X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-119-22419

Well Details

Well ID: 34-119-22419
Loading map...
Country: United States
State: Ohio
County: Muskingum
Municipality: Washington Township
Operator Name: KENOIL LLC
Well Pad ID:
Farm/Lease Name: DUNLAP
License Status: Plugged and Abandoned
License Date: 2016-08-24
Spud Date: 1970-11-30
Spud Drilling Contractor:
Final Drill Date: 1970-12-30
Well Total Depth: 3630.00 ft
Configuration: Vertical
Latitude: 40.040000
Longitude: -81.980000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1970-11-27 627 KENOIL GeoDate 11/27/70
Original Spud 1970-11-30 UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017.
Completed 1970-12-30 UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017.
Reached Total Depth 1970-12-30 UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017.
Correction to Well 2016-08-19 UPDATED ACREAGE PER PLUGGING APPLICATION AND FURTHER INVESTIGATION OF PLAT
APP 2016-08-24 Proposed Formations:CLINTON, Issued Date:8/24/2016, Expired Date:8/24/2018 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2016-10-04 UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017.
Record Last Modified 2017-05-25 UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017.
Construction Permit Expires 2018-08-24 UPDATED LOCATION PER SURVEYOR COORDINATES-ALE 03/29/2017.

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 2000 Bbl 0

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 IRVIN DRILLING CORP 5419.00 0.00 0
1985 IRVIN DRILLING CORP 268.00 0.00 365
1986 IRVIN DRILLING CORP 3119.00 0.00 365
1987 IRVIN DRILLING CORP 5813.00 0.00 365
1988 IRVIN DRILLING CORP 5495.00 0.00 365
1989 IRVIN DRILLING CORP 6389.00 0.00 365
1990 IRVIN DRILLING CORP 4175.00 0.00 365
1991 KENOIL LLC 1579.00 0.00 365
1992 KENOIL LLC 2231.00 0.00 365
1993 KENOIL LLC 1386.00 0.00 365
1994 KENOIL LLC 4756.00 0.00 0
1995 KENOIL LLC 3171.00 0.00 0
1996 KENOIL LLC 1693.00 0.00 0
1997 KENOIL LLC 1592.00 81.00 365
1998 KENOIL LLC 1551.00 0.00 365
1999 KENOIL LLC 2166.00 0.00 0
2000 KENOIL LLC 1624.00 0.00 365
2001 KENOIL LLC 1411.00 0.00 365
2002 KENOIL LLC 1058.00 0.00 365
2003 KENOIL LLC 959.00 0.00 365
2004 KENOIL LLC 1581.00 0.00 365
2005 KENOIL LLC 800.00 0.00 365
2006 KENOIL LLC 661.00 0.00 0
2007 KENOIL LLC 560.00 0.00 0
2008 KENOIL LLC 569.00 0.00 365
2009 KENOIL LLC 525.00 0.00 365
2010 KENOIL LLC 148.00 0.00 365
2011 KENOIL LLC 1279.00 0.00 0
2012 KENOIL LLC 1166.00 0.00 366
2013 KENOIL LLC 1711.00 0.00 365
2014 KENOIL LLC 780.00 0.00 365
2016 KENOIL LLC 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 IRVIN DRILLING CORP Brine 0 0
1985 IRVIN DRILLING CORP Brine 0 365
1986 IRVIN DRILLING CORP Brine 0 365
1987 IRVIN DRILLING CORP Brine 0 365
1988 IRVIN DRILLING CORP Brine 0 365
1989 IRVIN DRILLING CORP Brine 0 365
1990 IRVIN DRILLING CORP Brine 0 365
1991 KENOIL LLC Brine 0 365
1992 KENOIL LLC Brine 0 365
1993 KENOIL LLC Brine 0 365
1994 KENOIL LLC Brine 0 0
1995 KENOIL LLC Brine 0 0
1996 KENOIL LLC Brine 0 0
1997 KENOIL LLC Brine 0 365
1998 KENOIL LLC Brine 0 365
1999 KENOIL LLC Brine 0
2000 KENOIL LLC Brine 365
2001 KENOIL LLC Brine 0 365
2002 KENOIL LLC Brine 0 365
2003 KENOIL LLC Brine 0 365
2004 KENOIL LLC Brine 0 365
2005 KENOIL LLC Brine 0 365
2006 KENOIL LLC Brine 0
2007 KENOIL LLC Brine 0
2008 KENOIL LLC Brine 0 365
2009 KENOIL LLC Brine 0 365
2010 KENOIL LLC Brine 0 365
2011 KENOIL LLC Brine 0
2012 KENOIL LLC Brine 0 366
2013 KENOIL LLC Brine 0 365
2014 KENOIL LLC Brine 0 365
2016 KENOIL LLC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-286885216 2016-10-25 0:00 PB No Violations 2.00
-373904520 2016-9-27 0:00: PB No Violations 7.00
-820416157 2016-9-28 0:00: PB No Violations 8.00
-863327426 2016-9-30 0:00: PB No Violations 4.50
0000DP6630 Final Restoration No Violations Final Restoration done information from Data Point
0286885216 2016-10-25 Plug / Plug Back No Violations On the day of inspection I met with Tom Smith a surveyor for ODNR Oil and Gas. The well was recently plugged and there is a sand and gravel operation heading toward the plugged well. We will stop back at a later date.
0373904520 2016-09-27 Plug / Plug Back No Violations On the day of my inspection Phil Moran washed 3 tons of clay down the 5.5 inch casing. Phil ran his ripping tools in to a depth of 3200 feet to start looking for a telegraph. He was only able to get 12 to 15 inches of stretch. He was unsuccessful at finding a telegraph as he came up the hole. Phil stopped and ripped on the casing at 2500 feet without telegraph, but he could not pull the casing. Phil continued to come up the hole searching for a telegraph, finally getting one at 1400 feet. Phil pulled the tools out and washed another 5 tons of clay down the 5.5 inch casing for a total of 8 tons on the bottom plug. He shut down to let the clay settle overnight before going in to part the casing.
0820416157 2016-09-28 Plug / Plug Back No Violations On the day of my inspection Phil Moran went back in to 1400 feet and parted the 5.5 inch casing. The crew pulled the casing from the well. Phil set a pre-cast tapered cement plug on the 7 inch casing seat at a depth of 926 feet. He made several attempts to pull the 8.625 inch casing. The 8.625 inch casing was cut off at ground level with the 10 inch casing. Phil used a spear go inside of the casing to pull. The casing would not budge at 45,000 to 50,000 pounds of pull. Phil disengaged the spear to investigate the possibility of the two casing strings being welded. They dug out around the 10 inch and cleaned the top of the two strings. We found the top of the 8.625 inch casing was rotted and tearing apart. The annular space was filled with sand and rust fragments. Phil went in with his ripper to search for a telegraph. He got a telegraph at 105 feet, and ripped on the casing for some time until he shut down due to weather. The tools came out dry.
0863327426 2016-09-30 Plug / Plug Back No Violations On the day of my inspection I met with Phil Moran at the site to discuss the plan for the 8.625 inch casing. The top of the casing was too deteriorated to weld a sub to, or try to continue pulling with a spear. The top of the fluid was at an approximate depth of 400 feet, indicating good casing integrity, and mud job downhole. I discussed the situation with Muskingum County inspector Pat Shreve, and we agreed to allow Phil to leave the casing in place. Another factor in the decision was that a surface mining operation was scheduled to be at the well within two months. The well casing will eventually be cut off at 60 to 65 feet below grade; therefore, it would be pointless to spend an excessive amount of time trying to remove the top joint of casing. Phil rigged down and washed approximately 6 tons of clay down the well filling it to surface from the pre-cast plug at 926 feet. The clay was settling down the hole slowly. We decided to allow the clay to settle over the weekend, before washing any more in. Phil covered his clay with a tarp and covered the open casing.
1406137642 2014-07-23 Production Wells No Violations Well is a producing well that was set up as an old gas plunger lift well. The well is currently shut in because Gatherco has shut them in. The water content is too high for the Dominion line. They will get with Gatherco and get scrubber installed and get well on line. There is a steel 100 barrel tank and a meter run. The company is current with their production records. The company will re attach an identification at well head.
1475011251 2016-09-26 Plug / Plug Back No Violations On the day of my inspection I found that Phil Moran was rigged up to plug the well, and pulling the tubing. The clay had just been delivered. They got 20.8 tons from Logan Clay. It started to rain, so Phil covered the clay and shut down for the day .
1475512441 2016-10-03 Plug / Plug Back No Violations On the day of my inspection I found that Phil Moran was not working at the plug job site. He said that he would be back the following day to finish up. The clay had fallen over the weekend to a depth that was out of visibility from the surface. I dropped a rock down the casing and found the top of the clay/fluid to be at an approximate depth of 200 feet.
1475593125 2016-10-04 Plug / Plug Back No Violations On the day of my inspection I found that the clay top was still at an approximate depth of 200 feet. Phil got another 3 to 4 tons of clay in, filling the well to surface. We let it set while they finished digging out around the casing, and the clay did not fall any further. Phil cut the casing off 36 inches below grade and capped the casing with a steel plate inscribed with the permit number. He then covered the casing up and filled in the excavated area.
2077052623 2014-07-23 Production Wells No Violations On the date of inspection I accompanied ODNR Inspector Patrick Shreve to check the status of the well. The well was shut in at the time of inspection. Refer to Patrick Shreves report for further details.
DP6630 FR No Violations

For data sources see[8]

References