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34-115-21277

Well Details

Well ID: 34-115-21277
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Country: United States
State: Ohio
County: Morgan
Municipality: Bristol Township
Operator Name: OHIO ENERGY ASSETS, INC.
Well Pad ID:
Farm/Lease Name: KALB ROBERT
License Status: Final Restoration
License Date: 2008-04-14
Spud Date: 1972-03-28
Spud Drilling Contractor: WORTHINGTON OIL
Final Drill Date: 1972-04-12
Well Total Depth: 4677.00 ft
Configuration: Vertical
Latitude: 39.680000
Longitude: -81.780000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1972-03-28
Completed 1972-04-12
Reached Total Depth 1972-04-12
CO 1972-09-22 199 WORTHINGTON OIL CO INC GeoDate 9/22/72
Oil and Gas 1972-09-22 Issued Date 9/22/72 Expired Date 9/22/73 Acres 0000000 Tool Type Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1992-12-09 3243 OHIO PRODUCTION CORP GeoDate 9/22/72
Change of Owner 1998-03-10 Operator changed from 3243, OHIO PRODUCTION CORP to 6091, OHIO ENERGY ASSETS, INC.
APP 2007-02-06 Proposed Formations:BEREA, Issued Date:2/6/2007, Expired Date:2/6/2008 6:00:00 AM, Drilling unit acres:78, Proposed Well Type:OG, Proposed Well Class:POOL
Plugged/Abandoned 2008-04-10
APP 2008-04-14 Proposed Formations:CLINTON, Issued Date:4/14/2008, Expired Date:4/14/2009 6:00:00 AM, Drilling unit acres:78, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 2009-04-14
Record Last Modified 2013-03-14

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1914 Bbl 35000 BROKE @ 900 PSI, AVG. RATE 42 BPM, AVG. PRESS. 1750 PSI, SHUT IN PRESS. 625 PSI, SHUT IN CSG. PRESS. 1500 PSI.
H2O 0 1914 Bbl 35000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1991 REDMAN OIL CO INC 355.00 0.00 31
1993 OHIO PRODUCTION CORP 1479.00 88.00 214
1994 OHIO PRODUCTION CORP 0.00 0.00 0
1995 OHIO PRODUCTION CORP 1512.00 152.00 146
1996 OHIO PRODUCTION CORP 146.00 0.00 29
1997 OHIO PRODUCTION CORP 339.00 0.00 58
1998 OHIO ENERGY ASSETS, INC. 0.00 59.00 35
1999 OHIO ENERGY ASSETS, INC. 0.00 0.00 0
2000 OHIO ENERGY ASSETS, INC. 0.00 0.00 0
2001 OHIO ENERGY ASSETS, INC. 0.00 0.00 0
2002 OHIO ENERGY ASSETS, INC. 0.00 0.00 0
2003 OHIO ENERGY ASSETS, INC. 0.00 0.00 0
2004 OHIO ENERGY ASSETS, INC. 0.00 0.00 0
2005 OHIO ENERGY ASSETS, INC. 0.00 0.00 0
2006 OHIO ENERGY ASSETS, INC. 0.00 0.00 0
2007 OHIO ENERGY ASSETS, INC. 0.00 0.00 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1991 REDMAN OIL CO INC Brine 463 31
1993 OHIO PRODUCTION CORP Brine 46 214
1994 OHIO PRODUCTION CORP Brine 0 0
1995 OHIO PRODUCTION CORP Brine 0 146
1996 OHIO PRODUCTION CORP Brine 0 29
1997 OHIO PRODUCTION CORP Brine 0 58
1998 OHIO ENERGY ASSETS, INC. Brine 0 35
1999 OHIO ENERGY ASSETS, INC. Brine 0 0
2000 OHIO ENERGY ASSETS, INC. Brine 0 0
2001 OHIO ENERGY ASSETS, INC. Brine 0 0
2002 OHIO ENERGY ASSETS, INC. Brine 0 0
2003 OHIO ENERGY ASSETS, INC. Brine 0 0
2004 OHIO ENERGY ASSETS, INC. Brine 0 0
2005 OHIO ENERGY ASSETS, INC. Brine 0 0
2006 OHIO ENERGY ASSETS, INC. Brine 0 0
2007 OHIO ENERGY ASSETS, INC. Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1544374614 2006-9-29 0:00: PW No Violations
-1649450756 2008-12-18 0:00 FR No Violations
-805281351 2008-4-3 0:00:0 PB No Violations
0805281351 2008-04-03 Plug / Plug Back No Violations Stopped by service rig for update on upcoming plug job, rig crew was pulling tubing to take off anchor joint in preparation for setting bottom hole plug also 2.875 in well set on packer there is a hole in 4.5 casing @4300 according to company records will log well and determine where packer is located and shot off 2.875 right above it.
1206393583 2008-03-24 Production Wells Violations Noted Upon inspecting well site found well to be idle all valves at wellhead were shut on the day of my inspection, tried to work with company on getting well placed into production they applied for permit to plug but permit has since expired well is leakinf trace amounts of oil within diked area around wellhead, well is equipped with 4.5 production casing and tubing possibly set on packer and 1-20 bbl plastic tank.
1207869162 2008-04-10 Production Wells Violations Noted Well has been plugged resolving previous Notice of Violation.
1544374614 2006-09-29 Production Wells No Violations Upon inspecting well site found small mess within dike area and no I.D. posted called and talked to Nancy Melville about concerns at well site she said her husband would be up over the weekend to resolve issues,told her if issues werent resolved then violations would be in order told her that Iwould check site for compliance 10/6/06.
1649450756 2008-12-18 Final Restoration No Violations Restoration work at site satisfactory,pit has been filled in and site restored and vegetation has been established.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1206393583 US-OH-105400 2008-03-24 Well insufficiently equipped to prevent escape of oil and gas
1206393583 US-OH-105401 2008-03-24 Failure to legibly identify well
1206393583 US-OH-105402 2008-03-24 Well shall be plugged
1207869162 US-OH-105433 2008-03-24 Well insufficiently equipped to prevent escape of oil and gas
1207869162 US-OH-105434 2008-03-24 Failure to legibly identify well
1207869162 US-OH-105435 2008-03-24 Well shall be plugged

For data sources see[8]

References