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Well ID: 34-119-26360 | Loading map...
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Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Adams Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: CONSOLIDATION COAL CO | |
License Status: Final Restoration | |
License Date: 2015-07-06 | |
Spud Date: 1982-09-24 | |
Spud Drilling Contractor: CVAS DRLG | |
Final Drill Date: 1982-09-28 | |
Well Total Depth: 4170.00 ft | |
Configuration: Vertical | |
Latitude: 40.130000 | |
Longitude: -81.900000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1982-06-03 | 2143 CARLESS RESOURCES INC GeoDate 6/3/82 |
Oil and Gas | 1982-06-03 | Issued Date 6/3/82 Expired Date 12/1/82 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 04170 Proposed Drill Depth 04170 |
Original Spud | 1982-09-24 | |
Completed | 1982-09-28 | |
Reached Total Depth | 1982-09-28 | |
Completion Report Received | 1984-02-28 | |
Change of Owner | 1998-07-02 | Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2015-07-06 | Proposed Formations:CLINTON, Issued Date:7/6/2015, Expired Date:7/5/2017 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:HAD, Proposed Well Class: |
Plugged/Abandoned | 2015-09-03 | |
Record Last Modified | 2017-05-27 | |
Construction Permit Expires | 2017-07-05 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 3989 | 4048 | 0 |
3989 | 4048 | 0 | |
2006-09-11 | 3991 | 4044 | 81 |
3991 | 4044 | 81 | |
3989 | 4048 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 92000 Gal | 60000 | FRAC;H2O,SAND |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1623872518 | 2003-4-24 0:00: | PW | No Violations | |
-1737701879 | 2008-10-16 0:00 | PW | No Violations | |
-519408734 | 2015-4-6 0:00:0 | PW | No Violations | |
-808455723 | 2015-9-3 0:00:0 | PB | No Violations | 7.00 |
0000PL8529 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0157071201 | 2016-02-08 | Plug / Plug Back | No Violations | 119-26360 well was owned by Enervest and plugged. I walked in on lease road and revealed that the Final Restoration will not pass on day of inspection. The vegetation is sparse and will need to be more vegetated before the release. The well site and tank site will pass but not the lease road which is 1.2 miles in length. All Equipment has been removed from well site and tank site.
Well coordinates are 40.134511,-81.903730 epe10 Entry coordinates are 40.13009,-81.89816 epe19 |
0519408734 | 2015-04-06 | Production Wells | Violations Noted | Well is non producing well that is shut in with no production records since 2007. The well is gas pluger lift system (Rabbit Well). There is 8.625x4.5well head and 4.5x2.375tubing head. The tubing valve is shut and the tubing annulus is shut. There is a 100 barrel steel tank and a 50 barrel steel tank. There is a horizontal seperator. Every piece of equipment has heavy brush grown up around it. Dike and identification is present. Plug well within 180 days or further Enforcement Action may be taken. |
0746570863 | 2016-07-13 | Final Restoration | No Violations | Final Restoration passed on 7-13-16 by Patrick Shreve. Well was plugged in compliance OAC 1501-9-11. The land was restored back under ORC 1509.072. The lease road and the site have been vegetated back with no substantial erosion. |
0808455723 | 2015-09-03 | Plug / Plug Back | No Violations | Chipco ran small set of tools in and tagged the top of the cement plug at 1800. They got telegraph at 1404. They ripped off 4.5casing at 1404 and pulled one joint. Then Chipco set Bottom of surface plug at 1362-1162 thru 4.5casing. Then rig pulled up to 200-0 and set top plug. All plugs circulated. Pull out 4.5casing and top off well with 20 sacks. |
1106854148 | 2005-01-27 | Production Wells | No Violations | Shut in, e-mailed Murrey |
1441281030 | 2015-09-02 | Plug / Plug Back | No Violations | Chipco had tubing ran to depth of 3999 and set a plug of 30 sacks of regular class Cement at 3999-3599 in the 4.5casing. Then Chipco pulled all the 2.375upset tubing out and ripped 4.5casing off at 2834. The pipe was dragging as Chipco was pulling out the casing. The rig weight -indicator was at 50,000lb/ft. The weight should have been at 30,000lb/ft. The decision was made to pull some pipe out. Chipco pulled 505 out of 4.5casing. Chipco set a plug at 2329-1929 with 115 sacks of class A cement. There no circulation and there was gas on 4.5casing annulus. |
1441791392 | 2015-09-03 | Plug / Plug Back | No Violations | Well has been plugged in accordance with OAC 1501-9-11. This resolves the Compliance Notice number -519408734 that was issued to the Company. |
1494268146 | 2017-05-08 | Final Restoration | No Violations | Final Restoration passed on 5-8-17 by Patrick Shreve. Well was plugged in compliance OAC 1501-9-11. The land was restored back under ORC 1509.072. Tom Smith and I went in to location and located the old well with GA52CX Magnetic locator. Tom shot the coordinates of the plugged well with the Trimble unit. |
157071201 | 2016-2-8 0:00:0 | PB | No Violations | 2.00 |
1623872518 | 2003-04-24 | Production Wells | No Violations | Shut-in. |
1669495550 | 2008-03-10 | Production Wells | No Violations | Shut-in. For 5 years will call Murrey with a produce or plug order |
1737701879 | 2008-10-16 | Production Wells | No Violations | Well is shut in and has been for several years. Production prior was poor so there is no reason for this well to be out there. Will send out NOV. |
746570863 | 2016-7-13 0:00: | FR | No Violations | 0.50 |
PL8529 | PL | No Violations |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0519408734 | US-OH-125671 | 2015-09-22 | Well shall be plugged | |
0519408734 | US-OH-125672 | 2015-09-22 | Statement of annual production not filed |
For data sources see[9]