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34-111-23803

Well Details

Well ID: 34-111-23803
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Country: United States
State: Ohio
County: Monroe
Municipality: Benton Township
Operator Name: BECK ENERGY CORPORATION
Well Pad ID:
Farm/Lease Name: HENSEL WALTER
License Status: Producing
License Date: 2002-06-05
Spud Date: 2002-07-11
Spud Drilling Contractor: R WOLFE DRLG
Final Drill Date: 2002-07-16
Well Total Depth: 2850.00 ft
Configuration: Vertical
Latitude: 39.580000
Longitude: -81.050000

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2002-06-05 Proposed Formations:BEREA/30 FOOT/GORDON, Issued Date:6/5/2002, Expired Date:6/5/2003 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL
Original Spud 2002-07-11 RBDMS Rec
Completed 2002-07-16 RBDMS Rec
Reached Total Depth 2002-07-16 RBDMS Rec
Completion Report Received 2002-09-17 RBDMS Rec
Construction Permit Expires 2003-06-05 RBDMS Rec
Record Last Modified 2015-09-24 RBDMS Rec

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2002-10-25 2174 2177 4
2002-10-25 1301 1309 17
1301 1309 17
2174 2177 4
2233 2237 17
2408 2494 25
2640 2683 28
1301 1309 17
2002-10-25 2233 2237 17
2002-10-25 2640 2683 28
2002-10-25 2408 2494 25

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 139000 Gal 0 3 STAGE FRAC

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2002 BECK ENERGY CORPORATION 4154.00 129.00 0
2003 BECK ENERGY CORPORATION 5234.00 188.00 365
2004 BECK ENERGY CORPORATION 3249.00 40.00 365
2005 BECK ENERGY CORPORATION 3189.00 0.00 365
2006 BECK ENERGY CORPORATION 1535.00 80.00 365
2007 BECK ENERGY CORPORATION 1480.00 0.00 365
2008 BECK ENERGY CORPORATION 1253.00 29.00 365
2009 BECK ENERGY CORPORATION 3078.00 0.00 365
2010 BECK ENERGY CORPORATION 7088.00 0.00 365
2011 BECK ENERGY CORPORATION 4089.00 0.00 365
2012 BECK ENERGY CORPORATION 2153.00 0.00 366
2013 BECK ENERGY CORPORATION 1660.00 48.00 365
2014 BECK ENERGY CORPORATION 740.00 0.00 365
2015 BECK ENERGY CORPORATION 636.00 0.00 365
2016 BECK ENERGY CORPORATION 549.00 20.00 365
2017 BECK ENERGY CORPORATION 509.00 0.00 365
2018 BECK ENERGY CORPORATION 518.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2002 BECK ENERGY CORPORATION Brine 630
2003 BECK ENERGY CORPORATION Brine 0 365
2004 BECK ENERGY CORPORATION Brine 0 365
2005 BECK ENERGY CORPORATION Brine 25 365
2006 BECK ENERGY CORPORATION Brine 0 365
2007 BECK ENERGY CORPORATION Brine 0 365
2008 BECK ENERGY CORPORATION Brine 0 365
2009 BECK ENERGY CORPORATION Brine 0 365
2010 BECK ENERGY CORPORATION Brine 0 365
2011 BECK ENERGY CORPORATION Brine 0 365
2012 BECK ENERGY CORPORATION Brine 0 366
2013 BECK ENERGY CORPORATION Brine 13 365
2014 BECK ENERGY CORPORATION Brine 0 365
2015 BECK ENERGY CORPORATION Brine 0 365
2016 BECK ENERGY CORPORATION Brine 53 365
2017 BECK ENERGY CORPORATION Brine 0 365
2018 BECK ENERGY CORPORATION Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1005962693 2018-8-1 0:00:0 PW No Violations 1.00
-320590498 2020-5-21 0:00: PW No Violations 0.50
0360989451 2018-08-09 Production Wells No Violations On this day, I am conducting a compliance notice follow-up inspection pertaining to the high chloride content around the wellhead. I found that the issue has been addressed and the well is now within compliance.
1005962693 2018-08-01 Production Wells Violations Noted On this day, I found the well equipped with a 7-inch diameter surface casing head, 4.5-inch diameter production casing, and 1.9-inch diameter tubing. It is produced by means of a pumping unit with rods, and a gas engine. The production facility is shared with permit number 2-3821 and consists of (2) 100-barrel steel tanks within an earthen dike, (2) vertical separators, (2) drip tanks, and (2) orifice sales meters with current charts. It will be noted that there is contamination within the immediate vicinity of the wellhead (approximately 4 feet in diameter) consisting of stressed vegetation that was tested with a High Range Quantab resulting in 2,400+ parts per million chlorides. Pictures were taken during the inspection. The affected area shall be remediated, and new vegetation established. I spoke with Becky Simms on 08/03/2018 at 8:45am to inform her of the issue.
1617646005 2004-11-04 Preliminary Restoration No Violations Restoration satisfactory.
360989451 2018-8-9 0:00:0 PW No Violations 0.30

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1005962693 US-OH-100051 2018-09-11 Well operation causing pollution and contamination

For data sources see[9]

References