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34-115-22678

Well Details

Well ID: 34-115-22678
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Country: United States
State: Ohio
County: Morgan
Municipality: Center Township
Operator Name: M & R INVESTMENTS OHIO LLC
Well Pad ID:
Farm/Lease Name: MORRIS
License Status: Final Restoration
License Date: 2017-12-18
Spud Date: 1981-12-17
Spud Drilling Contractor:
Final Drill Date: 1981-12-21
Well Total Depth: 5622.00 ft
Configuration: Vertical
Latitude: 39.640000
Longitude: -81.590000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1981-12-04 56 BUCKEYE OIL PRODUCING CO GeoDate 12/4/81
Original Spud 1981-12-17 UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. GMM UPDATED PLUG STATUS PER PLUG REPORT
Completed 1981-12-21 UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. GMM UPDATED PLUG STATUS PER PLUG REPORT
Reached Total Depth 1981-12-21 UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. GMM UPDATED PLUG STATUS PER PLUG REPORT
CO 1996-09-18 4350 CENTURY WELL SERVICE GeoDate 12/4/81
Change of Owner 2007-10-03 Operator changed from 4350, CENTURY WELL SERVICE to 7033, BROAD STREET ENERGY COMPANY
Change of Owner 2008-02-14 Operator changed from 7033, BROAD STREET ENERGY COMPANY to 8312, BROAD STREET SERV LLC
Change of Owner 2015-07-16 Operator changed from 8312, BROAD STREET SERV LLC to 8685, M & R INVESTMENTS OHIO LLC
APP 2017-12-18 Proposed Formations:MEDINA, Issued Date:12/18/2017, Expired Date:12/18/2019 12:00:00 PM, Drilling unit acres:80, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2018-07-19 UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. GMM UPDATED PLUG STATUS PER PLUG REPORT
Record Last Modified 2018-10-31 UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. GMM UPDATED PLUG STATUS PER PLUG REPORT
Construction Permit Expires 2019-12-18 UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. GMM UPDATED PLUG STATUS PER PLUG REPORT

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5486 5497 12
5486 5497 12
5486 5497 12

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1500 Bbl 40000 CROSS-LINK

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 BT ENERGY CORP 9540.00 0.00 365
1985 BT ENERGY CORP 6908.00 0.00 365
1986 BT ENERGY CORP 7541.00 0.00 365
1987 BUCKEYE OIL PRODUCING CO 4553.00 0.00 365
1988 BUCKEYE OIL PRODUCING CO 4473.00 0.00 365
1989 BUCKEYE OIL PRODUCING CO 2071.00 0.00 365
1990 BUCKEYE OIL PRODUCING CO 1880.00 0.00 365
1991 BUCKEYE OIL PRODUCING CO 2607.00 0.00 365
1992 BUCKEYE OIL PRODUCING CO 1756.00 0.00 365
1993 BUCKEYE OIL PRODUCING CO 1990.00 0.00 365
1994 BUCKEYE OIL PRODUCING CO 1898.00 0.00 365
1995 BUCKEYE OIL PRODUCING CO 1591.00 0.00 365
1996 CENTURY WELL SERVICE 0.00 0.00 365
1997 CENTURY WELL SERVICE 0.00 0.00 365
1998 CENTURY WELL SERVICE 0.00 0.00 365
1999 CENTURY WELL SERVICE 0.00 0.00 365
2000 CENTURY WELL SERVICE 0.00 0.00 365
2001 CENTURY WELL SERVICE 0.00 0.00 365
2002 CENTURY WELL SERVICE 0.00 0.00 365
2003 CENTURY WELL SERVICE 0.00 0.00 365
2004 CENTURY WELL SERVICE 0.00 0.00 365
2005 CENTURY WELL SERVICE 0.00 0.00 365
2006 CENTURY WELL SERVICE 0.00 0.00 365
2007 BROAD STREET SERV LLC 0.00 0.00 365
2008 BROAD STREET SERV LLC 0.00 0.00 0
2009 BROAD STREET SERV LLC 0.00 0.00 0
2011 BROAD STREET SERV LLC 0.00 0.00 0
2012 BROAD STREET SERV LLC 0.00 0.00 0
2013 BROAD STREET SERV LLC 0.00 0.00 0
2014 BROAD STREET SERV LLC 0.00 0.00 0
2015 M & R INVESTMENTS OHIO LLC 0.00 0.00 0
2016 M & R INVESTMENTS OHIO LLC 10.00 0.00 0
2017 M & R INVESTMENTS OHIO LLC 0.00 0.00 0
2018 M & R INVESTMENTS OHIO LLC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 BT ENERGY CORP Brine 0 365
1985 BT ENERGY CORP Brine 0 365
1986 BT ENERGY CORP Brine 0 365
1987 BUCKEYE OIL PRODUCING CO Brine 0 365
1988 BUCKEYE OIL PRODUCING CO Brine 55 365
1989 BUCKEYE OIL PRODUCING CO Brine 0 365
1990 BUCKEYE OIL PRODUCING CO Brine 0 365
1991 BUCKEYE OIL PRODUCING CO Brine 0 365
1992 BUCKEYE OIL PRODUCING CO Brine 55 365
1993 BUCKEYE OIL PRODUCING CO Brine 0 365
1994 BUCKEYE OIL PRODUCING CO Brine 0 365
1995 BUCKEYE OIL PRODUCING CO Brine 0 365
1996 CENTURY WELL SERVICE Brine 0 365
1997 CENTURY WELL SERVICE Brine 0 365
1998 CENTURY WELL SERVICE Brine 0 365
1999 CENTURY WELL SERVICE Brine 0 365
2000 CENTURY WELL SERVICE Brine 0 365
2001 CENTURY WELL SERVICE Brine 0 365
2002 CENTURY WELL SERVICE Brine 0 365
2003 CENTURY WELL SERVICE Brine 0 365
2004 CENTURY WELL SERVICE Brine 0 365
2005 CENTURY WELL SERVICE Brine 0 365
2006 CENTURY WELL SERVICE Brine 0 365
2007 BROAD STREET SERV LLC Brine 0 365
2008 BROAD STREET SERV LLC Brine 0 0
2009 BROAD STREET SERV LLC Brine 0 0
2011 BROAD STREET SERV LLC Brine 0 0
2012 BROAD STREET SERV LLC Brine 0 0
2013 BROAD STREET SERV LLC Brine 0 0
2014 BROAD STREET SERV LLC Brine 0 0
2015 M & R INVESTMENTS OHIO LLC Brine 0 0
2016 M & R INVESTMENTS OHIO LLC Brine 0 0
2017 M & R INVESTMENTS OHIO LLC Brine 0 0
2018 M & R INVESTMENTS OHIO LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1208090362 2018-6-20 0:00: PW No Violations 0.20
-126043234 2008-3-24 0:00: PW No Violations
-1506417260 2008-3-24 0:00: PW No Violations
-1804814323 2008-3-24 0:00: PW No Violations
-1916455080 2018-7-18 0:00: PB No Violations 5.00
-326109707 2015-5-26 0:00: PW No Violations 1.50
-424331467 2008-3-24 0:00: PW No Violations
-847199785 2008-3-24 0:00: PW No Violations
-928035612 2018-7-12 0:00: PB No Violations 1.00
-940270007 2018-6-12 0:00: PW No Violations 0.50
0126043234 2008-03-24 Production Wells No Violations FOLLOW UP TO NOV # 1588549301 Upon inspecting well site found well incapable of producing,tubing is rotted off in the tubing head and 4.5 is rotted in the wellhead, well is venting H2S gas,no I.D. posted and well also has 1-100 bbl tank&separator in need of dike if placed into produ
0159470866 2017-06-12 Production Wells No Violations I was on location today to do a follow-up inspection on this well. During the time of my inspection the company had a dozer on location to dress up the lease road and clear out around the well. I talked with Kenny OBrien during my inspection he was on location. He stated that they are planning on getting a rig in on this well to plug it.
0166004416 2008-03-24 Production Wells No Violations FOLLOW UP TO NOV # 1588549301 Upon inspecting well site found well incapable of producing,tubing is rotted off in the tubing head and 4.5 is rotted in the wellhead, well is venting H2S gas,no I.D. posted and well also has 1-100 bbl tank&separator in need of dike if placed into production.Last production reported on well was back in 1995.
0228555955 2017-03-13 Production Wells No Violations I called Joedy Jasper of M&R Investments and spoke to him about this well. I informed him that the 4 1/2 inch diameter wellhead had rotted off the well and that some of the 2 inch diameter lines appeared to be disconnected or rotted away as well. I told him they need to get a plan together as soon as possible and let me know if they were going to plug or produce the well. If we did not receive a plan ODNR would be moving foreword with stricter enforcement and look to issue a chiefs order on this well. Joedy understood and said he would talk to Kenny of M&R as soon as possible and come up with a plan.
0326109707 2015-05-26 Production Wells No Violations I went out to this well to do a follow-up inspection on the well. The violation has not been resolved and the well is still in violation at this time. I talked with Jake Glasscock to get Ed Butlers number from Broad Street. I tried to contact Ed but it went straight to his voice mail. I left a message for him to contact me.
0424331467 2008-03-24 Production Wells No Violations FOLLOW UP TO NOV # 685618739 FOLLOW UP TO NOV # 1588549301 Upon inspecting well site found well incapable of producing,tubing is rotted off in the tubing head and 4.5 is rotted in the wellhead, well is venting H2S gas,no I.D. posted and well also has 1-100 bbl tank&separator in need of dike if placed into produ
0433608700 2017-11-13 Production Wells No Violations I have returned to this well today to do a follow-up inspection on it. At this time I am unable to do an inspection on the well because the roadway to the well is flooded from the rain that we have had. This is the third time in the last 2 weeks that I have tried to get to the well. I will have to wait until the water level drops so I can get to the well.
0585069053 2018-07-19 Plug / Plug Back No Violations I was back on location today to witness the plugging of this well. Today the rig crew will finish plugging the well through the 4.5 inch diameter casing. The 4.5 inch was shot off at 1850 feet. The rig crew pulled one joint to make sure the pipe was free then Formation Cementing pumped a 300 foot plug to cover the bottom of the surface. The casing was then pulled to the surface to set a 200 foot surface plug. The well is now plugged.
0685618739 2008-03-24 Production Wells No Violations FOLLOW UP TO NOV # 1588549301 Upon inspecting well site found well incapable of producing,tubing is rotted off in the tubing head and 4.5 is rotted in the wellhead, well is venting H2S gas,no I.D. posted and well also has 1-100 bbl tank&separator in need of dike if placed into produ
0847199785 2008-03-24 Production Wells No Violations FOLLOW UP TO NOV # 1588549301 Upon inspecting well site found well incapable of producing,tubing is rotted off in the tubing head and 4.5 is rotted in the wellhead, well is venting H2S gas,no I.D. posted and well also has 1-100 bbl tank&separator in need of dike if placed into production.Last production reported on well was back in 1995.
0928035612 2018-07-12 Plug / Plug Back No Violations I stopped by the well today to see what the plan was but the rig crew had already left for the day.
0940270007 2018-06-12 Production Wells No Violations I was contacted by Larry Fetterman today to let me know they are planning on plugging this well within the next few weeks.
0962841209 2018-07-17 Plug / Plug Back No Violations I was on location today to witness the plugging of this well. Today Appalachian Wireline Services has been called out to shoot the 1.5 inch diameter tubing off. They were only able to get down to 4916 feet. They were getting stuck in the well at this point. I told them to come up to the nearest color and shoot the pipe off. The tubing was shot off at 4884 feet but was still hung in the well. with the stretch we are pulling on the well it looks like we are hung around 2,000 feet. The rig crew is lining up Formation Cementing tomorrow to set one big plug.
1030846799 2018-07-16 Plug / Plug Back No Violations I was on location today to check on the plugging activities of this well. Kenny Wright is rigged up on the well to plug it. They are trying to get the 1.5 inch diameter tubing out of the well. They had to rent an over shot to latch onto the tubing. When they pulled up on the tubing it broke off at the surface. They then had to rent a center sphere to run into the tubing to pull it out but the tubing is hung in the well.
1208090362 2018-06-20 Production Wells No Violations I was contacted by a Larry Fetterman from M&R Investments letting me know that they would be plugging this well in the next few weeks.
1214350543 2008-06-24 Production Wells No Violations Follow up inspection revealed no change in status of well it is still incapable of producing in it present state of repair.
1225407722 2009-03-11 Production Wells Violations Noted Inspection revealed that well is stil incapable of producing,tubing rotted off at wellhead there is sulphur odor at site suspect H2S present at site owner has made no attempts to plug or repair well since Notice of Violation was issued.
1226530399 2008-11-12 Production Wells Violations Noted No change in status of well it is still idle and venting H2S gas,talked to company rep to discuss future plans for said well she stated they would put service rig on well as soon as time permits to see if there was any up hole potential production?.
1250476893 2014-03-03 Production Wells No Violations Compliance Action Follow-up -1506417260: There has been no resolution to any of the issues. I sent Ed butler a list of outstanding compliance actions in Morgan County and explained the issues. He is going to review the list and try to work on resolving well issues.
1369301256 2014-07-29 Production Wells No Violations Compliance Action Follow-up -1506417260: There has been no resolution to any of the issues.
1379618995 2013-09-19 Production Wells No Violations Compliance Action Follow-up -1506417260: There has been no resolution to any of the issues.
1394810074 2014-03-14 Production Wells No Violations Compliance Follow-up -1506417260: I met with the well tender, Kenny, and we drove to inspect the well. He put an identification at the tank battery and will inform Ed Butler of well status.
1419672279 2017-03-09 Production Wells No Violations I was accompanied by Supervisor Eric Conrad today on this inspection. The inspection this day revealed that this well is equipped with a 8 5/8 inch diameter wellhead and 1 1/2 inch diameter production tubing. The tubing has rusted off at the 8 5/8 inch diameter wellhead and there is a 4 1/2 inch diameter wellhead laying on the ground next to the well. All the lines are disconnected or rusted off to the wellhead and the valves are closed at the time of inspection. The tank battery for this well is equipped with a horizontal separator station and a 100 barrel steel tank. Inside the separator station there is a meter box that has been broken off and has no chart in it. The well is currently idle and there has been no resolution to any of the issues with this well.
1506417260 2008-03-24 Production Wells No Violations FOLLOW UP TO NOV # -847199785 FOLLOW UP TO NOV # 1588549301 Upon inspecting well site found well incapable of producing,tubing is rotted off in the tubing head and 4.5 is rotted in the wellhead, well is venting H2S gas,no I.D. posted and well also has 1-100 bbl tank&separator in need of dike if placed into production.Last production reported on well was back in 1995.
1573671018 2016-03-17 Production Wells No Violations There has been no resolution to the issues at this well. Well is still idle.
1588549301 2008-03-24 Production Wells Violations Noted Upon inspecting well site found well incapable of producing,tubing is rotted off in the tubing head and 4.5 is rotted in the wellhead, well is venting H2S gas,no I.D. posted and well also has 1-100 bbl tank&separator in need of dike if placed into production.Last production reported on well was back in 1995.
159470866 2017-6-12 0:00: PW No Violations 1.50
166004416 2008-3-24 0:00: PW No Violations
1750266895 2011-11-10 Production Wells No Violations Inspection this day found well with very corroded wellhead and a hole in the 4.5 casing at ground level. Valves were open and I detected a slight H2S odor. There was no well identification posted. Records in our databae show the last recorded production for this well was in 1996.
1804814323 2008-03-24 Production Wells No Violations FOLLOW UP TO NOV # -126043234 FOLLOW UP TO NOV # 1588549301 Upon inspecting well site found well incapable of producing,tubing is rotted off in the tubing head and 4.5 is rotted in the wellhead, well is venting H2S gas,no I.D. posted and well also has 1-100 bbl tank&separator in need of dike if placed into produ
1892112549 2011-08-11 Production Wells No Violations Inspection this day found well idle, slight odor of H2S. NOV wrote 2008 and still nothing done. Will call company and see why problem has not been addressed. Marijuana near location, might be best to wait until after harvest - royalty owner in area reports much marijuana/cameras. Talked to Ed, supervisor of work crews at Broadstreet - says they were in there recently, plan to have a rig on well and will service, plug if necessary and clean out tanks, post good IDs.
1916455080 2018-07-18 Plug / Plug Back No Violations I was on location today to witness the plugging operations of this well. Today Formation Cementing will be pumping the bottom plug through the 1.5 inch tubing. We were unable to get to bottom with the wireline truck so the tubing was shot at 4884. With the stretch we are getting on the 1.5 inch diameter tubing we are showing free pipe at 1900 feet. So we will be pumping one big plug to cover the bottom zone and the Big Lime plug. A plug was pumped from 4884-3884. Once the plug was set Appalachian Wireline Services ran in the well to shoot the 1.5 inch diameter tubing off. The tubing was shot off at 1870 feet and then pulled from the well. Appalachian Wireline Services then ran back in the well to shoot the 4.5 inch diameter casing off at 1850 feet. The rig crew shut down for the day.
2077222491 2019-8-9 0:00:0 FR No Violations 0.50
228555955 2017-3-13 0:00: PW No Violations 0.50
433608700 2017-11-13 0:00 PW No Violations 0.50
585069053 2018-7-19 0:00: PB No Violations 5.00
685618739 2008-3-24 0:00: PW No Violations
962841209 2018-7-17 0:00: PB No Violations 3.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1225407722 US-OH-106068 2008-03-24 Well insufficiently equipped to prevent escape of oil and gas
1225407722 US-OH-106069 2008-03-24 Failure to legibly identify well
1225407722 US-OH-106070 2008-03-24 Well shall be plugged
1226530399 US-OH-106087 2008-03-24 Well insufficiently equipped to prevent escape of oil and gas
1226530399 US-OH-106088 2008-03-24 Failure to legibly identify well
1226530399 US-OH-106089 2008-03-24 Well shall be plugged
1588549301 US-OH-115540 2008-03-24 Well insufficiently equipped to prevent escape of oil and gas
1588549301 US-OH-115541 2008-03-24 Failure to legibly identify well
1588549301 US-OH-115542 2008-03-24 Well shall be plugged

For data sources see[9]

References