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34-111-24194

Well Details

Well ID: 34-111-24194
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Country: United States
State: Ohio
County: Monroe
Municipality: Center Township
Operator Name: BECK ENERGY CORPORATION
Well Pad ID:
Farm/Lease Name: TAYLOR
License Status: Producing
License Date: 2008-05-12
Spud Date: 2008-11-09
Spud Drilling Contractor: MONROE DRILLING OPERATION, LLC
Final Drill Date: 2008-11-12
Well Total Depth: 2730.00 ft
Configuration: Vertical
Latitude: 39.770000
Longitude: -81.070000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2008-05-12 Proposed Formations:BEREA/30 FOOT/GORDON, Issued Date:5/12/2008, Expired Date:5/12/2009 6:00:00 AM, Drilling unit acres:30, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2008-11-12
Completion Report Received 2008-12-26
Construction Permit Expires 2009-05-12
Record Last Modified 2015-09-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2009-04-27 2414 2448 39
2009-04-27 2114 2130 33
2114 2130 33
2414 2448 39
2536 2563 44
2656 2658 3
2114 2130 33
2009-04-27 2656 2658 3
2009-04-27 2536 2563 44

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 182000 Gal 50000 1ST STAGE OF FRAC ALSO INCLUDED THE GORDON & FIFTH SANDSTONES … NO TREATMENT OR RESERVOIR PRESSURES WERE REPORTED, AND ONLY A SINGLE SET OF FRAC VOLUMES WERE REPORTED

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2009 BECK ENERGY CORPORATION 1072.00 483.00 365
2010 BECK ENERGY CORPORATION 539.00 361.00 365
2011 BECK ENERGY CORPORATION 462.00 217.00 365
2012 BECK ENERGY CORPORATION 336.00 156.00 366
2013 BECK ENERGY CORPORATION 284.00 156.00 365
2014 BECK ENERGY CORPORATION 204.00 132.00 365
2015 BECK ENERGY CORPORATION 104.00 165.00 365
2016 BECK ENERGY CORPORATION 96.00 86.00 365
2017 BECK ENERGY CORPORATION 70.00 122.00 365
2018 BECK ENERGY CORPORATION 5.00 117.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2009 BECK ENERGY CORPORATION Brine 977 365
2010 BECK ENERGY CORPORATION Brine 683 365
2011 BECK ENERGY CORPORATION Brine 584 365
2012 BECK ENERGY CORPORATION Brine 546 366
2013 BECK ENERGY CORPORATION Brine 532 365
2014 BECK ENERGY CORPORATION Brine 393 365
2015 BECK ENERGY CORPORATION Brine 537 365
2016 BECK ENERGY CORPORATION Brine 371 365
2017 BECK ENERGY CORPORATION Brine 327 365
2018 BECK ENERGY CORPORATION Brine 395 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-800472646 2008-11-25 0:00 CT No Violations
0078906284 2008-11-21 Completion Testing No Violations RAN TUBING INTO WELL WITH ROB ARMSTRONGS RIG AND UNIVERSAL SHOWED UP TO DO AN ACID JOB.RAY WANTED TO PUMP ACID AND DISPLACE WITH WATER AND LET RUN ON GROUND. MADE THEM HOOK UP FLOW TEE AND RUN TREATING IRON TO 300BBL FRAC TANK.FRAC WILL BE MONDAY.
0502345021 2008-11-24 Completion Testing No Violations WENT TO FRAC JOB.FRAC THREE ZONES.GORDON,BEREA AND 30 FT SANDS.NEW OIL SAVER WAS LEAKING BUT WILL GET FIITTINGS.FRAC EQUIP.LEFT AT 4:15 PM.AT 5:00PM RAY,DUANE AND I WERE ON LOCATION.ROB COME BACK WE HOOKED UP FLOWLINE TO TANKS.BRIAN HOLLAND AND I WERE THERE FLOWING BACK INTO TANKS.WILL CHECK BACK IN MORNING.
0800472646 2008-11-25 Completion Testing No Violations WELL FLOWED BACK ABOUT 2 300BBL TANKSPER BRIAN HOLLAND.BECK SIMS CALLED LATER THAT DAY SAYING THAT A TOTAL OF 4 -300BBL TANKS WERE FILLED.SHE ALSO TOLD ME ABOUT RAY BECK DUMPING TANKS ON EARLY NO.2.SHE SAID THAT SHE TOLD RAY NOT TO BUT HE SAID EVERYTHING WOULD BE OK BECKY.PER RAY BECK.HE COMMENCED TO DUMP THEM .
1343834202 2012-08-01 Production Wells No Violations Inspection of the well head found the following equipment, 4.5 production casing, 1.5 tubing & pumping rods with the production valves open and the well being produced by the means of a pumping unit. At the production fluid storage area a single 100 barrel storage tank along with a mechanical separator and gas meter are present in an established dike with proper well identification.
1731297974 2010-01-28 Preliminary Restoration No Violations Well is supplied with a pumpjack ,7cas,4.5cas,1.5tubing.There is a 100bbl tank that has id and dike inplace.There is 90%vegetation established.
502345021 2008-11-24 0:00 CT No Violations
78906284 2008-11-21 0:00 CT No Violations

For data sources see[9]

References