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34-115-22290

Well Details

Well ID: 34-115-22290
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Country: United States
State: Ohio
County: Morgan
Municipality: Center Township
Operator Name: STONEBRIDGE OPERATING CO LLC
Well Pad ID:
Farm/Lease Name: TAYLOR LEORA
License Status: Final Restoration
License Date: 2015-12-23
Spud Date: 1981-01-12
Spud Drilling Contractor:
Final Drill Date: 1981-01-27
Well Total Depth: 1835.00 ft
Configuration: Vertical
Latitude: 39.600000
Longitude: -81.590000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1980-12-31 335 BERRESFORD ENTERPRISES IN GeoDate 12/31/80
Oil and Gas 1980-12-31 Issued Date 12/31/80 Expired Date Acres 0080000 Tool Type RTA Proposed Formation BEREA Proposed Depth 01835 Proposed Drill Depth 01835
Original Spud 1981-01-12
Completed 1981-01-27
Reached Total Depth 1981-01-27
Completion Report Received 1981-06-13
CO 1995-06-27 2070 HALWELL COMPANY GeoDate 12/31/80
APP 2015-12-23 Proposed Formations:BEREA, Issued Date:12/23/2015, Expired Date:12/22/2017 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:HAD, Proposed Well Class:
Plugged/Abandoned 2016-01-28
Record Last Modified 2017-02-10
Construction Permit Expires 2017-12-22

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1781 1783 5
2006-09-11 1788 1792 9
1781 1783 5
1781 1783 5

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 28 250 Gal 0
H2O 0 900 Bbl 30000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 BERRESFORD ENTERPRISES IN 0.00 0.00 0
1985 BERRESFORD ENTERPRISES IN 0.00 0.00 365
1995 STONEBRIDGE OPERATING CO LLC 0.00 0.00 7
1996 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
1997 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
1998 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2000 STONEBRIDGE OPERATING CO LLC 0.00 0.00 366
2001 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2002 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2003 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2004 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2005 STONEBRIDGE OPERATING CO LLC 16.00 0.00 0
2006 STONEBRIDGE OPERATING CO LLC 46.00 0.00 0
2007 STONEBRIDGE OPERATING CO LLC 0.00 0.00 7
2008 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2009 STONEBRIDGE OPERATING CO LLC 34.00 0.00 0
2010 STONEBRIDGE OPERATING CO LLC 61.00 0.00 70
2011 STONEBRIDGE OPERATING CO LLC 94.00 0.00 0
2012 STONEBRIDGE OPERATING CO LLC 116.00 0.00 0
2013 STONEBRIDGE OPERATING CO LLC 130.00 0.00 0
2014 STONEBRIDGE OPERATING CO LLC 47.00 0.00 0
2015 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0
2016 STONEBRIDGE OPERATING CO LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 BERRESFORD ENTERPRISES IN Brine 0 0
1985 BERRESFORD ENTERPRISES IN Brine 2990 365
1995 STONEBRIDGE OPERATING CO LLC Brine 0 7
1996 STONEBRIDGE OPERATING CO LLC Brine 0 0
1997 STONEBRIDGE OPERATING CO LLC Brine 0 0
1998 STONEBRIDGE OPERATING CO LLC Brine 0 0
2000 STONEBRIDGE OPERATING CO LLC Brine 0 366
2001 STONEBRIDGE OPERATING CO LLC Brine 0 0
2002 STONEBRIDGE OPERATING CO LLC Brine 0 0
2003 STONEBRIDGE OPERATING CO LLC Brine 0 0
2004 STONEBRIDGE OPERATING CO LLC Brine 0 0
2005 STONEBRIDGE OPERATING CO LLC Brine 0 0
2006 STONEBRIDGE OPERATING CO LLC Brine 0 0
2007 STONEBRIDGE OPERATING CO LLC Brine 0 7
2008 STONEBRIDGE OPERATING CO LLC Brine 0 0
2009 STONEBRIDGE OPERATING CO LLC Brine 0 0
2010 STONEBRIDGE OPERATING CO LLC Brine 0 70
2011 STONEBRIDGE OPERATING CO LLC Brine 0
2012 STONEBRIDGE OPERATING CO LLC Brine 0 0
2013 STONEBRIDGE OPERATING CO LLC Brine 0 0
2014 STONEBRIDGE OPERATING CO LLC Brine 0 0
2015 STONEBRIDGE OPERATING CO LLC Brine 0 0
2016 STONEBRIDGE OPERATING CO LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1301086594 2016-11-8 0:00: FR No Violations 2.00
-1519880277 2016-1-28 0:00: PB No Violations 8.00
-1942342125 2014-2-10 0:00: PW No Violations 0.70
-2037907190 2015-8-18 0:00: PW No Violations 1.00
-2057466632 2014-9-16 0:00: PW No Violations
-750399925 2014-3-13 0:00: AM No Violations
0136681156 2014-05-20 Production Wells No Violations The well is still idle and there has been no resolution to any of the issues.
0750399925 2014-03-13 Administrative Inspection No Violations Stonebridge has reported production to the state. Eddie Biehl asked the state for an extension of time until April 25 to evaluate this well and legal situation. In this time they will apply for either a permit to plug back and re-complete or to plug and abandon. He asked to then be allowed to utilize up to the full term of the permit to resolve outstanding legal issues including any pending or potential litigation in the local Court of Common Pleas. Once they are able to clear the legal issues, they will safely perform the work in the field.
1022070021 2014-05-19 Production Wells No Violations Compliance Action Follow-up 1363031771: There has been no resolution to any of the issues and the well is still not capable of production. I talked to John Schneider and he stated that he had applied for a plug permit around 4 weeks ago but it was not yet processed due to missing information. He said to expect it here shortly. He did not know when they were actually going to plug the well.
1291438803 2013-11-04 Production Wells No Violations Compliance Action Follow-up 1363031771:There has been no resolution to any of the issues and John Schneider has been informed that the lease has been broken and that Stonebridge is required to plug the well.
1301086594 2016-11-08 Final Restoration No Violations This well was plugged and abandoned earlier this year. The inspection today revealed that this well has had all equipment removed, vegetation has been established, the pit has been closed and buried, and erosion has been controlled. This well has passed final restoration in accordance with ORC 1509.072(B).
1363031771 2013-03-11 Production Wells Violations Noted This inspection is for a landowner complaint. The inspection revealed an idle well with a pumpjack, separator, and a 50 barrel tank. There is no identification. The pumpjack has a motor with a broken belt. The separator is broken and laying on the ground. The tank is empty and completely rusted through on the top and bottom, and there is no dike. The steel line at the tank from the wellhead is broken and rusted to pieces. The valves on the 4.5 casing are closed and the valves on the 2 tubing are open leading to the tank. The well was leaking gas at the top of the 4.5. Landowner stated that they received house gas over 15 years ago and owned the pumpjack which they used to relieve well of fluid. It produced too much water so they stopped using house gas. She stated the well has never produced anything except house gas. She said Stonebridge came out around 2011 and said they bought the well, painted just the wellhead and production suddenly showed up on the state website. Their attorney has filed a Affidavit for forfeiture of lease with the courthouse and a Notice to Recorder to Cancel Lease dated 2/28/2013. Operator must make well capable of production within 30 days; or plugging is required in 30 days. Failure to comply may result in forfeiture of bond.
136681156 2014-5-20 0:00: PW No Violations
1369757661 2013-05-28 Administrative Inspection Violations Noted Compliance Action Follow-up 1363031771: I obtained the Affidavit of Forfeiture and the Notice to Cancel lease that the Skinners lawyer had filed at the courthouse. I also obtained the new lease that the Skinners had signed with Triad Hunter LLC. Stonebridge no longer holds the lease and must plug the well.
1519880277 2016-01-28 Plug / Plug Back No Violations On location to witness plugging operations and to train Inspector Brian Sefcik on well plugging. Matheny Well Services is the plugging contractor. 1.5 tubing was set at 1781 and Formation Cementing pumped a 400 bottom plug inside of 3.5 casing using 21 sks class A cement and 3.5 bbls of freshwater displacement. Tubing was pulled OOH and Appalachian Well Surveys was brought in to determine free point on the 3.5 casing and shoot it off. A VDL log revealed that the well bored was caved in on the casing-hole annulus all the way to approximately 350. Casing was shot off at 332 and a solid plug was set through the 3.5 casing from 332-0. The remaining casing was pulled OOH and cement was topped off from surface.
1789174751 2015-07-21 Production Wells No Violations I was at this well to do a follow-up inspection on it. The well is still idle at this time. The valves are shut at the wellhead making it incapable of production. I took pictures of my findings during my inspection.
1839707120 2015-11-17 Production Wells No Violations I returned to this well to do a follow-up inspection on it. The well is still currently sitting idle with no change in it being capable of production. The well is in violation.
1928824360 2013-05-01 Production Wells No Violations Compliance Action Follow-Up 1363031771: There has been no resolution to any of the well issues. Landowner told me that they have already broken the lease and signed and received money from Triad Resources.
1942342125 2014-02-10 Production Wells No Violations Compliance Action Follow-up 1363031771: The well is still not in production and there is still a broken separator laying on the ground and rusted tank adjacent to the wellhead. The wellhead was bubbling with gas and the valve was open on the tubing but the flow line was shut at the broken end of separator line. I saw the landowner and he stated that they own the equipment. There has been no resolution to any of the issues.
2037907190 2015-08-18 Production Wells No Violations I was on location to do a follow-up inspection on the well. There has been no change to the well. The well is still incapable of production and is still in violation. I took updated photos of the well during my inspection.
2057466632 2014-09-16 Production Wells No Violations Compliance Action Follow-up 1363031771: The well is not in production, there is a broken separator laying on the ground, and the tank adjacent to the wellhead is rusted through the sides. The valve was open on the tubing but the flow line was shut at the broken end of separator line. The valve on the annulus is closed and disconnected from old house gas line. The lines from the wellhead to the tank and separator are broken and rusted in various places. There is no identification posted at location.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1363031771 US-OH-110612 2014-04-10 Forfeiture of bond
1363031771 US-OH-110613 2014-04-10 Well insufficiently equipped to prevent escape of oil and gas
1363031771 US-OH-110614 2014-04-10 Failure to legibly identify well
1363031771 US-OH-110615 2014-04-10 No SPCC dike/or failure to keep dike free of water or oil
1363031771 US-OH-110616 2014-04-10 Well shall be plugged
1363031771 US-OH-110617 2014-04-10 Nonproduction; well shall be plugged or placed in temporary inactive status
1363031771 US-OH-110618 2014-04-10 Defective casing, leaking well
1369757661 US-OH-110908 2014-04-10 Failure to submit water samples urban

For data sources see[9]

References