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Well ID: 34-119-27983 | Loading map...
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Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Meigs Township | |
Operator Name: ATLAS NOBLE LLC | |
Well Pad ID: | |
Farm/Lease Name: OHIO POWER | |
License Status: Final Restoration | |
License Date: 2016-07-13 | |
Spud Date: 1995-10-03 | |
Spud Drilling Contractor: MATTMARK DRILLING | |
Final Drill Date: 1995-10-11 | |
Well Total Depth: 5315.00 ft | |
Configuration: Vertical | |
Latitude: 39.800000 | |
Longitude: -81.700000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1995-06-30 | 3071 KINGSTON OIL CORP GeoDate 6/30/95 |
Oil and Gas | 1995-06-30 | Issued Date 6/30/95 Expired Date 6/29/96 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05315 Proposed Drill Depth 05315 |
Original Spud | 1995-10-04 | GMM STATUS CHANGED TO PLUGGED PER PLUG REPORT. UPDATED WELL LOCATION PER SURVEYOR'S COORDINATES ALE 03/29/2017. |
Completed | 1995-10-11 | GMM STATUS CHANGED TO PLUGGED PER PLUG REPORT. UPDATED WELL LOCATION PER SURVEYOR'S COORDINATES ALE 03/29/2017. |
Reached Total Depth | 1995-10-11 | GMM STATUS CHANGED TO PLUGGED PER PLUG REPORT. UPDATED WELL LOCATION PER SURVEYOR'S COORDINATES ALE 03/29/2017. |
Completion Report Received | 1995-11-24 | GMM STATUS CHANGED TO PLUGGED PER PLUG REPORT. UPDATED WELL LOCATION PER SURVEYOR'S COORDINATES ALE 03/29/2017. |
Change of Owner | 2001-01-12 | Operator changed from 3071, KINGSTON OIL CORP to 6867, ATLAS AMERICA INC |
Change of Owner | 2004-03-23 | Operator changed from 6867, ATLAS AMERICA INC to 6866, ATLAS NOBLE INC |
APP | 2016-07-13 | Proposed Formations:CLINTON, Issued Date:7/13/2016, Expired Date:7/13/2018 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2016-09-29 | GMM STATUS CHANGED TO PLUGGED PER PLUG REPORT. UPDATED WELL LOCATION PER SURVEYOR'S COORDINATES ALE 03/29/2017. |
Construction Permit Expires | 2018-07-13 | GMM STATUS CHANGED TO PLUGGED PER PLUG REPORT. UPDATED WELL LOCATION PER SURVEYOR'S COORDINATES ALE 03/29/2017. |
Record Last Modified | 2018-08-07 | GMM STATUS CHANGED TO PLUGGED PER PLUG REPORT. UPDATED WELL LOCATION PER SURVEYOR'S COORDINATES ALE 03/29/2017. |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 5012 | 2 | |
5001 | 5086 | 0 | |
2006-09-11 | 5059 | 5066 | 7 |
5012 | 2 | ||
5001 | 5086 | 0 | |
1997-06-29 | 5001 | 5086 | 0 |
2006-09-11 | 5161 | 5164 | 3 |
2006-09-11 | 5070 | 5080 | 8 |
2006-09-11 | 5043 | 5053 | 1 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 15 | 700 Gal | 0 | FRAC W/2700 BW & 425 SX SAND | ||
H2O | 0 | 2700 Bbl | 0 | 425SKS 20/40 SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1996 | KINGSTON OIL CORP | 18531.00 | 0.00 | 290 |
1997 | KINGSTON OIL CORP | 11878.00 | 0.00 | 350 |
1998 | KINGSTON OIL CORP | 11736.00 | 0.00 | 350 |
1999 | KINGSTON OIL CORP | 9546.00 | 0.00 | 0 |
2000 | KINGSTON OIL CORP | 10767.00 | 0.00 | 0 |
2001 | CHEVRON APPALACHIA LLC | 6592.00 | 0.00 | 330 |
2002 | CHEVRON APPALACHIA LLC | 8608.00 | 0.00 | 365 |
2003 | ATLAS NOBLE LLC | 6999.00 | 32.00 | 365 |
2004 | ATLAS NOBLE LLC | 5948.00 | 0.00 | 365 |
2005 | ATLAS NOBLE LLC | 5119.00 | 0.00 | 365 |
2006 | ATLAS NOBLE LLC | 4747.00 | 0.00 | 365 |
2007 | ATLAS NOBLE LLC | 4347.00 | 0.00 | 365 |
2008 | ATLAS NOBLE LLC | 3914.00 | 35.00 | 366 |
2009 | ATLAS NOBLE LLC | 3359.00 | 0.00 | 365 |
2010 | ATLAS NOBLE LLC | 297.00 | 0.00 | 365 |
2011 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2012 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2013 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2014 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2015 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2016 | ATLAS NOBLE LLC | 0.00 | 0.00 | 366 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1996 | KINGSTON OIL CORP | Brine | 209 | 290 |
1997 | KINGSTON OIL CORP | Brine | 0 | 350 |
1998 | KINGSTON OIL CORP | Brine | 0 | 350 |
1999 | KINGSTON OIL CORP | Brine | 0 | |
2000 | KINGSTON OIL CORP | Brine | 40 | |
2001 | CHEVRON APPALACHIA LLC | Brine | 0 | 330 |
2002 | CHEVRON APPALACHIA LLC | Brine | 57 | 365 |
2003 | ATLAS NOBLE LLC | Brine | 0 | 365 |
2004 | ATLAS NOBLE LLC | Brine | 57 | 365 |
2005 | ATLAS NOBLE LLC | Brine | 80 | 365 |
2006 | ATLAS NOBLE LLC | Brine | 47 | 365 |
2007 | ATLAS NOBLE LLC | Brine | 80 | 365 |
2008 | ATLAS NOBLE LLC | Brine | 48 | 366 |
2009 | ATLAS NOBLE LLC | Brine | 80 | 365 |
2010 | ATLAS NOBLE LLC | Brine | 0 | 365 |
2011 | ATLAS NOBLE LLC | Brine | 30 | |
2012 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2013 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2014 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2015 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2016 | ATLAS NOBLE LLC | Brine | 68 | 366 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1138579469 | 2016-4-21 0:00: | PW | No Violations | 1.00 |
-1456103411 | 2016-9-28 0:00: | PB | No Violations | 3.50 |
-1592476424 | 2017-1-20 0:00: | FR | No Violations | 1.00 |
-746620090 | 2015-11-5 0:00: | PW | No Violations | 1.00 |
-795391656 | 2004-12-8 0:00: | PL | No Violations | |
-884335104 | 2016-8-2 0:00:0 | PW | No Violations | 2.50 |
0049643701 | 2003-10-22 | Production Wells | No Violations | |
0383719683 | 2016-09-29 | Plug / Plug Back | No Violations | The Compliance Notice 1455722146 has been plugged in accordance with OAC 1501-9-11. This resolves the Compliance Notice that was issued to the Company. |
0646513560 | 2008-01-14 | Production Wells | No Violations | Producing, no problems noted |
0746620090 | 2015-11-05 | Production Wells | No Violations | Well is shut in due to H2S. There is a wind sock at the wellhead. The well is equipped with a gas plunger lift system. There is a 8.625x 4.5well head and a 4.5x 2.375tubing head. The tubing valve is shut in and the tubing annulus is shut in. The 4.5casing and the 2.375tubing are decomposing due to the corrosive environment. There is motor valve that is unhooked and in the closed position. The flow line is shut in and closed. There is a bull plug needed for the 2valve on the 4.5casing annulus. There is 1-210 barrel steel tank that has leak on the side about 4 from the bottom. There is a 30 barrel steel tank and the dike surrounds the tanks. There are identifications at the well and the tank. Well will need plugged. The well coordinates are 39.80023, -81.70308 epe6. The tank coordinates are 39.80170, -81.70596 epe6. The entry coordinates are 39.80172, -81.70563 epe9. |
0795391656 | 2004-12-08 | Preliminary Restoration | No Violations | |
0884335104 | 2016-08-02 | Production Wells | No Violations | Trisha Cartmell and I went out to the well to check the condition of the well and the tank site. The well and tank site were both shut in and secure. The wind sock was still in place at the wellhead. Atlas Noble LLC man Pat Irving stated that rig will be moving in on site approximately 2-3 weeks. |
1103606693 | 2010-03-29 | Production Wells | No Violations | Producing, rabbit well, no problems noted. |
1138579469 | 2016-04-21 | Production Wells | No Violations | On the day of my inspection I was accompanied by Austin Gutridge. The well is on the plugging list. The well is an H2S well. The valves were shut and not blowing gas into the atmosphere. I will call Pat Irving with Atlas. The wind sock is currently up at the well. |
1310610699 | 2006-08-30 | Production Wells | No Violations | Producing |
1455722146 | 2016-02-17 | Production Wells | Violations Noted | 08:30-10:30 Well 119-27983 well owned by Atlas is being issued a Compliance Notice for the following: Well is shut in due to H2S. There is a wind sock at the wellhead. The well is equipped with a gas plunger lift system. There is a 8.625x 4.5well head and a 4.5x 2.375tubing head. The tubing valve is shut in and the tubing annulus is shut in. The 4.5casing and the 2.375tubing are decomposing due to the corrosive environment. There is motor valve that is unhooked and in the closed position. The flow line is shut in and closed. There is a bull plug needed for the 2valve on the 4.5casing annulus. There is 1-210 barrel steel tank that has leak on the side about 4 from the bottom. There is a 30 barrel steel tank and the dike surrounds the tanks. There are identifications at the well and the tank. Well will need plugged. There has been no production filed since 2011. The well coordinates are 39.80023, -81.70308 epe6. The tank coordinates are 39.80170, -81.70596 epe6. The entry coordinates are 39.80172, -81.70563 epe9. The well owner /operator shall submit a written plugging schedule to Patrick Shreve at 5880 Memory Rd. Zanesville, Ohio 43701 within 30 days per OAC 1501:9-11-05(B) and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied. |
1456103411 | 2016-09-28 | Plug / Plug Back | No Violations
- | |
1474457004 | 2016-09-07 | Production Wells | No Violations | The purpose of the inspection is a Compliance Notice Follow--210 barrel steel tank that the bottom half is rusting away causing leakage and there is 1-30 barrel steel with that is shut in with locks. There were pictures taken that are on file. |
1592476424 | 2017-01-20 | Final Restoration | No Violations | Final Restoration did not pass on 1-20-17 by Patrick Shreve. Well was plugged in compliance OAC 1501-9-11. The land however was not restored back under ORC 1509.072. The lease road and the site were just roughed in. The site needs to be final graded and then seed and mulch in place. Tom Smith and I found old well casing with Magnetic pipe locator GA-52CX and the coordinates were updated with the Trimble unit. |
1853411402 | 2016-09-29 | Plug / Plug Back | No Violations
| |
1915751908 | 2018-06-20 | Final Restoration | No Violations | The inspection was conducted under hot, humid and dry conditions. The temperature is 80 degrees Fahrenheit. The Final Restoration passed on this day of 6-20-18 by Patrick Shreve. The vegetation is sufficient to prevent substantial erosion. |
383719683 | 2016-9-29 0:00: | PB | No Violations | 8.00 |
49643701 | 2003-10-22 0:00 | PW | No Violations | |
646513560 | 2008-1-14 0:00: | PW | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1455722146 | US-OH-113188 | 2016-10-31 | General Safety | |
1455722146 | US-OH-113189 | 2016-10-31 | Well shall be plugged | |
1455722146 | US-OH-113190 | 2016-10-31 | Statement of annual production not filed |
For data sources see[9]