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Well ID: 34-115-22369 | Loading map...
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Country: United States | |
State: Ohio | |
County: Morgan | |
Municipality: Penn Township | |
Operator Name: STONEBRIDGE OPERATING CO LLC | |
Well Pad ID: | |
Farm/Lease Name: POTTS (NICEWANGER) | |
License Status: Final Restoration | |
License Date: 2016-04-18 | |
Spud Date: 1981-03-25 | |
Spud Drilling Contractor: PERKINS DRLG | |
Final Drill Date: 1981-04-03 | |
Well Total Depth: 4903.00 ft | |
Configuration: Vertical | |
Latitude: 39.590000 | |
Longitude: -81.860000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1981-02-09 | 2098 OPI INC GeoDate 2/9/81 |
Unknown | 1981-02-09 | Issued Date 2/9/81 Expired Date 2/9/82 Acres 0000000 Tool Type RTA Proposed Formation Proposed Depth 04903 Proposed Drill Depth 04903 |
Original Spud | 1981-03-29 | |
Completed | 1981-04-03 | |
Reached Total Depth | 1981-04-03 | |
Completion Report Received | 1981-08-20 | |
CO | 1994-06-28 | 631 BT ENERGY CORP GeoDate 2/9/81 |
Change of Owner | 2007-10-12 | Operator changed from 631, BT ENERGY CORP to 2070, STONEBRIDGE OPERATING CO |
APP | 2016-04-18 | Proposed Formations:CLINOTN, Issued Date:4/18/2016, Expired Date:4/18/2018 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:HAD, Proposed Well Class: |
Plugged/Abandoned | 2016-11-09 | |
Record Last Modified | 2017-10-03 | |
Construction Permit Expires | 2018-04-18 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 4756 | 4761 | 12 |
4756 | 4761 | 12 | |
4756 | 4761 | 12 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 700 Bbl | 50000 | X-LINK |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | BT ENERGY CORP | 0.00 | 65.00 | 365 |
1985 | BT ENERGY CORP | 1572.00 | 126.00 | 365 |
1986 | BT ENERGY CORP | 1714.00 | 126.00 | 365 |
1987 | BT ENERGY CORP | 1243.00 | 185.00 | 365 |
1988 | BT ENERGY CORP | 1475.00 | 419.00 | 365 |
1991 | BT ENERGY CORP | 0.00 | 0.00 | 365 |
1993 | BT ENERGY CORP | 1101.00 | 0.00 | 365 |
1994 | BT ENERGY CORP | 742.00 | 89.00 | 365 |
1995 | BT ENERGY CORP | 0.00 | 0.00 | 0 |
1996 | BT ENERGY CORP | 0.00 | 0.00 | 0 |
1997 | BT ENERGY CORP | 0.00 | 0.00 | 0 |
1998 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 0 |
2000 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 366 |
2001 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 0 |
2002 | BT ENERGY CORP | 0.00 | 0.00 | 0 |
2003 | BT ENERGY CORP | 0.00 | 0.00 | 0 |
2004 | BT ENERGY CORP | 43.00 | 3.00 | 7 |
2005 | BT ENERGY CORP | 75.00 | 52.00 | 7 |
2006 | BT ENERGY CORP | 0.00 | 8.00 | 196 |
2007 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 343 |
2008 | STONEBRIDGE OPERATING CO LLC | 0.00 | 73.00 | 365 |
2009 | STONEBRIDGE OPERATING CO LLC | 23.00 | 0.00 | 7 |
2010 | STONEBRIDGE OPERATING CO LLC | 50.00 | 0.00 | 273 |
2011 | STONEBRIDGE OPERATING CO LLC | 101.00 | 0.00 | 0 |
2012 | STONEBRIDGE OPERATING CO LLC | 15.00 | 0.00 | 364 |
2013 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 365 |
2014 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 365 |
2015 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 357 |
2016 | STONEBRIDGE OPERATING CO LLC | 0.00 | 0.00 | 357 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1165367444 | 2017-4-12 0:00: | PB | No Violations | |
-1376711486 | 2017-9-26 0:00: | FR | No Violations | 1.00 |
-1476972195 | 2014-4-1 0:00:0 | PW | No Violations | 1.00 |
0134014622 | 2012-10-31 | Production Wells | Violations Noted | This well was part of the complaint inspection for #21937. Upon inspection I found the well to be incapable of production. There was a pump jack at well head which was incapable of pumping due to disabled motor and broken belt. The pump jack is in poor condition. The well was equipped with 8 and 4 1/2 casing as well as tubing and rod. All of the plastic lines running from the wellhead to house and tank battery at the road have been cut and plowed up by landowner with a bulldozer within the last week to gain access to the wellhead and pumpjack. The valves were all turned on at the wellhead and the landowner stated there has been no production out of this well and the house gas was shut off in 2002. The Tank battery was freshly painted. There was no current chart on the meter and the steel sales line was disconnected and damaged. There are two 100 barrel tanks and one 450 gallon plastic drum in battery. There is oil contamination in dike which appears to be from plastic drum. There is no ID at wellhead or tank battery. Stonebridge is currently and has been reporting production on this well. Stonebridge needs to plug the well. Failure to comply may result in forfeiture of bond. |
0745197068 | 2013-11-20 | Production Wells | No Violations | Compliance Action Follow-Up #134014622:There has been no resolution to any of the issues. The landowner has a restraining order on the operator therefore they cannot go on to property to service the well. |
0799809702 | 2015-07-28 | Production Wells | No Violations | I was at this well to do a follow-up inspection on it. At this time the well is not capable of production. The well is still in violation at this time. I took pictures off my findings during my inspection. |
0841765074 | 2014-09-15 | Production Wells | No Violations | Compliance Action Follow-Up #134014622: The well is still idle and there is an old chart on the meter. The production lines are still broken and scattered across the property all the way downhill to the wellhead. The valves are shut on the separator. There is no motor on the pumpjack. The landowner was present and stated that the yellow plastic lines were his and that his father had bought and laid those lines a long time ago for domestic gas. There is a 55 gallon drum adjacent to the wellhead which is starting to leak. |
0971059714 | 2014-02-21 | Production Wells | No Violations | Compliance Action Follow-Up #134014622: The well is still idle and there is an old chart on the meter. The production lines are still broken and scattered across the property all the way downhill to the wellhead. There has been no resolution to any of the issues. The landowner has a restraining order on the operator therefore they cannot go on to property to service the well. |
1042563377 | 2015-11-18 | Production Wells | No Violations | I returned to this well to do a follow-up inspection on it. The well is still currently sitting idle with no change in it being capable of production. The well is in violation. |
1165367444 | 2017-04-12 | Plug / Plug Back | No Violations | I was on location today to do a field inspection on this well. At this time I am unable to pass the final restoration because the plastic flow line is still on location. I will check back at a later date for the final restoration. |
1221745410 | 2016-11-07 | Plug / Plug Back | No Violations | I was on location on 11/7/2016 to witness the well plugged by Huffman & Bowers. Barry set a Clinton Sand plug (4630-4230 feet), a Big Lime/rip plug (3520-3320 feet), a bottom of surface plug (1740-1540 feet), and a surface plug (200-0 feet). Barry was able to rip the pipe off at around 3520 feet. They then pulled one joint to about 3479 feet where we set our rip plug. All 4 1/2 inch diameter casing was pulled from the hole after plugging was finished. The Berea was covered by the surface casing and no individual plug was needed. |
134014622 | 2012-10-31 0:00 | PW | No Violations | 3.50 |
1376711486 | 2017-09-26 | Final Restoration | No Violations | The final restoration meets 150.072 B requirements. |
1470359970 | 2015-08-17 | Production Wells | No Violations | I was on location to do a follow-up inspection on the well. There has been no change to the well. The well is still incapable of production and is still in violation. I took updated photos of the well during my inspection. |
1476972195 | 2014-04-01 | Production Wells | No Violations | Compliance Action Follow-Up #134014622: The well is still idle and there is an old chart on the meter. The production lines are still broken and scattered across the property all the way downhill to the wellhead. The valves at the wellhead are now open however the steel line that runs up to tank battery is closed at the separator. There is still an old chart on the meter. I will refer this well to supervisor for legal review. |
1478180136 | 2016-11-03 | Plug / Plug Back | No Violations | I was on location to plug this well. Barry Bowers was the plug and cementing operator on this well. Barry had called me previously to say the rods and tubing were stuck in the hole. He then called me to inform me they had gotten them free and were going to plug Thursday November 3rd. When I arrived on site he was unable to get the 1 1/2 inch diameter tubing back to the bottom of the hole. I then contacted Inspector Smith to see what should be done. He suggested running the tools to the bottom of the hole to unblock whatever it was. Barry was not comfortable doing that in fear the tools would get stuck. I then called Supervisor Conrad and he suggested milling the hole. Barry wanted to try to work the tubbing to the bottom of the hole before trying that. No other updates to report at this time. |
1855698300 | 2013-02-11 | Production Wells | No Violations | Compliance Action Follow-Up #134014622: Identification has been posted on the tank, however Stonebridge has yet to resolve the remainder of the previous compliance actions. I called and left a message with John Schnieder of Stonebridge in regards to the compliance actions. |
745197068 | 2013-11-20 0:00 | PW | No Violations | 0.30 |
799809702 | 2015-7-28 0:00: | PW | No Violations | 1.00 |
841765074 | 2014-9-15 0:00: | PW | No Violations | |
971059714 | 2014-2-21 0:00: | PW | No Violations | 0.20 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0134014622 | US-OH-109789 | 2012-12-12 | Forfeiture of bond | |
0134014622 | US-OH-109790 | 2012-12-12 | Failure to legibly identify well | |
0134014622 | US-OH-109791 | 2012-12-12 | Well shall be plugged |
For data sources see[9]