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34-115-23697

Well Details

Well ID: 34-115-23697
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Country: United States
State: Ohio
County: Morgan
Municipality: Bristol Township
Operator Name: SMITH RONALD DBA CHIPCO
Well Pad ID:
Farm/Lease Name: CARRELL JAMES
License Status: Producing
License Date: 2014-04-04
Spud Date: 1987-12-28
Spud Drilling Contractor: [[ALTEX INC [ALTHEIRS]]]
Final Drill Date: 1988-07-22
Well Total Depth: 4846.00 ft
Configuration: Vertical
Latitude: 39.700000
Longitude: -81.810000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1984-10-24 471 EAGLE MOUNTAIN ENERGY GeoDate 10/24/84
Oil and Gas 1984-10-24 Issued Date 10/24/84 Expired Date 4/22/85 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 04846 Proposed Drill Depth 04846
CO 1987-11-18 471 EAGLE MOUNTAIN ENERGY GeoDate 11/18/87
Oil and Gas 1987-11-18 Issued Date 11/18/87 Expired Date 11/17/88 Acres 0010400 Tool Type RTA Proposed Formation BEREA Proposed Depth 01510 Proposed Drill Depth 01510
Plugged Back 1987-11-21
Completed 1987-12-30
Completion Report Received 1988-02-12
Original Spud 1988-06-17
Reached Total Depth 1988-07-22
Change of Owner 1999-12-15 Operator changed from 471, EAGLE MOUNTAIN ENERGY to 2165, PETRO QUEST INC
Change of Owner 2005-03-01 Operator changed from 2165, PETRO QUEST INC to 7640, SMITH RONALD DBA CHIPCO
Last Compliance Report 2007-05-21
APP 2007-05-29 Proposed Formations:BEREA, Issued Date:5/29/2007, Expired Date:5/28/2008 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
APP 2014-04-04 Proposed Formations:BEREA, Issued Date:4/4/2014, Expired Date:4/3/2016 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Record Last Modified 2015-09-24
Construction Permit Expires 2016-04-03

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 0 0
0 0
2006-09-11 1430 1440 1
1430 1440 1
0 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
OIL 0 66 Bbl 2000 FRAC: H2O,SAND,CO2

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 EAGLE MOUNTAIN ENERGY 10671.00 211.00 350
1987 EAGLE MOUNTAIN ENERGY 1306.00 35.00 365
1988 EAGLE MOUNTAIN ENERGY 118.00 70.00 365
1989 SCION ENERGY INC 588.00 20.00 365
1990 EAGLE MOUNTAIN ENERGY 46.00 0.00 365
1991 EAGLE MOUNTAIN ENERGY 0.00 0.00 365
1999 PETRO QUEST INC 0.00 0.00 0
2000 PETRO QUEST INC 0.00 0.00 0
2002 PETRO QUEST INC 0.00 0.00 0
2003 PETRO QUEST INC 0.00 0.00 0
2004 PETRO QUEST INC 0.00 0.00 0
2005 PETRO QUEST INC 0.00 0.00 0
2009 PETRO QUEST INC 0.00 0.00 0
2014 SMITH RONALD DBA CHIPCO 0.00 0.00 0
2016 SMITH RONALD DBA CHIPCO 0.00 0.00 0
2017 SMITH RONALD DBA CHIPCO 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 EAGLE MOUNTAIN ENERGY Brine 478 350
1987 EAGLE MOUNTAIN ENERGY Brine 1408 365
1988 EAGLE MOUNTAIN ENERGY Brine 417 365
1989 SCION ENERGY INC Brine 440 365
1990 EAGLE MOUNTAIN ENERGY Brine 0 365
1991 EAGLE MOUNTAIN ENERGY Brine 0 365
1999 PETRO QUEST INC Brine 0 0
2000 PETRO QUEST INC Brine 0 0
2002 PETRO QUEST INC Brine 0 0
2003 PETRO QUEST INC Brine 0 0
2004 PETRO QUEST INC Brine 0 0
2005 PETRO QUEST INC Brine 0 0
2009 PETRO QUEST INC Brine 0 0
2014 SMITH RONALD DBA CHIPCO Brine 0 0
2016 SMITH RONALD DBA CHIPCO Brine 0 0
2017 SMITH RONALD DBA CHIPCO Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1259450730 2019-2-28 0:00: PW No Violations 2.00
-1268965486 2007-1-16 0:00: AD No Violations
-1330087083 2007-1-16 0:00: AD No Violations
-174371324 2007-4-16 0:00: AD No Violations
-1956463854 2017-1-9 0:00:0 PW No Violations 1.00
-2022340505 2015-3-18 0:00: PW No Violations 1.50
-291613605 2007-1-16 0:00: AD No Violations
-431230717 2007-1-16 0:00: AD No Violations
-454850285 2007-1-16 0:00: AD No Violations
-635089795 2007-1-16 0:00: AD No Violations
-945051674 2007-1-16 0:00: AD No Violations
0000PL9466 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0174371324 2007-04-16 Annular Disposal No Violations No change in status of well it is still idle,owner is awaiting plugging permit to be issued once received he will begin plugging program.
0291613605 2007-01-16 Annular Disposal Violations Noted A.D. not hooked up,upon inspecting well site found well to be idle and no I.D. could be found well is equipped with tubing and rods and 1-100 bbl tank last production reported on well was back in 1990.
0369368592 2007-01-16 Annular Disposal No Violations FOLLOW UP TO NOV # -1330087083 FOLLOW UP TO NOV # -291613605 A.D. not hooked up,upon inspecting well site found well to be idle and no I.D. could be found well is equipped with tubing and rods and 1-100 bbl tank last production reported on well was back in 1990.
0431230717 2007-01-16 Annular Disposal No Violations FOLLOW UP TO NOV # -1268965486 FOLLOW UP TO NOV # -291613605 A.D. not hooked up,upon inspecting well site found well to be idle and no I.D. could be found well is equipped with tubing and rods and 1-100 bbl tank last production reported on well was back in 1990.
0431432977 2013-11-25 Production Wells No Violations Compliance Action Follow-up -1330087083: There has been no resolution to any of the issues.
0454850285 2007-01-16 Annular Disposal No Violations FOLLOW UP TO NOV # -291613605 A.D. not hooked up,upon inspecting well site found well to be idle and no I.D. could be found well is equipped with tubing and rods and 1-100 bbl tank last production reported on well was back in 1990.
0529035237 2016-10-24 Production Wells No Violations The inspection today revealed that this well is equipped with a 5 1/2 inch diameter wellhead and 2 inch production tubing. The well appears to have had a pumping unit on it at one time but, the well no long has a pumping unit or rods on it. There are no production lines on the wellhead and all the valves are closed on the well. Near the wellhead is an old electric box that is no longer hooked up and in use. There is a 310 barrel tank near the well head laying on its side and is not in use. There is no proper identification on the wellhead or the tank near the well. There has been no resolution to any of the issues on this well.
0586016754 2015-12-02 Field Inspected, Well Not Found No Violations On my inspection today I was going to this well to do a compliance follow-up. After wandering around in the woods I was unable to locate this well. I also heard a shot gun go off in the distance of the area I was headed so I assumed hunters were in the area. I decided to turn back as to not put myself in danger. I will also try to meet with inspector Glasscock to see if he can assist me at finding this well at another time when hunters are not around.
0635089795 2007-01-16 Annular Disposal No Violations FOLLOW UP TO NOV # -291613605 A.D. not hooked up,upon inspecting well site found well to be idle and no I.D. could be found well is equipped with tubing and rods and 1-100 bbl tank last production reported on well was back in 1990.
0945051674 2007-01-16 Annular Disposal No Violations FOLLOW UP TO NOV # -635089795 FOLLOW UP TO NOV # -291613605 A.D. not hooked up,upon inspecting well site found well to be idle and no I.D. could be found well is equipped with tubing and rods and 1-100 bbl tank last production reported on well was back in 1990.
1240574650 2009-04-24 Production Wells No Violations PERMIT EXPIRED5/28/08
1259450730 2019-02-28 Production Wells No Violations I conducted a compliance notice follow-up on this well today. Inspector David Ball issued a compliance notice to Chipco on 1/16/2007 to plug the well. My inspection revealed that the well has not been plugged or placed into production. I took four photos of the well. I contacted Chip Smith at 2:22 PM and discussed the well with him. Chip said he would be filing for an application for a permit and plug the well this summer. Time of inspection: 12:50 PM. Weather: 33 degrees F, Sunny
1268965486 2007-01-16 Annular Disposal No Violations FOLLOW UP TO NOV # -291613605 A.D. not hooked up,upon inspecting well site found well to be idle and no I.D. could be found well is equipped with tubing and rods and 1-100 bbl tank last production reported on well was back in 1990.
1328193344 2012-02-01 Production Wells No Violations My inspection this day found the well not capable of production, very grown over with briars. The original NOV was wrote in 2007 - the landowner recently called to see why the well has not been plugged. I suggested he call Chip Smith and see what his plans were for the well. NO identification found, old frac tank back by the welland well has 1 tubing on a packer. The landowner on the adjoining property showed me this well and says it leaks gas - leak very noticeable on low cloady days - I smelled no gas this day. Records show the well last produced in 1990.
1330087083 2007-01-16 Annular Disposal Violations Noted FOLLOW UP TO NOV # -291613605 A.D. not hooked up,upon inspecting well site found well to be idle and no I.D. could be found well is equipped with tubing and rods and 1-100 bbl tank last production reported on well was back in 1990.
1484142410 2017-01-11 Administrative Inspection No Violations I was at the Morgan County Court House this day with Inspector Jake Glasscock for a training opportunity. The information on this well has shown that this well is indeed owned by Smith Ronald DBA Chipco as per information in book 147 page 725 showing this well was transferred to Chipco as well as several other wells.
1520339944 2014-03-05 Production Wells No Violations Compliance Action Follow-up -1330087083: There has been no resolution to any of the issues. Well is still idle and I called and left Chip Smith a message regarding the well issues.
1525973091 2018-05-10 Production Wells No Violations I conducted a compliance notice follow-up on the Carrell #1 well today. Inspector David Ball issued a compliance notice to Chipco on 1/16/2007 to plug the well. My inspection revealed that the well has not been plugged or placed into production. The well was completely covered in brush. It was equipped with 1 inch tubing and no rods. The tubing was shut in. There were no production lines connected to the well. I could hear and smell a slight gas leak from the well. I observed a frac tank near the well location. I took 6 photos of the well and tank. I accessed the well from the tank battery for Pearl E. Swallow #3 API permit number 1718 well. I left a voicemaill message for Chip Smith at 2:17 PM. Time of inspection: 12:30 PM. Weather: 77 degrees F, Sunny
1594898566 2020-7-15 0:00: PW No Violations 1.00
1801221584 2016-06-25 Production Wells No Violations The inspection on this day revealed that this well still has it valves shut in and is not capable of production. There has been no resolution at this time. I spoke with Chip to see what he had planned to do with this well. He thought he had sold it off to another company and was not even sure where it was. He did not have any plan at the time of talking to him to plug this well, but would go look at it and give me an idea. I asked him to call me when he could and I would take him to the wellhead and show him where it was.
1956463854 2017-01-09 Production Wells No Violations The inspection today revealed that this well is equipped with a 5 1/2 inch diameter wellhead and 2 inch production tubing. The well appears to have had a pumping unit on it at one time but, the well no long has a pumping unit or rods on it. There are no production lines on the wellhead and all the valves are closed on the well. Near the wellhead is an old electric box that is no longer hooked up and in use. There is a 310 barrel tank near the well head laying on its side and is not in use. There is no proper identification on the wellhead or the tank near the well. There has been no resolution to any of the issues on this well and this well is idle at the time of inspection.
2022340505 2015-03-18 Production Wells No Violations Compliance Action Follow-up -1330087083: There has been no resolution to any of the issues. There is a 310 bbl tank laying on its side adjacent to the wellhead. The well is equipped with 4.5 casing and tubing which is completely overgrown. There is an old electric box next to wellhead and flow lines visible in various places. The actual access road is at gate for Bar-G tank battery. Follow to coordinates 39.70779/-81.80698.
369368592 2007-1-16 0:00: AD No Violations
431432977 2013-11-25 0:00 PW No Violations 2.00
529035237 2016-10-24 0:00 PW No Violations 2.00
586016754 2015-12-2 0:00: NF No Violations 1.00
62811335 2019-6-12 0:00: PW No Violations 0.60
PL9466 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0291613605 US-OH-123032 2007-01-15 Failure to legibly identify well
0291613605 US-OH-123033 2007-01-15 Well shall be plugged
1330087083 US-OH-109442 2007-01-15 Failure to legibly identify well
1330087083 US-OH-109443 2007-01-15 Well shall be plugged

For data sources see[9]

References