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34-115-21984

Well Details

Well ID: 34-115-21984
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Country: United States
State: Ohio
County: Morgan
Municipality: Deerfield Township
Operator Name: H L ALTIER SERVICE CO INC
Well Pad ID:
Farm/Lease Name: TAYLOR
License Status: Final Restoration
License Date: 2014-09-29
Spud Date: 1980-02-18
Spud Drilling Contractor:
Final Drill Date: 1980-03-24
Well Total Depth: 1378.00 ft
Configuration: Vertical
Latitude: 39.660000
Longitude: -81.990000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1979-12-12 1512 ALTIER H L SERVICE CO INC GeoDate 12/12/79
Original Spud 1980-02-18
Completed 1980-03-24
Reached Total Depth 1980-03-24
Correction to Well 2008-11-07 CORRECTION TO X, Y COORDINATES; X= 2,141,410 AND Y= 607,679.
APP 2014-09-29 Proposed Formations:BEREA, Issued Date:9/29/2014, Expired Date:9/28/2016 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2015-01-23
Construction Permit Expires 2016-09-28
Record Last Modified 2017-02-10

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1339 1343 1
1339 1343 1
1339 1343 1

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 18000 Gal 6500

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1991 H L ALTIER SERVICE CO INC 0.00 25.00 35
1992 H L ALTIER SERVICE CO INC 0.00 20.00 30
1993 H L ALTIER SERVICE CO INC 0.00 20.00 30
1994 H L ALTIER SERVICE CO INC 0.00 20.00 30
1995 H L ALTIER SERVICE CO INC 0.00 5.00 30
2009 H L ALTIER SERVICE CO INC 0.00 0.00 0
2010 H L ALTIER SERVICE CO INC 0.00 0.00 0
2011 H L ALTIER SERVICE CO INC 0.00 0.00 0
2012 H L ALTIER SERVICE CO INC 0.00 0.00 0
2013 H L ALTIER SERVICE CO INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1991 H L ALTIER SERVICE CO INC Brine 10 35
1992 H L ALTIER SERVICE CO INC Brine 10 30
1993 H L ALTIER SERVICE CO INC Brine 10 30
1994 H L ALTIER SERVICE CO INC Brine 10 30
1995 H L ALTIER SERVICE CO INC Brine 5 30
2009 H L ALTIER SERVICE CO INC Brine 0 0
2010 H L ALTIER SERVICE CO INC Brine 0 0
2011 H L ALTIER SERVICE CO INC Brine 0 0
2012 H L ALTIER SERVICE CO INC Brine 0 0
2013 H L ALTIER SERVICE CO INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1099003537 2014-2-13 0:00: PW No Violations 0.50
-1549856405 2014-6-23 0:00: PW No Violations
-1878098072 2015-3-26 0:00: PB No Violations 2.00
-2112382723 2015-7-8 0:00:0 FR No Violations
-242332708 2013-7-12 0:00: PW No Violations 0.30
-734533749 2005-9-14 0:00: PW No Violations
-826272942 2014-6-23 0:00: PW No Violations
0199750800 2015-09-01 Final Restoration No Violations The final restoration meets 1509.072B.
0242332708 2013-07-12 Production Wells Violations Noted I found an overgrown pumpjack with valves open however I could no find the tank associated with this well. It is hard to tell if this well is actually in production especially since no production has been reported since 1995. I called Tim Altier and left a message concerning the issues. Operator must report production to the state, and operator must post ID and must make well capable of production within 60 days; or plugging is required in 60 days. 7/16/2013: Tim Altier called and said the well is incapable of producing and it is no longer providing house gas. He is going to try and work out a way to plug the well.
0443538079 2015-02-12 Plug / Plug Back No Violations The casing, tubing, and pumpjack are still on location. The areas has not yet been graded and there are still pieces of steel and plastic flowline in various places as well as the electric wire. I will continue to monitor the restoration.
0734533749 2005-09-14 Production Wells No Violations Well appears to be hooked up,but no production has been reported on well in quite some time.

Will need to contact company rep and find out why they are not reporting production.

0826272942 2014-06-23 Production Wells No Violations Compliance Action Follow-up -242332708: The well is still equipped with an idle pumpjack. There has been no resolution to any of the issues.
1022431627 2013-10-21 Production Wells No Violations Compliance Action Follow-up -242332708: There has been no resolution to any of the issues.
1099003537 2014-02-13 Production Wells No Violations Compliance Action Follow-up -242332708: The well is still equipped with an idle pumpjack. There has been no resolution to any of the issues. I left a message with Tim Altier in regards to the well issues.
1346795453 2015-01-23 Plug / Plug Back No Violations I was onsite to witness the plugging of this well. Kenny Wright and his rig crew were on location when I arrived. They rigged up their 4 tools to tag the cement plug. They ran the tools down hole and tagged the plug at 1042. They then brought the tools back out of the hole and put the ripper on the bottom. They ran back in the well to find telegraph and started ripping the 4.5 at 826ft. They were able to rip the 4.5 at 826ft. The 4.5 was pulled up to 370ft and a plug was set to the surface. The well will be left open over the weekend and checked on Monday .
1422293310 2015-01-22 Plug / Plug Back No Violations I was on location to witness Kenny Wright of Wright Well Services and formation Cement Company set the bottom hole Berea Plug. Formation set the plug from 1124-1378 using 20 sacks of Class A cement.
1549856405 2014-06-23 Production Wells No Violations Compliance Action Follow-up -242332708: The well is still equipped with an idle pumpjack. There has been no resolution to any of the issues. I talked to Tim Altier and he is going to apply for a plug permit this week and line up a rig for this summer to plug the well.
1878098072 2015-03-26 Plug / Plug Back No Violations The pumpjack and casing was still on location. There were sections of line still lying around and the wellhead was still open with cement around 10 down. I met with Pat Altier and he stated he was in charge of restoration and was planning on getting the location complete once the ground was dry enough to move in heavy equipment.
199750800 2015-9-1 0:00:0 FR No Violations 1.00
2112382723 2015-07-08 Final Restoration No Violations I went out to this well to do a final restoration on it. I was unable to pass the final restoration because the well has not been cut off at the surface. The plastic line is still on location along with the pumping unit and some electric line. Once all the equipment and reclaiming has been done I can pass the final restoration.
2131060594 2015-01-20 Plug / Plug Back No Violations Kenny Wright of Wright Well Services has his service rig on location. He has removed the pumpjack and pulled the rods and 41 joints of tubing from the well. There was no activity on the well today.
443538079 2015-2-12 0:00: PB No Violations 0.20

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0242332708 US-OH-122436 2015-02-02 Failure to legibly identify well
0242332708 US-OH-122437 2015-02-02 Well shall be plugged
0242332708 US-OH-122438 2015-02-02 Nonproduction; well shall be plugged or placed in temporary inactive status
0242332708 US-OH-122439 2015-02-02 Statement of annual production not filed

For data sources see[9]

References