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34-115-22040

Well Details

Well ID: 34-115-22040
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Country: United States
State: Ohio
County: Morgan
Municipality: Malta Township
Operator Name: DIVERSIFIED PRODUCTION LLC
Well Pad ID:
Farm/Lease Name: DODRILL CARL D
License Status: Producing
License Date: 1980-01-17
Spud Date: 1980-06-05
Spud Drilling Contractor:
Final Drill Date: 1980-06-26
Well Total Depth: 1451.00 ft
Configuration: Vertical
Latitude: 39.670000
Longitude: -81.930000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1980-01-17 1868 DUSTY DRILL & PRO CORP GeoDate 1/17/80
Oil and Gas 1980-01-17 Issued Date 1/17/80 Expired Date Acres 0010000 Tool Type CT Proposed Formation BEREA Proposed Depth 00000 Proposed Drill Depth 00000
Original Spud 1980-06-05
Completed 1980-06-26
Reached Total Depth 1980-06-26
Completion Report Received 1980-07-29
Change of Owner 2003-11-05 Operator changed from 1868, DUSTY DRILL & PRO CORP to 2867, DNL OIL CORP
Change of Owner 2007-07-11 Operator changed from 2867, DNL OIL CORP to 8227, DEEP RESOURCES LLC
Change of Owner 2011-10-13 Operator changed from 8227, DEEP RESOURCES LLC to 8685, M & R INVESTMENTS OHIO LLC
Record Last Modified 2013-10-03

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1390 1399 1
1390 1399 1
1390 1399 1

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 900 Bbl 25000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 DUSTY DRILLING & PRODUCING COR 1643.00 139.00 0
1985 DUSTY DRILLING & PRODUCING COR 1246.00 115.00 363
1986 DUSTY DRILLING & PRODUCING COR 1236.00 110.00 365
1987 DUSTY DRILLING & PRODUCING COR 1000.00 76.00 365
1988 DUSTY DRILLING & PRODUCING COR 401.00 82.00 330
1989 DUSTY DRILLING & PRODUCING COR 392.00 74.00 358
1990 DUSTY DRILLING & PRODUCING COR 392.00 91.00 323
1991 DUSTY DRILLING & PRODUCING COR 527.00 98.00 365
1992 DUSTY DRILLING & PRODUCING COR 455.00 70.00 358
2004 DNL OIL CORP 0.00 48.00 100
2005 DNL OIL CORP 391.00 63.00 365
2006 DNL OIL CORP 188.00 48.00 365
2007 DEEP RESOURCES LLC 21.00 0.00 180
2010 DEEP RESOURCES LLC 185.00 44.00 365
2011 DEEP RESOURCES LLC 293.00 20.00 90
2012 M & R INVESTMENTS OHIO LLC 0.00 0.00 366
2013 M & R INVESTMENTS OHIO LLC 0.00 41.00 365
2014 M & R INVESTMENTS OHIO LLC 0.00 20.00 365
2015 M & R INVESTMENTS OHIO LLC 0.00 38.00 365
2016 M & R INVESTMENTS OHIO LLC 0.00 0.00 0
2017 M & R INVESTMENTS OHIO LLC 0.00 0.00 0
2018 M & R INVESTMENTS OHIO LLC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 DUSTY DRILLING & PRODUCING COR Brine 0 0
1985 DUSTY DRILLING & PRODUCING COR Brine 360 363
1986 DUSTY DRILLING & PRODUCING COR Brine 342 365
1987 DUSTY DRILLING & PRODUCING COR Brine 274 365
1988 DUSTY DRILLING & PRODUCING COR Brine 275 330
1989 DUSTY DRILLING & PRODUCING COR Brine 248 358
1990 DUSTY DRILLING & PRODUCING COR Brine 307 323
1991 DUSTY DRILLING & PRODUCING COR Brine 303 365
1992 DUSTY DRILLING & PRODUCING COR Brine 215 358
2004 DNL OIL CORP Brine 0 100
2005 DNL OIL CORP Brine 75 365
2006 DNL OIL CORP Brine 52 365
2007 DNL OIL CORP Brine 32 183
2010 DEEP RESOURCES LLC Brine 78 365
2011 DEEP RESOURCES LLC Brine 0 90
2012 M & R INVESTMENTS OHIO LLC Brine 0 366
2013 M & R INVESTMENTS OHIO LLC Brine 404 365
2014 M & R INVESTMENTS OHIO LLC Brine 262 365
2015 M & R INVESTMENTS OHIO LLC Brine 0 365
2016 M & R INVESTMENTS OHIO LLC Brine 67 0
2017 M & R INVESTMENTS OHIO LLC Brine 0 0
2018 M & R INVESTMENTS OHIO LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1351313991 2013-11-18 0:00 PW No Violations 0.80
-1597181476 2014-10-15 0:00 PW No Violations
-1945816425 2014-4-15 0:00: AM No Violations
-1971041797 2014-11-5 0:00: PW No Violations
-2128778058 2014-3-4 0:00:0 PW No Violations 0.30
-243118604 2014-9-23 0:00: PW No Violations
-426172291 2014-2-27 0:00: PW No Violations 0.30
-440694095 2014-3-28 0:00: PW No Violations 0.20
-682300317 2015-3-26 0:00: PW No Violations 1.50
0243118604 2014-09-23 Production Wells No Violations Compliance Action Follow-up -1351313991: Andy has been working the location with dozer and is planning on bringing topsoil and gravel in the next few days. He will also remove the plastic tank.
0315605380 2014-06-23 Production Wells No Violations Compliance Action Follow-up -1351313991: There is still a scald area and contamination just outside of the dike. The plastic tank is still present and 3/4 full of fluid. I talked with Andy and asked him about the cleanup and he stated he will begin working on it this week. He stated that they could not rent any equipment due to unpaid bills but now they are clean and can move in and clean up the dike location.
0426172291 2014-02-27 Production Wells No Violations Compliance Action Follow-up -1351313991: There has been no resolution to any of the issues. I left Rusty Hutson a message in regards to the pollution and contamination clean-up. Andy was present and he said he would notify his boss. I talked with the field supervisor Jody Jasper and he said they would get on all of these problems this week.
0440694095 2014-03-28 Production Wells No Violations Compliance Action Follow-up -1351313991: Andy has cleaned up and graveled the main dike, however there is oil contamination that spilled from the smaller plastic tank. Andy stated he was not aware of this issue and will take care of it today. He still needs to bring in a backhoe and remove scald area and restore vegetative growth.
0682300317 2015-03-26 Production Wells No Violations Compliance Action Follow-up -1351313991: The plastic tank has been removed from location; however, there is still contamination outside and inside dike. I called and left a message with Supervisor, Rusty Hutson about the dike issues.
0708322628 2015-01-12 Production Wells No Violations Compliance Action Follow-up -1351313991: The plastic tank is still slowly leaking brine from the bottom. The operator needs to drain and remove the tank in order to prevent further contamination issues outside of the dike. I sent a message to the Field Supervisor Rusty Hutson in regards to the issues.
1343837529 2017-02-28 Production Wells No Violations The inspection this day revealed that this well is equipped with a pumping unit, a 4 1/2 inch diameter wellhead, and 1 1/2 inch diameter production tubing. The valves were closed on this wellhead at the time of inspection. The tank battery for this well is equipped with two (2) 100 barrel steel tanks and a vertical separator. I ran into Luke Mallet at the tank battery and spoke with him about the wells in this area. This tank battery previously had a spill on it that is still being cleaned up. He had thrown down more lime to try to neutralize the chlorides still left in the soil. Luke informed me he had seeded the area and had some of it growing but the deer had come along and eaten the freshly grown grass. Luke also informed me the well was closed in due to him having an issue with a pin on the bridle on the well that was giving him issues with pumping the well. Luke was waiting for some parts to be able to fix the well and the well would be back online after. There are no issues to report at this time.
1351313991 2013-11-18 Production Wells Violations Noted This is a tank battery inspection. There is brine contamination inside the dike due to leaking lines. There is a 1500gallon tank on down slope side. There are lines leaking into the second plastic tank dike, and it appears that this plastic holding tank has also overflowed in the past. The contaminated area heads down slope about 100 feet. Pictures were taken of the entire area. Operator must remove all contamination in this area and replace any leaking lines or equipment. Operator must restore vegetative growth.
1386605302 2013-12-09 Production Wells No Violations Compliance Action Follow-up -1351313991: Rusty Hutson stated Andy was going to begin cleanup several weeks ago and there has been no effort to take care of the issues.
1419369958 2014-12-23 Production Wells No Violations Compliance Action Follow-up -1351313991: There has been recent excavation of the contaminated soil. Andy Corp, with M & R, has also spread seed and straw all over the area. The 1500 gallon plastic tank is still in same spot and is half full of waste. It appears to have some leak issues underneath. I called Andy and Rusty and told them the tank needs to be removed or replaced with a proper storage tank. Andy said he would take care of the issues.
1421770916 2011-01-20 Production Wells No Violations Compliance Action Follow-up -1351313991: Operator removed the plastic tank from the location. There are no more issues to report at this time.
1597181476 2014-10-15 Production Wells No Violations Compliance Action Follow-up -1351313991: Operator has not cleaned up area and there are signs of leaks in various places. I will refer this well to supervisor for legal review.
1945816425 2014-04-15 Administrative Inspection No Violations Compliance Action Follow-up -1351313991: Andy called and stated he has a backhoe lined up and will have it back in compliance by end of the week.
1971041797 2014-11-05 Production Wells No Violations Compliance Action Follow-up -1351313991: I met with field supervisor, Rusty Hutson, and he will have heavy equipment and dumptruck out to take care of contamiantion as soon as possible.
2128778058 2014-03-04 Production Wells No Violations Compliance Action Follow-up -1351313991: Andy has cleaned up and performed some work in the dike, however the contamination issues outside of the dike are still present and will need better weather for cleanup and restoration. He stated that he has corrected the various line leaks, but I will continue to monitor this area and his progress until the are is in compliance.
315605380 2014-6-23 0:00: PW No Violations
708322628 2015-1-12 0:00: PW No Violations 0.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1351313991 US-OH-110172 2015-01-26 Well operation causing pollution and contamination
1351313991 US-OH-110173 2015-01-26 Equipment pressure rated below operating pressure
1351313991 US-OH-110174 2015-01-26 No SPCC dike/or failure to keep dike free of water or oil
1351313991 US-OH-110175 2015-01-26 Dike or pit not able to prevent escape of brine or other wastes

For data sources see[9]

References