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34-115-23091

Well Details

Well ID: 34-115-23091
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Country: United States
State: Ohio
County: Morgan
Municipality: Bristol Township
Operator Name: OHIO ENERGY ASSETS, INC.
Well Pad ID:
Farm/Lease Name: RAY HOPE W ETAL
License Status: Final Restoration
License Date: 2005-08-23
Spud Date: 1983-10-10
Spud Drilling Contractor: WORTHINGTON OIL
Final Drill Date: 1983-10-14
Well Total Depth: 5250.00 ft
Configuration: Vertical
Latitude: 39.710000
Longitude: -81.730000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1982-12-17 Issued Date 12/17/82 Expired Date 6/15/83 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1983-10-05 1283 COSHOCTON PIPE CO GeoDate 10/5/83
Oil and Gas 1983-10-05 Issued Date 10/5/83 Expired Date 4/2/84 Acres 0040000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05250 Proposed Drill Depth 05250
Original Spud 1983-10-10 R.I. 10-4-83
Completed 1983-10-14 R.I. 10-4-83
Reached Total Depth 1983-10-14 R.I. 10-4-83
CO 1984-11-09 853 REDMAN OIL CO INC GeoDate 12/17/82
Completion Report Received 1985-01-22 R.I. 10-4-83
CO 1992-12-09 3243 OHIO PRODUCTION CORP GeoDate 10/5/83
Change of Owner 1998-03-10 Operator changed from 3243, OHIO PRODUCTION CORP to 6091, OHIO ENERGY ASSETS, INC.
APP 2004-06-09 Proposed Formations:CLINTON, Issued Date:6/9/2004, Expired Date:6/9/2005 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:TAAD, Proposed Well Class:
APP 2005-08-23 Proposed Formations:CLINTON/MEDINA, Issued Date:8/23/2005, Expired Date:8/23/2006 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:TAAD, Proposed Well Class:
Plugged/Abandoned 2005-09-07 R.I. 10-4-83
Last Compliance Report 2005-10-17 R.I. 10-4-83
Construction Permit Expires 2006-08-23 R.I. 10-4-83
Record Last Modified 2015-09-24 R.I. 10-4-83

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 4930 5010 0
4930 5010 0
2006-09-11 4964 5075 19
4964 5075 19
4930 5010 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 0 60000
N2 0 334050 0 FRAC: H2O,SAND,N2

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 COSHOCTON PIPE CO 105890.00 216.00 0
1985 COSHOCTON PIPE CO 27360.00 79.00 0
1986 COSHOCTON PIPE CO 17860.00 68.00 365
1987 REDMAN OIL CO INC 11780.00 0.00 365
1988 COSHOCTON PIPE CO 9430.00 0.00 366
1989 COSHOCTON PIPE CO 10221.00 0.00 0
1990 REDMAN OIL CO INC 1977.00 44.00 365
1991 REDMAN OIL CO INC 9695.00 0.00 365
1994 OHIO PRODUCTION CORP 0.00 0.00 0
2005 OHIO ENERGY ASSETS, INC. 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 COSHOCTON PIPE CO Brine 0 0
1985 COSHOCTON PIPE CO Brine 0 0
1986 COSHOCTON PIPE CO Brine 0 365
1987 REDMAN OIL CO INC Brine 0 365
1988 COSHOCTON PIPE CO Brine 0 366
1989 COSHOCTON PIPE CO Brine 1400 0
1990 REDMAN OIL CO INC Brine 440 365
1991 REDMAN OIL CO INC Brine 0 365
1994 OHIO PRODUCTION CORP Brine 0 0
2005 OHIO ENERGY ASSETS, INC. Brine 55 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1651270323 2005-6-13 0:00: PW No Violations
-445211291 2005-12-15 0:00 FR No Violations
-616014244 2005-3-14 0:00: PW No Violations
0000PL9786 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0445211291 2005-12-15 Final Restoration No Violations Restoration work at site satisfactory.
0616014244 2005-03-14 Production Wells Violations Noted Upon inspecting well site found well to be idle no I.D. posted tubing on ground no production reported on well since 1991.Plug permit issued for well 6/9/04.
1126358492 2005-09-07 Annular Disposal No Violations Well has been plugged resolving NOV and Chiefs Order.
1265936301 2005-09-06 Production Wells No Violations Meeting with Joe Melville, Bill Mitten to discuss plugging of said well, operator was recompleating well in 1992 and had cementing problems they were attempting to shut off water zone in Oriskany sands when apparently cement locked up.electric bridge plug was set@3700 and oriskany ws perfed and operator tried to squeeze cement with no avail! Information was gathered from reviewing company records.
1651270323 2005-06-13 Production Wells Violations Noted Upon inspecting well site found no change in status of well, still idle well owner had a plug permit but it has since expired,recommend Chiefs Order.
1693154823 2015-11-23 Final Restoration No Violations This well is showing final restoration in our system. I went out to do a field inspection on this location. During the inspection I did not find any well or any production equipment left behind. There are no violations at this time.
PL9786 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0616014244 US-OH-126958 2005-03-19 Failure to legibly identify well
0616014244 US-OH-126959 2005-03-19 Well shall be plugged
1651270323 US-OH-116292 2005-03-19 Failure to legibly identify well
1651270323 US-OH-116293 2005-03-19 Well shall be plugged

For data sources see[9]

References