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34-119-27136

Well Details

Well ID: 34-119-27136
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Country: United States
State: Ohio
County: Muskingum
Municipality: Rich Hill Township
Operator Name: M & R INVESTMENTS OHIO LLC
Well Pad ID:
Farm/Lease Name: OHIO POWER
License Status: Plugged and Abandoned
License Date: 2018-08-08
Spud Date: 1984-08-23
Spud Drilling Contractor: DYNAMIC DRILLING
Final Drill Date: 1984-08-28
Well Total Depth: 5061.00 ft
Configuration: Vertical
Latitude: 39.890000
Longitude: -81.730000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1984-08-07 Issued Date 8/7/84 Expired Date 2/3/85 Acres 0080000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05061 Proposed Drill Depth 05061
Original Spud 1984-08-23
Completed 1984-08-28
Reached Total Depth 1984-08-28
Completion Report Received 1984-09-13
CO 1984-11-12 1115 CAVENDISH PETRO OF OH INC GeoDate 8/7/84
CO 1996-05-01 3071 KINGSTON OIL CORP GeoDate 8/7/84
Change of Owner 2001-01-12 Operator changed from 3071, KINGSTON OIL CORP to 6867, ATLAS AMERICA INC
Change of Owner 2004-03-23 Operator changed from 6867, ATLAS AMERICA INC to 6866, ATLAS NOBLE INC
APP 2017-02-02 Proposed Formations:CLINTON, Issued Date:2/2/2017, Expired Date:2/2/2019 12:00:00 PM, Drilling unit acres:80, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2017-10-17 Operator changed from 6866, ATLAS NOBLE LLC to 8685, M & R INVESTMENTS OHIO LLC
APP 2018-08-08 Proposed Formations:CLINTON, Issued Date:8/8/2018, Expired Date:8/7/2020 12:00:00 PM, Drilling unit acres:80, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2018-10-29
Record Last Modified 2019-01-31
Construction Permit Expires 2020-08-07

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4798 4954 1
4826 4890 0
1997-06-29 4826 4890 0
4798 4954 1
4798 4954 1

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
CO2 0 17 Tons 0 F/W ACID
H2O 0 45500 Gal 0 FRAC: H2O,SAND,CO2

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 CALTEK MINERALS CORP 0.00 143.00 0
1985 CAVENDISH PETRO OF OH INC 6948.00 523.00 365
1986 CAVENDISH PETRO OF OH INC 3732.00 442.00 0
1987 CAVENDISH PETRO OF OH INC 3097.00 255.00 0
1988 CAVENDISH PETRO OF OH INC 2615.00 250.00 365
1989 CAVENDISH PETRO OF OH INC 920.00 138.00 365
1990 KINGSTON OIL CORP 1219.00 124.00 365
1991 KINGSTON OIL CORP 1104.00 224.00 365
1992 KINGSTON OIL CORP 898.00 147.00 350
1993 KINGSTON OIL CORP 803.00 173.00 350
1994 KINGSTON OIL CORP 977.00 160.00 350
1995 KINGSTON OIL CORP 811.00 115.00 350
1996 KINGSTON OIL CORP 566.00 170.00 350
1997 KINGSTON OIL CORP 568.00 204.00 350
1998 KINGSTON OIL CORP 645.00 183.00 350
1999 KINGSTON OIL CORP 606.00 133.00 0
2000 KINGSTON OIL CORP 1203.00 119.00 0
2001 CHEVRON APPALACHIA LLC 788.00 200.00 330
2002 CHEVRON APPALACHIA LLC 646.00 95.00 365
2003 ATLAS NOBLE LLC 490.00 158.00 365
2004 ATLAS NOBLE LLC 571.00 167.00 365
2005 ATLAS NOBLE LLC 718.00 167.00 365
2006 ATLAS NOBLE LLC 740.00 106.00 365
2007 ATLAS NOBLE LLC 639.00 178.00 365
2008 ATLAS NOBLE LLC 672.00 141.00 366
2009 ATLAS NOBLE LLC 661.00 106.00 365
2010 ATLAS NOBLE LLC 603.00 45.00 365
2011 ATLAS NOBLE LLC 680.00 112.00 0
2012 ATLAS NOBLE LLC 291.00 65.00 179
2013 ATLAS NOBLE LLC 0.00 0.00 0
2014 ATLAS NOBLE LLC 0.00 0.00 0
2015 ATLAS NOBLE LLC 0.00 0.00 0
2016 ATLAS NOBLE LLC 0.00 0.00 0
2017 M & R INVESTMENTS OHIO LLC 0.00 0.00 0
2018 M & R INVESTMENTS OHIO LLC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 CALTEK MINERALS CORP Brine 0 0
1985 CAVENDISH PETRO OF OH INC Brine 24 365
1986 CAVENDISH PETRO OF OH INC Brine 0 0
1987 CAVENDISH PETRO OF OH INC Brine 0 0
1988 CAVENDISH PETRO OF OH INC Brine 0 365
1989 CAVENDISH PETRO OF OH INC Brine 0 365
1990 KINGSTON OIL CORP Brine 35 365
1991 KINGSTON OIL CORP Brine 0 365
1992 KINGSTON OIL CORP Brine 0 350
1993 KINGSTON OIL CORP Brine 0 350
1994 KINGSTON OIL CORP Brine 0 350
1995 KINGSTON OIL CORP Brine 0 350
1996 KINGSTON OIL CORP Brine 0 350
1997 KINGSTON OIL CORP Brine 35 350
1998 KINGSTON OIL CORP Brine 0 350
1999 KINGSTON OIL CORP Brine 0
2000 KINGSTON OIL CORP Brine 0
2001 CHEVRON APPALACHIA LLC Brine 0 330
2002 CHEVRON APPALACHIA LLC Brine 0 365
2003 ATLAS NOBLE LLC Brine 0 365
2004 ATLAS NOBLE LLC Brine 0 365
2005 ATLAS NOBLE LLC Brine 9 365
2006 ATLAS NOBLE LLC Brine 20 365
2007 ATLAS NOBLE LLC Brine 0 365
2008 ATLAS NOBLE LLC Brine 18 366
2009 ATLAS NOBLE LLC Brine 0 365
2010 ATLAS NOBLE LLC Brine 0 365
2011 ATLAS NOBLE LLC Brine 4
2012 ATLAS NOBLE LLC Brine 0 179
2013 ATLAS NOBLE LLC Brine 0 0
2014 ATLAS NOBLE LLC Brine 0 0
2015 ATLAS NOBLE LLC Brine 10 0
2016 ATLAS NOBLE LLC Brine 0 0
2017 ATLAS NOBLE LLC Brine 0 0
2018 M & R INVESTMENTS OHIO LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-171772050 2016-9-13 0:00: PW No Violations 1.00
-1827515817 2016-9-14 0:00: AM No Violations
-33593851 2017-11-14 0:00 PW No Violations 1.00
-859371591 2018-10-29 0:00 PB No Violations 11.00
0000PL8128 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0033593851 2017-11-14 Production Wells No Violations The purpose of my inspection is due to a follow-up to Compliance Notice number -
0125746126 2018-10-26 Plug / Plug Back No Violations The inspection was conducted under plugging operations and a Compliance Notice Follow-up to number -171772050. Wright well service had all 2 3/8--inch casing off at 3744 feet. There was crude oil in the casing. The crude oil will be circulated out of the well bore before the cementing starts.
0171772050 2016-09-13 Production Wells Violations Noted

-11-05(B) and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied.

0662611424 2017-07-19 Production Wells No Violations On the day of my inspection, Surveyor, Tom Smith and I went in to the well site to verify the location with a Trimble unit prior to plugging the well. A plugging permit has been issued and the well was shut in and idle on the day of my inspection.
0757446749 2008-05-27 Production Wells No Violations Could not get to well as beavers have road blocked in two directions and it was too cold to go wading. Checked meter chart and well is producing gas.
0859371591 2018-10-29 Plug / Plug Back No Violations The inspection was conducted under plugging operations and a Compliance Notice Follow-up to number --3404 feet. They ran 85 sacks of regular class A cement and 1 % CaCl. There was cotton seed hulls placed in the slurry. The displacement was 54 barrels of salt water. The bottom of the 8 5/8-inch casing was at 1674 feet. The plug was set at 1774-1574 feet with 60 sacks of regular class A cement at 1% CaCl. Broke circulation with fresh water set the plug and displaced down with 24 barrels of fresh water. Wright pulled all the casing out and topped off the well with a 200-foot cement plug in 8 5/8- inch casing. There was small stone plug set at 200. Formation Cementing ran 54 sacks of Regular class A cement. The plugging operation is complete and resolved the Compliance Notice.
1201360313 2019-11-18 0:00 FR No Violations 1.50
125746126 2018-10-26 0:00 PB No Violations 4.10
1742688289 2018-10-25 Plug / Plug Back No Violations The inspection was conducted under plugging operations and a Compliance Notice Follow-up to number -171772050. Wright well service was rigged up over the well and had tripped all 2 3/8- inch tubing out and ran in opened ended to 4770 feet. Formation Cementing services were on site and would set the bottom Clinton plug from 4770-4370 feet with 30 sacks of regular class A cement. The plug was placed thru 2 3/8-
1827515817 2016-09-14 Administrative Inspection No Violations I called Pat Irving of Atlas and stated the well has gas emitting from the well. This a follow-up with the company stating they will be receiving an inspection with number -171772050. He said he would apply for a Plugging Permit or fix the flowline.
2122249944 2017-01-12 Production Wells No Violations The purpose of the inspection is due to a follow-up on Compliance Notice number -171772050. The Company Atlas representatives were Chuck Wood, Chris Belch and Matt Kapanus. The Company Representatives and I Inspector Patrick Shreve entered the well site and verified the status of the well. They opened the tubing and the casing annulus to check for H2S. There was no H2S present that registered on the day of the inspection. The well is shut in and idle due to a tank battery that had been removed from the site. The well is not capable of production. The well will be plugged but may move to low threat due to no smell on the well. They will be in touch and get back with me on the status.
662611424 2017-7-19 0:00: PW No Violations 1.00
757446749 2008-5-27 0:00: PW No Violations
PL8128 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0171772050 US-OH-117043 2018-11-27 9-9-02 General Safety
0171772050 US-OH-117044 2018-11-27 9-9-05(A)1 Well insufficiently equipped to prevent escape of oil and gas
0171772050 US-OH-117045 2018-11-27 NONE Well shall be plugged

For data sources see[9]

References