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34-115-21290

Well Details

Well ID: 34-115-21290
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Country: United States
State: Ohio
County: Morgan
Municipality: Bristol Township
Operator Name: KNOX ENERGY INC.
Well Pad ID:
Farm/Lease Name: MABEL LAWRENCE HEIRS
License Status: Final Restoration
License Date: 2014-11-17
Spud Date: 1972-06-13
Spud Drilling Contractor:
Final Drill Date: 1972-07-08
Well Total Depth: 4752.00 ft
Configuration: Vertical
Latitude: 39.690000
Longitude: -81.770000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1972-06-13 199 WORTHINGTON OIL CO INC GeoDate 6/13/72
Oil and Gas 1972-06-13 Issued Date 6/13/72 Expired Date 6/13/73 Acres 0000000 Tool Type Proposed Formation Proposed Depth 00000 Proposed Drill Depth 00000
Original Spud 1972-06-13 INJECTION PERMIT EXPIRED, WELL NOT CONVERTED CONVERT 1-30-99, CONVERT SWIW 10-18-97
Completed 1972-07-08 INJECTION PERMIT EXPIRED, WELL NOT CONVERTED CONVERT 1-30-99, CONVERT SWIW 10-18-97
Reached Total Depth 1972-07-08 INJECTION PERMIT EXPIRED, WELL NOT CONVERTED CONVERT 1-30-99, CONVERT SWIW 10-18-97
CO 1992-12-09 3243 OHIO PRODUCTION CORP GeoDate 6/13/72
APP 1997-10-17 Proposed Formations:, Issued Date:10/17/97, Expired Date:10/17/98 6:00:00 AM, Drilling unit acres:72.6, Proposed Well Type:SWD, Proposed Well Class:O
Change of Owner 1998-04-16 Operator changed from 3243, OHIO PRODUCTION CORP to 6091, OHIO ENERGY ASSETS, INC.
APP 1999-01-29 Proposed Formations:CLINTON, MEDINA, Issued Date:1/29/99, Expired Date:1/29/00 6:00:00 AM, Drilling unit acres:72.6, Proposed Well Type:SWD, Proposed Well Class:SWIW
Last Compliance Report 1999-06-24 INJECTION PERMIT EXPIRED, WELL NOT CONVERTED CONVERT 1-30-99, CONVERT SWIW 10-18-97
Change of Owner 2014-04-03 Operator changed from 6091, OHIO ENERGY ASSETS, INC. to 6295, KNOX ENERGY INC.
APP 2014-11-17 Proposed Formations:CLINTON, Issued Date:11/17/2014, Expired Date:11/16/2016 12:00:00 PM, Drilling unit acres:72.6, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2016-08-16 INJECTION PERMIT EXPIRED, WELL NOT CONVERTED CONVERT 1-30-99, CONVERT SWIW 10-18-97
Construction Permit Expires 2016-11-16 INJECTION PERMIT EXPIRED, WELL NOT CONVERTED CONVERT 1-30-99, CONVERT SWIW 10-18-97
Record Last Modified 2018-04-17 INJECTION PERMIT EXPIRED, WELL NOT CONVERTED CONVERT 1-30-99, CONVERT SWIW 10-18-97

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2000-05-02 4586 4686 0
2006-09-11 4677 4686 0
4586 4686 0
4677 4686 0
4586 4686 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0
H2O 0 2025 Bbl 35000 CSG. PRESS 1250 PSI AFTER SWAB BACK
0 0 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2014 KNOX ENERGY INC. 0.00 0.00 0
2015 KNOX ENERGY INC. 0.00 0.00 0
2016 KNOX ENERGY INC. 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2014 KNOX ENERGY INC. Brine 0 0
2015 KNOX ENERGY INC. Brine 0 0
2016 KNOX ENERGY INC. Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-106572726 2019-8-13 0:00: FR No Violations 0.50
-1213800340 2016-1-13 0:00: PW No Violations 1.50
-1587795718 2018-11-2 0:00: FR No Violations 0.70
-225621501 2016-8-9 0:00:0 PW No Violations 2.00
-548166340 2016-8-11 0:00: PB No Violations 3.00
0171603168 2015-11-18 Production Wells No Violations Upon inspection, it was observed that this well is currently shut-in and is idle. The well is set up as a gas well only and consists of 4.5 production casing, 2 production tubing, and associated 2 steel flow lines. The well appears to be capable of production. The well location is very overgrown with brushy vegetation. There is no tank battery associated with the well. The lease road for the well is overgrown with vegetation and is essentially nonexistent. No ID information is posted at the well. I spoke with Bill Mitton of Knox Energy in order to ask how to get to the well. Mr. Mitton stated that Knox Energy plans to plug the well this winter. The entry to the well is through the AEP Area 11 hunting area off of TR. 940.
0225621501 2016-08-09 Production Wells No Violations Today I met with Donnie Strange at the site to make sure he was going to be rigging up on the proper well to plug. I found that the well he had found in the woods appears to be the correct one. He called me later and informed me they had rigged up and would be plugging tomorrow afternoon hopefully.
0548166340 2016-08-11 Plug / Plug Back No Violations I am onsite to witness the placement of the bottom plug at the request of inspector Sefcik. Berrys Well Service is providing the plugging services. The 2.375 EUE tubing was ran to a depth of 4511. Cemenco circulated a thirty sack class A plug with a 15.6 pound per gallon weight and a 1.18 cubic foot per sack yield. Circulation was established prior to placement of the plug. Fluid circulated to the annulus of the 4.5 casing as well.
1213800340 2016-01-13 Production Wells Violations Noted On my inspection today I found this well to be a 4 1/2 inch well head with 2 inch production lines. All of the valves for the production lines are closed off and the well has been idle for some time as production records are not up to date. Inspector Parkins did an inspection on this well on 11/18/2015 and spoke with Knox energy. He made them aware it was idle and they informed him they planned to plug it in the winter some time. The well was way back in the woods and Inspector Parkins marked off a good path with orange survey tape. The well owner/operator shall submit a written plugging schedule to the Brian Sefciks office at 5880 Memory road, Zanesville OH, 43701 within 30 days and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied. Brian Sefcik can be contacted via his cell phone at 740-255-2833.
1587795718 2018-11-02 Final Restoration No Violations I am on location today to do the final restoration on this well. The final restoration meets 1509.072(B) requirements.
171603168 2015-11-18 0:00 PW No Violations 2.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1213800340 US-OH-105610 2016-10-04 NONE Well shall be plugged

For data sources see[9]

References