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34-111-65434

Well Details

Well ID: 34-111-65434
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Country: United States
State: Ohio
County: Monroe
Municipality: Wayne Township
Operator Name: BECK ENERGY CORPORATION
Well Pad ID:
Farm/Lease Name: CLINE
License Status: Final Restoration
License Date: 2010-11-30
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 39.680000
Longitude: -81.130000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Plugged/Abandoned 2010-11-23 NO RECORD.
APP 2010-11-30 Proposed Formations:, Issued Date:11/30/2010, Expired Date:11/29/2012 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 2012-11-29 NO RECORD.
Record Last Modified 2019-06-14 NO RECORD.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2011-01-05 250 254 15
250 254 15
250 254 15

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1993 MCM OIL 0.00 0.00 0
1994 MCM OIL 0.00 20.00 0
1995 MCM OIL 0.00 22.00 0
1996 MCM OIL 0.00 18.00 0
2001 WATTERS JOY & LEMON JANICE & T 0.00 0.00 365
2002 WATTERS JOY & LEMON JANICE & T 0.00 25.00 365
2003 WATTERS JOY & LEMON JANICE & T 0.00 21.00 365
2004 WATTERS JOY & LEMON JANICE & T 0.00 17.00 365
2005 WATTERS JOY & LEMON JANICE & T 0.00 19.00 365
2006 WATTERS JOY & LEMON JANICE & T 0.00 19.00 365
2008 WATTERS JOY & LEMON JANICE & T 0.00 15.00 365
2009 WATTERS JOY & LEMON JANICE & T 0.00 14.00 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1993 MCM OIL Brine 0 0
1994 MCM OIL Brine 0 0
1995 MCM OIL Brine 0 0
1996 MCM OIL Brine 0 0
2001 WATTERS JOY & LEMON JANICE & T Brine 0 365
2002 WATTERS JOY & LEMON JANICE & T Brine 0 365
2003 WATTERS JOY & LEMON JANICE & T Brine 0 365
2004 WATTERS JOY & LEMON JANICE & T Brine 0 365
2005 WATTERS JOY & LEMON JANICE & T Brine 0 365
2006 WATTERS JOY & LEMON JANICE & T Brine 0 365
2008 WATTERS JOY & LEMON JANICE & T Brine 0 365
2009 WATTERS JOY & LEMON JANICE & T Brine 0 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1408242942 2010-11-18 0:00 PB No Violations 8.50
-2080867617 2010-11-15 0:00 PB No Violations 2.00
1128632874 2010-11-05 Production Wells No Violations On day of inspection well has a pit to contain oil. This well was blown out by Beck energy frac job.Beck will plug well. Upon meeting with the landowners Tom and Janet Lemon they will get the necessary paperwork done and get bonded and registered. I delivered a packet to them. Kenny and Rosalie are Janet Lemons parents. They are deceased.
1289222552 2010-11-04 Production Wells No Violations Inspection found well over-flowing after frac with Beck on well #111-4261. Has communicated when fracting the Berea - dug pits, lined, to collect oil. After took pressure off new well, this well quit flowing. Checked other wells on the lease and saw no damage, called owner and informed him what had happened.
1290013445 2010-11-16 Plug / Plug Back No Violations On day of Formation was at well to set bottom hole plug with class A cement. We set a 500plug from 1754-1254.Will tag plug tomorrow with JT Wireline.
1290173876 2010-11-17 Plug / Plug Back No Violations On day of inspection JT Wireline came in to run bond log and found top of cement. Top of cement was at 1310.Ran bond log. Shot 15-3/8 holes into 6 1/4casing at 250.Will set plug from 1310-1110.Pull up and set plug 250 back to surface.
1290186406 2010-11-19 Plug / Plug Back No Violations On day of inspection showed up at well at 8:00am and Armstrong never showed up. Went made phone call told Armstrong he was to meet me there and tag plug. This was set up night before. He failed to show up. He stated he would call a water truck and pump water down casing to see if it would seal.JT Wireline will be set up for Tuesday at 11:00am -12:00pm.
1393344081 2014-02-25 Final Restoration No Violations Records show the well plugged and inspection of the well site shows the restoration meets 1509.072.
1408242942 2010-11-18 Plug / Plug Back No Violations On day of inspection formation cementing came in to cement well. Armstrong ran tubing in to the top of the cement at 1310.We set a plug from 1310-1110.Armstrong then pulled all 1.5tubing out and ran 8 jts back in to set the 250plug to surface thru the perfs.We ran a total of 30 sks reg class A cement @2%gel and no LCM on the 1st plug. The top plug we circulated cement back to surface but the well would drink the cement. We had circulation on backside and we ran cement in and would fill up casing and the cement would displace the lighter fluid out the backside. We put 174sks of cement on the top. We ran out of cement will come in at 8:00am and see where the top is.
1625928243 2010-11-23 Plug / Plug Back No Violations Well has been plugged.
2080867617 2010-11-15 Plug / Plug Back No Violations On day of inspection JT Wireline services were in make a run and record depth of well and bottom of 6 1/4casing.The td of well is 1774.Bottom of surface is at 1281.

For data sources see[8]

References