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34-111-24181

Well Details

Well ID: 34-111-24181
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Country: United States
State: Ohio
County: Monroe
Municipality: Malaga Township
Operator Name: BECK ENERGY CORPORATION
Well Pad ID:
Farm/Lease Name: BLOCK
License Status: Producing
License Date: 2008-02-15
Spud Date: 2008-04-28
Spud Drilling Contractor: R WOLFE DRLG
Final Drill Date: 2008-04-29
Well Total Depth: 2640.00 ft
Configuration: Vertical
Latitude: 39.820000
Longitude: -81.150000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2008-02-15 Proposed Formations:BEREA/30 FOOT/GORDON, Issued Date:2/15/2008, Expired Date:2/14/2009 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL
Reached Total Depth 2008-04-29
Completion Report Received 2008-10-10
Construction Permit Expires 2009-02-14
Record Last Modified 2015-09-24

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2008-11-24 2050 2060 25
2008-11-24 2314 2360 33
2050 2060 25
2314 2360 33
2422 2466 22
2050 2060 25
2008-11-24 2422 2466 22

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 221000 Gal 0 3 STAGE FRAC

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2008 BECK ENERGY CORPORATION 374.00 0.00 0
2009 BECK ENERGY CORPORATION 1745.00 364.00 365
2010 BECK ENERGY CORPORATION 2362.00 350.00 365
2011 BECK ENERGY CORPORATION 1086.00 220.00 365
2012 BECK ENERGY CORPORATION 1066.00 139.00 366
2013 BECK ENERGY CORPORATION 1889.00 308.00 365
2014 BECK ENERGY CORPORATION 1545.00 116.00 365
2015 BECK ENERGY CORPORATION 1194.00 130.00 365
2016 BECK ENERGY CORPORATION 1099.00 128.00 365
2017 BECK ENERGY CORPORATION 999.00 63.00 365
2018 BECK ENERGY CORPORATION 786.00 74.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2008 BECK ENERGY CORPORATION Brine 0
2009 BECK ENERGY CORPORATION Brine 47 365
2010 BECK ENERGY CORPORATION Brine 144 365
2011 BECK ENERGY CORPORATION Brine 18 365
2012 BECK ENERGY CORPORATION Brine 21 366
2013 BECK ENERGY CORPORATION Brine 199 365
2014 BECK ENERGY CORPORATION Brine 59 365
2015 BECK ENERGY CORPORATION Brine 36 365
2016 BECK ENERGY CORPORATION Brine 33 365
2017 BECK ENERGY CORPORATION Brine 22 365
2018 BECK ENERGY CORPORATION Brine 12 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1211460903 2008-05-08 Production Wells Violations Noted THE DAY OF 05-08-08 IDROVE IN TO SEE THE STATUS ON THE SERVICE RIG.ROB ARMSTRONG WAS OPERATING THE RIG AND WAS SWABBING ON THE OPEN GROUND.THE FLUID WAS BLOWING OUT OF THE OILSAVER AND THE 2VALVE ON THE 7WELLHEAD DURING THE RETRACTION OF THE SAND LINE.HE THEN SHUT DOWN THE RIG AND CAME TO THE JEEP AND I ASK WHERE THE FLUID WAS GOING.ROB SAID INTO THE PIT.THEY LEFT AND WENT TO LUNCH AND I WENT TO LOOK AT THE INCIDENT.THEY WERE SWABBING ONTO THE OPEN GROUND.THE FLUID WENT DOWN THE HILL AND INTO A CREEK.PICTURS AND A WATER SAMPLE WERE TAKEN.
1245433005 2009-05-21 Production Wells No Violations DAY OF INSPECTION WELL IS A RABBET WELL WITH 7CAS,4.5CAS,1.5TUBING.WELL IS SUPPLIED WITH A 100BBL TANK AND DIKE AND ID IS SUFFICIENT.SITE NEEDS TO BE SCRATCHED UP AND RESEEDED.CALLED BECKY SIMS.MATT LOGWELL WILL MOVE IN TAKE CARE OF SITE.
1251136328 2009-08-24 Preliminary Restoration No Violations WELL IS A RABBIT WELL SUPPLIED WITH 7CAS,4.5CAS,1.5TUBING.100BBL TANK WITH ID AND DIKE IN PLACE.WELL IS COMPLIANT.
1428509062 2015-04-08 Production Wells No Violations Status check production well inspection found the following equipment present at the well head-4.5 production casing -1.5tubing and rods with the production valves in the open position and the well set up to be produced by the means of a pumping unit. At the production fluid storage area a single 100 barrel production tank is present along with a mechanical separator and gas sales meter, proper well identification is posted. No violations noted on the day of my inspection.
2016754140 2008-05-16 Production Wells Violations Noted ON 05-16-2008 AT 8:30 AM I WAS STOPPING TO SEE IF THE DRILL PIT WAS CLOSED UP.I WENT DOWN TO WELL AND LOOKED AT PIT.THE BACKSIDE WALL GAVE AWAY.CAUSING THE CONTENTS TOSPILL DOWN INTO WOODS AND DOWN TO A CREEK.ALL OF THE FRAC TANKS WERE STILL PRESENT.SHALLOW SPRINGS WERE CHARGING UP THE SITUATION.I CALLED RAY BECK ON THE MATTER.HE DIRECTLY HAD SOME OF HIS EMPLOYEES SHOW UP AT ABOUT 9:30 AM.WE TOOK A DOZER AND CLOSED OFF THE OPEN PART OF THE PIT.WE THEN STARTED DIKING UP THE LOWER PART OF THE SPILL SO FLUID WOULD NOT GO DOWN INTO CREEK.WE TOOK OIL ABSORBENTS AND WENT TO DIKE UP THE LITTLE FEEDERS FROM THE SPRINGS CARRYING SHEEN FROM THE APPARENT SPILL.AT 11:00AM STARTED TO HOOK A PUMP UP TO THE FLOW LINE AND PUMP INTO THE 100BBL TANK AT TANK PAD.AT 1:30PM WE STARTED MOVING 2 300 BBL FRAC TANKS DOWN BY THE TANKPAD.AT 2:30 PM WATER TRUCKS WERE CALLED.AT 3:00 PM THE HAULERS CALLED BACK AND SAID THEY WOULD HAVE TO WAIT TILL SATURDAY MORNING.ALL DISPOSAL WELLS WERE FULL AND ONE WAS DOWN.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1211460903 US-OH-105535 2008-05-22 Well operation causing pollution and contamination
2016754140 US-OH-120485 2008-05-22 Well operation causing pollution and contamination
2016754140 US-OH-120486 2008-05-22 Dike or pit not able to prevent escape of brine or other wastes

For data sources see[9]

References