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Well ID: 34-119-22374 | Loading map...
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Country: United States | |
State: Ohio | |
County: Muskingum | |
Municipality: Monroe Township | |
Operator Name: BIG SKY ENERGY INC | |
Well Pad ID: | |
Farm/Lease Name: BARR ROBERT & JOAN | |
License Status: Producing | |
License Date: 1975-11-20 | |
Spud Date: 1970-12-22 | |
Spud Drilling Contractor: ARMSTRONG DRLG | |
Final Drill Date: 1970-12-29 | |
Well Total Depth: 4741.00 ft | |
Configuration: Vertical | |
Latitude: 40.080000 | |
Longitude: -81.730000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1970-12-22 | WELL PLUGGED: 9/14/74 AND THEN REOPENED IN '75/'76? NO WELL RECORD FILED BUT WELL WAS TRANSFERRED IN 1998 FROM ROBT. BARR TO VALLEY ENTERPRISES. RE-OPEN 11/26/1975 RE- |
Completed | 1970-12-29 | WELL PLUGGED: 9/14/74 AND THEN REOPENED IN '75/'76? NO WELL RECORD FILED BUT WELL WAS TRANSFERRED IN 1998 FROM ROBT. BARR TO VALLEY ENTERPRISES. RE-OPEN 11/26/1975 RE- |
Reached Total Depth | 1970-12-29 | WELL PLUGGED: 9/14/74 AND THEN REOPENED IN '75/'76? NO WELL RECORD FILED BUT WELL WAS TRANSFERRED IN 1998 FROM ROBT. BARR TO VALLEY ENTERPRISES. RE-OPEN 11/26/1975 RE- |
Completion Report Received | 1971-03-19 | WELL PLUGGED: 9/14/74 AND THEN REOPENED IN '75/'76? NO WELL RECORD FILED BUT WELL WAS TRANSFERRED IN 1998 FROM ROBT. BARR TO VALLEY ENTERPRISES. RE-OPEN 11/26/1975 RE- |
Plugged/Abandoned | 1974-08-14 | WELL PLUGGED: 9/14/74 AND THEN REOPENED IN '75/'76? NO WELL RECORD FILED BUT WELL WAS TRANSFERRED IN 1998 FROM ROBT. BARR TO VALLEY ENTERPRISES. RE-OPEN 11/26/1975 RE- |
CO | 1981-01-26 | 579 CHRIS OIL CO GeoDate 1/26/81 |
Change of Owner | 1998-03-08 | Operator changed from 4003, BARR ROBERT V to 4431, VALLEY ENTERPRISES |
Change of Owner | 2007-12-13 | Operator changed from 4431, VALLEY ENTERPRISES to 1333, BIG SKY ENERGY INC |
Record Last Modified | 2017-10-17 | WELL PLUGGED: 9/14/74 AND THEN REOPENED IN '75/'76? NO WELL RECORD FILED BUT WELL WAS TRANSFERRED IN 1998 FROM ROBT. BARR TO VALLEY ENTERPRISES. RE-OPEN 11/26/1975 RE- |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 1220 | 1235 | 2 |
2003-05-30 | 4550 | 4602 | 25 |
4550 | 4602 | 25 | |
1220 | 1235 | 2 | |
1220 | 1235 | 2 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 1150 Bbl | 30000 | |||
H2O | 0 | 800 Bbl | 30000 |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1699064029 | 2016-4-16 0:00: | PW | No Violations | 1.00 |
-873346972 | 2004-2-20 0:00: | FR | No Violations | |
0873346972 | 2004-02-20 | Final Restoration | No Violations | Well was never Plugged!!!!! |
1064423839 | 2003-09-24 | Production Wells | No Violations | |
1699064029 | 2016-04-16 | Production Wells | Violations Noted | The follow-up inspection is due to a Temporary Restraining Order issued in the Trumble County Court of Common Pleas and the Chiefs Order #2015-535, Chiefs Order #2016-105.
-up that non-operational. The tubing annulus is open on the tubing head. The vegetation is heavy around the pumping unit. There is no known tank battery. Production has never been filed since well was re-opened. The company is ordered to plug the said well. The well owner /operator shall submit a written plugging schedule to Patrick Shreve at 5880 Memory Rd. Zanesville, Ohio 43701 within 30 days per OAC 1501:9-11-05(B) and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1699064029 | US-OH-116840 | 2016-06-06 | Failure to legibly identify well | |
1699064029 | US-OH-116841 | 2016-06-06 | Well shall be plugged | |
1699064029 | US-OH-116842 | 2016-06-06 | Statement of annual production not filed |
For data sources see[5]