | |
Well Pad ID: | |
Farm/Lease Name: STONEKING | |
License Status: Final Restoration | |
License Date: 2012-11-30 | |
Spud Date: 1969-10-19 | |
Spud Drilling Contractor: | |
Final Drill Date: 1969-11-02 | |
Well Total Depth: 5532.00 ft | |
Configuration: Vertical | |
Latitude: 39.820000 | |
Longitude: -81.610000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1959-10-19 | |
Completed | 1969-11-02 | |
Reached Total Depth | 1969-11-02 | |
Completion Report Received | 1970-10-09 | |
CO | 1982-07-13 | 201 GREEN GAS CO GeoDate 7/13/82 |
APP | 2012-11-30 | Proposed Formations:CLINTON, Issued Date:11/30/2012, Expired Date:11/30/2014 12:00:00 PM, Drilling unit acres:136.4, Proposed Well Type:OG, Proposed Well Class: |
Construction Permit Expires | 2014-11-30 | |
Plugged/Abandoned | 2016-07-01 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5291 | 5479 | 0 |
5291 | 5479 | 0 | |
5291 | 5479 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 3016 Bbl | 70000 | R.P. 72 HRS. NSR | ||
N2 | 0 | 200 Mscf | 0 | |||
FOAM | 0 | 3016 Bbl | 70000 | 200M SCF N2 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | NOBLE GAS CO | 6293.00 | 0.00 | 0 |
1985 | NOBLE GAS CO | 4879.00 | 0.00 | 0 |
1986 | NOBLE GAS CO | 1704.00 | 0.00 | 365 |
1995 | NOBLE GAS CO | 331.00 | 0.00 | 365 |
1998 | GREEN GAS CO | 1150.00 | 0.00 | 365 |
1999 | GREEN GAS CO | 0.00 | 0.00 | 0 |
2000 | GREEN GAS CO | 0.00 | 0.00 | 0 |
2001 | GREEN GAS CO | 0.00 | 0.00 | 0 |
2002 | GREEN GAS CO | 0.00 | 0.00 | 0 |
2012 | GREEN GAS CO | 0.00 | 0.00 | 0 |
2013 | GREEN GAS CO | 0.00 | 0.00 | 0 |
2014 | GREEN GAS CO | 0.00 | 0.00 | 0 |
2016 | GREEN GAS CO | 0.00 | 0.00 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | NOBLE GAS CO | Brine | 0 | 0 |
1985 | NOBLE GAS CO | Brine | 0 | 0 |
1986 | NOBLE GAS CO | Brine | 0 | 365 |
1995 | NOBLE GAS CO | Brine | 0 | 365 |
1998 | GREEN GAS CO | Brine | 0 | 365 |
1999 | GREEN GAS CO | Brine | 0 | 0 |
2000 | GREEN GAS CO | Brine | 0 | 0 |
2001 | GREEN GAS CO | Brine | 0 | 0 |
2002 | GREEN GAS CO | Brine | 0 | 0 |
2012 | GREEN GAS CO | Brine | 0 | 0 |
2013 | GREEN GAS CO | Brine | 0 | 0 |
2014 | GREEN GAS CO | Brine | 0 | 0 |
2016 | GREEN GAS CO | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1521332839 | 2015-12-30 0:00 | PW | No Violations | 2.00 |
-1825302504 | 2011-7-22 0:00: | PW | No Violations | |
-2108297637 | 2016-7-21 0:00: | FR | No Violations | 1.00 |
-308724996 | 2015-9-29 0:00: | AM | No Violations | |
-711384678 | 2011-9-26 0:00: | PW | No Violations | |
0187860301 | 2014-09-16 | Administrative Inspection | No Violations | I stopped at Green Gass shop and spoke to Scott Davis field superintendent. Mr. Davis stated that his plugging contractor would be plugging the well in October. |
0308724996 | 2015-09-29 | Administrative Inspection | No Violations | At 2:29 pm I received a call from Scott Davis in response to a voice mail I left. Mr. Davis and I discussed the companys plan for the well. Mr. Davis stated that he was going plug the well. Mr. Davis stated that he would remove the leaking tank in next two weeks. I reminded Mr. Davis that the well has been in violation for more that four years. |
0711384678 | 2011-09-26 | Production Wells | No Violations | No change in status of well. It still remains idle at this time. |
1141881142 | 2016-09-20 | Final Restoration | No Violations | My inspection today finds the well site meets the final restoration requirements of 1509.072(B). |
1195389157 | 2013-10-10 | Administrative Inspection | No Violations | I spoke to Scott Davis of Green Gas on 10-10-2013. Mr. Davis stated that they will plug the well as soon as the contractor they use becomes available. |
1311370399 | 2011-07-22 | Production Wells | Violations Noted | Upon receiving complaint from landowner John Denny of idle well on property inspected site and found well to be idle and incapable of producing in its present state of repair, well is equipped with 8 surface casing and 4.5 production casing and 1-100 bbl tank and separator located in thick brush pile.The last production reported on well was back in 1998 and all valves at wellhead were shut on the day of my inspection ad also there is no identification on tank or wellhead.
PLUG OR PRODUCE WELL OR FIL FOR TEMPORARY INACTIVE STATUS. FAILURE TO COMPLY MAY RESULT IN BOND FORFIETURE. |
1352814615 | 2012-11-13 | Production Wells | No Violations | My inspection today finds that the status of the well has not changed. The well is still idle. I stopped at Green Gass shop and informed the owner Scott Davis that he needed to file for a plugging permit within 30 days to avoid further action. |
1467292586 | 2016-06-30 | Plug / Plug Back | No Violations | I am onsite to witness the plugging operations. At the time of my arrival the 2.375 tubing was set at a depth of 5320. A 30 sack 400 class A cement plug was placed by Formation Cementing. The plug was displaced with 18.9 barrels of brine. The tubing was pulled up to 3970. Timco perforated the 4.5 casing at a depth of 4034 to 4024 with ten shots. The tubing was installed back to a depth of 4034 and a 57 sack plug was placed. |
1467378995 | 2016-07-01 | Plug / Plug Back | No Violations | On site inspection to witness the final stages of the well plugging process. On this day a service rig was on the hole owned by Thompson Well Service and 3 plugs were set through 2.375 tubing inside of the open well bore. The 1st plug was 54 sacks of cement and set from 1,669 to 1,469 to cover the Berea Sand formation. The 2nd plug was set from 598 to 398 to cover the bottom of the 8.625 surface casing at 507. The 3rd plug was set from 200 to surface and consisted of 60 sacks of cement with a plugs being set having a weight of 15.6 lb/gl -1% gel-1% calcium. Cement was witnessed to surface and the company was going to cut the casing off at 30 below grade-place a permanent marker on the surface casing and close the pit on this day. |
1521332839 | 2015-12-30 | Production Wells | No Violations | My inspection today finds the well is shut in and disconnected from any pipelines. The tank battery consists of one 100 barrel tank and a separator. The 100 barrel tank is seeping at the bottom and oily fluid has covered an area approximately 15 x 5. The tank battery is overgrown with vegetation. Photos were taken. |
1640474658 | 2014-03-13 | Production Wells | No Violations | My inspection finds the well is equipped with 4.5 casing. All production valves are closed. The tank battery consist of one 100 bbl tank and a production unit. There is an oil saturated area, approximately 15 square feet, at the base of the tank. The company has a permit to plug the well. |
1825302504 | 2011-07-22 | Production Wells | No Violations | FOLLOW UP TO NOV # 1311370399 Upon receiving complaint from landowner John Denny of idle well on property inspected site and found well to be idle and incapable of producing in its present state of repair, well is equipped with 8 surface casing and 4.5 production casing and 1-100 bbl tank and separator located in thick brush pile.The last production reported on well was back in 1998 and all valves at wellhead were shut on the day of my inspection ad also there is no identification on tank or wellhead.
PLUG OR PRODUCE WELL OR FIL FOR TEMPORARY INACTIVE STATUS. FAILURE TO COMPLY MAY RESULT IN BOND FORFIETURE. |
1863164911 | 2015-08-31 | Production Wells | No Violations | My inspection today finds the well is not capable of production. There are no gas or oil pipelines attached to the wellhead. The tank battery is overgrown with vegetation. The 100 barrel tank is leaking oil from underneath of it. |
187860301 | 2014-9-16 0:00: | AM | No Violations | 0.30 |
2093802599 | 2015-04-15 | Production Wells | No Violations | My inspection today finds the well is not capable of production. There are no gas or oil pipelines attached to the wellhead. The tank battery is overgrown with vegetation. The 100 barrel tank is leaking oil from underneath of it. |
2108297637 | 2016-07-21 | Final Restoration | No Violations | My inspection today finds the pits have been closed and the production equipment has been removed. The well has been plugged resolving the previous violation. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1311370399 | US-OH-108641 | 2011-07-22 | Failure to legibly identify well | |
1311370399 | US-OH-108642 | 2011-07-22 | Well shall be plugged | |
1311370399 | US-OH-108643 | 2011-07-22 | Nonproduction; well shall be plugged or placed in temporary inactive status |
For data sources see[9]