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Well ID: 34-119-27115 | Loading map...
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Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Rich Hill Township | |
Operator Name: M & R INVESTMENTS OHIO LLC | |
Well Pad ID: | |
Farm/Lease Name: OHIO POWER | |
License Status: Final Restoration | |
License Date: 2018-08-08 | |
Spud Date: 1984-08-12 | |
Spud Drilling Contractor: DYNAMIC DRILLING | |
Final Drill Date: 1984-08-16 | |
Well Total Depth: 5087.00 ft | |
Configuration: Vertical | |
Latitude: 39.890000 | |
Longitude: -81.740000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1984-07-19 | Issued Date 7/19/84 Expired Date 1/15/85 Acres 0080000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 05087 Proposed Drill Depth 05087 |
Original Spud | 1984-08-12 | |
Completed | 1984-08-16 | |
Reached Total Depth | 1984-08-16 | |
Completion Report Received | 1984-09-13 | |
CO | 1984-11-14 | 1115 CAVENDISH PETRO OF OH INC GeoDate 7/19/84 |
CO | 1996-05-01 | 3071 KINGSTON OIL CORP GeoDate 7/19/84 |
Change of Owner | 2001-01-12 | Operator changed from 3071, KINGSTON OIL CORP to 6867, ATLAS AMERICA INC |
Change of Owner | 2004-03-23 | Operator changed from 6867, ATLAS AMERICA INC to 6866, ATLAS NOBLE INC |
APP | 2017-02-02 | Proposed Formations:CLINTON, Issued Date:2/2/2017, Expired Date:2/2/2019 12:00:00 PM, Drilling unit acres:80, Proposed Well Type:OG, Proposed Well Class: |
Change of Owner | 2017-10-17 | Operator changed from 6866, ATLAS NOBLE LLC to 8685, M & R INVESTMENTS OHIO LLC |
APP | 2018-08-08 | Proposed Formations:CLINTON, Issued Date:8/8/2018, Expired Date:8/7/2020 12:00:00 PM, Drilling unit acres:80, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2018-10-23 | |
Record Last Modified | 2019-01-31 | |
Construction Permit Expires | 2020-08-07 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 4852 | 4916 | 0 |
4852 | 4916 | 0 | |
2006-09-11 | 4957 | 4979 | 12 |
4957 | 4979 | 12 | |
4852 | 4916 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
CO2 | 0 | 16 Tons | 0 | |||
H2O | 0 | 45000 Gal | 0 | FRAC: H2O,SAND,CO2 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | CALTEK MINERALS CORP | 0.00 | 487.00 | 0 |
1985 | CAVENDISH PETRO OF OH INC | 5365.00 | 1730.00 | 365 |
1986 | CAVENDISH PETRO OF OH INC | 3313.00 | 812.00 | 0 |
1987 | CAVENDISH PETRO OF OH INC | 1864.00 | 317.00 | 0 |
1988 | CAVENDISH PETRO OF OH INC | 0.00 | 0.00 | 365 |
1989 | CAVENDISH PETRO OF OH INC | 151.00 | 70.00 | 365 |
1990 | KINGSTON OIL CORP | 1810.00 | 580.00 | 365 |
1991 | KINGSTON OIL CORP | 2302.00 | 460.00 | 365 |
1992 | KINGSTON OIL CORP | 1681.00 | 236.00 | 350 |
1993 | KINGSTON OIL CORP | 1524.00 | 88.00 | 350 |
1994 | KINGSTON OIL CORP | 2096.00 | 134.00 | 350 |
1995 | KINGSTON OIL CORP | 1720.00 | 272.00 | 350 |
1996 | KINGSTON OIL CORP | 1505.00 | 236.00 | 350 |
1997 | KINGSTON OIL CORP | 1422.00 | 214.00 | 350 |
1998 | KINGSTON OIL CORP | 1347.00 | 201.00 | 350 |
1999 | KINGSTON OIL CORP | 1426.00 | 167.00 | 0 |
2000 | KINGSTON OIL CORP | 1589.00 | 114.00 | 0 |
2001 | CHEVRON APPALACHIA LLC | 934.00 | 99.00 | 330 |
2002 | CHEVRON APPALACHIA LLC | 1286.00 | 198.00 | 365 |
2003 | ATLAS NOBLE LLC | 1239.00 | 170.00 | 365 |
2004 | ATLAS NOBLE LLC | 1301.00 | 95.00 | 365 |
2005 | ATLAS NOBLE LLC | 1228.00 | 130.00 | 365 |
2006 | ATLAS NOBLE LLC | 1382.00 | 90.00 | 365 |
2007 | ATLAS NOBLE LLC | 1174.00 | 140.00 | 365 |
2008 | ATLAS NOBLE LLC | 959.00 | 93.00 | 366 |
2009 | ATLAS NOBLE LLC | 1130.00 | 99.00 | 365 |
2010 | ATLAS NOBLE LLC | 1020.00 | 108.00 | 365 |
2011 | ATLAS NOBLE LLC | 876.00 | 93.00 | 0 |
2012 | ATLAS NOBLE LLC | 357.00 | 83.00 | 271 |
2013 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2014 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2015 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2016 | ATLAS NOBLE LLC | 0.00 | 0.00 | 0 |
2017 | M & R INVESTMENTS OHIO LLC | 0.00 | 0.00 | 0 |
2018 | M & R INVESTMENTS OHIO LLC | 0.00 | 0.00 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | CALTEK MINERALS CORP | Brine | 0 | 0 |
1985 | CAVENDISH PETRO OF OH INC | Brine | 62 | 365 |
1986 | CAVENDISH PETRO OF OH INC | Brine | 30 | 0 |
1987 | CAVENDISH PETRO OF OH INC | Brine | 60 | 0 |
1988 | CAVENDISH PETRO OF OH INC | Brine | 0 | 365 |
1989 | CAVENDISH PETRO OF OH INC | Brine | 0 | 365 |
1990 | KINGSTON OIL CORP | Brine | 165 | 365 |
1991 | KINGSTON OIL CORP | Brine | 80 | 365 |
1992 | KINGSTON OIL CORP | Brine | 0 | 350 |
1993 | KINGSTON OIL CORP | Brine | 69 | 350 |
1994 | KINGSTON OIL CORP | Brine | 43 | 350 |
1995 | KINGSTON OIL CORP | Brine | 154 | 350 |
1996 | KINGSTON OIL CORP | Brine | 65 | 350 |
1997 | KINGSTON OIL CORP | Brine | 35 | 350 |
1998 | KINGSTON OIL CORP | Brine | 80 | 350 |
1999 | KINGSTON OIL CORP | Brine | 42 | |
2000 | KINGSTON OIL CORP | Brine | 0 | |
2001 | CHEVRON APPALACHIA LLC | Brine | 0 | 330 |
2002 | CHEVRON APPALACHIA LLC | Brine | 46 | 365 |
2003 | ATLAS NOBLE LLC | Brine | 0 | 365 |
2004 | ATLAS NOBLE LLC | Brine | 40 | 365 |
2005 | ATLAS NOBLE LLC | Brine | 14 | 365 |
2006 | ATLAS NOBLE LLC | Brine | 19 | 365 |
2007 | ATLAS NOBLE LLC | Brine | 20 | 365 |
2008 | ATLAS NOBLE LLC | Brine | 36 | 366 |
2009 | ATLAS NOBLE LLC | Brine | 13 | 365 |
2010 | ATLAS NOBLE LLC | Brine | 15 | 365 |
2011 | ATLAS NOBLE LLC | Brine | 22 | |
2012 | ATLAS NOBLE LLC | Brine | 14 | 271 |
2013 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2014 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2015 | ATLAS NOBLE LLC | Brine | 6 | 0 |
2016 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2017 | ATLAS NOBLE LLC | Brine | 0 | 0 |
2018 | M & R INVESTMENTS OHIO LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1420534207 | 2016-9-14 0:00: | AM | No Violations | |
-1659576358 | 2018-10-19 0:00 | PB | No Violations | 4.40 |
-1840695981 | 2018-10-22 0:00 | PB | No Violations | 5.50 |
-575795304 | 2019-11-18 0:00 | FR | No Violations | 1.50 |
-766875551 | 2017-7-19 0:00: | PW | No Violations | 2.40 |
0000PL8140 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0625716823 | 2008-05-27 | Production Wells | No Violations | Producing, no problems noted. Pumping when I was there. |
0766875551 | 2017-07-19 | Production Wells | No Violations | On the day of my inspection, Surveyor, Tom Smith and I went in to the well site to verify the location with a Trimble unit prior to plugging the well. A plugging permit has been issued and the well was shut in and idle on the day of my inspection. |
1420534207 | 2016-09-14 | Administrative Inspection | No Violations | I called Pat Irving of Atlas and stated the well has H2S emitting from the well. This a follow-up with the company stating they will be receiving a Compliance Notice with number 1705312064. He said he would apply for a Plugging Permit. |
1484248979 | 2017-01-12 | Production Wells | No Violations | The purpose of the inspection is due to a follow-up on Compliance Notice number 1705312064. The Company Atlas representatives were Chuck Wood, Chris Belch and Matt Kapanus. They and I Inspector Patrick Shreve entered the well site and verified the status of the well. They opened the tubing and the casing annulus to check for H2S. There was no H2S present that registered on the day of the inspection. The well is shut in and idle due to a tank battery that had been removed from the site. The well will be plugged but may move to low threat due to no smell on the well. They will be in touch and get back with me on the status. |
1510745236 | 2017-11-14 | Production Wells | No Violations | The purpose of my inspection is due to a Compliance Notice follow- |
1659576358 | 2018-10-19 | Plug / Plug Back | No Violations | The inspection is conducted under plugging operation and Compliance Notice follow-up to number 1705312064. Wright well service was over the well rigged up setting the bottom hole Clinton plug. Formation Cementing set the 30 sack plug of regular class A cement in the 4 1/2inch casing with the 2 3/8-inch tubing from 4950-4550. The displacement was 18 barrels of salt water. |
1705312064 | 2016-09-13 | Production Wells | Violations Noted
-11-05(B) and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied. | |
1840695981 | 2018-10-22 | Plug / Plug Back | No Violations | The inspection is conducted under plugging operation and Compliance Notice follow- |
1921446296 | 2018-10-23 | Plug / Plug Back | No Violations | The inspection is conducted under plugging operation and Compliance Notice follow--foot plug. The plug was set form 3780-3480. Formation Cementing ran 86 sacks of regular class A cement and displaced the plug with 55 barrels of salt water. The bottom of 8 5/8-inch casing plug was set from 1771-1571. Formation Cementing set a 200-foot plug with 60 sacks of regular class A cement. The displacement is 25 barrels of fresh water. The surface plug was set from 210-0. Formation Cementing ran 72 sacks of regular class A cement. Cement did not drop back. Circulation was established on the plugs. The plugging is completed which resolves the Compliance Notice. |
625716823 | 2008-5-27 0:00: | PW | No Violations | |
PL8140 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1705312064 | US-OH-116899 | 2018-11-27 | 9-9-02 | General Safety |
1705312064 | US-OH-116900 | 2018-11-27 | 9-9-05(A)1 | Well insufficiently equipped to prevent escape of oil and gas |
1705312064 | US-OH-116901 | 2018-11-27 | NONE18 | Defective casing, leaking well |
For data sources see[9]