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34-103-24488

Well Details

Well ID: 34-103-24488
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Country: United States
State: Ohio
County: Medina
Municipality: Medina Township
Operator Name: KAMINSKY MIKE P
Well Pad ID:
Farm/Lease Name: STARNER
License Status: Domestic Well
License Date: 1989-08-28
Spud Date: 1990-01-11
Spud Drilling Contractor: [[P&R INC [PEEK & ROWAN]]]
Final Drill Date: 1990-01-15
Well Total Depth: 3495.00 ft
Configuration: Vertical
Latitude: 41.170000
Longitude: -81.790000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1989-04-26 198 VIKING RESOURCES CORP GeoDate 4/26/89
Oil and Gas 1989-04-26 Issued Date 4/26/89 Expired Date 4/26/90 Acres 0020000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
CO 1989-08-28 198 VIKING RESOURCES CORP GeoDate 8/28/89
Oil and Gas 1989-08-28 Issued Date 4/26/89 Expired Date 4/26/90 Acres 0082110 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 03495 Proposed Drill Depth 03495
Original Spud 1990-01-11 RL 9-2-89
Completed 1990-01-15 RL 9-2-89
Reached Total Depth 1990-01-15 RL 9-2-89
Completion Report Received 1990-04-25 RL 9-2-89
Construction Permit Expires 1990-04-26 RL 9-2-89
Change of Owner 2007-10-22 Operator changed from 198, VIKING RESOURCES LLC to 8291, KAMINSKY MIKE P
Record Last Modified 2017-02-15 RL 9-2-89

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 3300 3386 0
3300 3386 0
2006-09-11 3328 3350 22
3328 3350 22
3300 3386 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 FRAC:WATER/SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1989 VIKING RESOURCES LLC 0.00 180.00 89
1990 VIKING RESOURCES LLC 7383.00 686.00 238
1992 VIKING RESOURCES LLC 3637.00 495.00 302
1993 VIKING RESOURCES LLC 2488.00 181.00 365
1994 VIKING RESOURCES LLC 2673.00 290.00 365
1995 VIKING RESOURCES LLC 2410.00 193.00 0
1996 VIKING RESOURCES LLC 1773.00 125.00 0
1997 VIKING RESOURCES LLC 1731.00 191.00 0
1998 VIKING RESOURCES LLC 1533.00 98.00 365
2000 RESOURCE AMERICA INC 1171.00 0.00 365
2001 VIKING RESOURCES LLC 655.00 0.00 365
2002 VIKING RESOURCES LLC 297.00 86.00 365
2003 VIKING RESOURCES LLC 8.00 0.00 365
2004 VIKING RESOURCES LLC 0.00 0.00 365
2005 VIKING RESOURCES LLC 215.00 0.00 365
2006 VIKING RESOURCES LLC 326.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1989 VIKING RESOURCES LLC Brine 155 89
1990 VIKING RESOURCES LLC Brine 20 238
1992 VIKING RESOURCES LLC Brine 98 302
1993 VIKING RESOURCES LLC Brine 38 365
1994 VIKING RESOURCES LLC Brine 38 365
1995 VIKING RESOURCES LLC Brine 0 0
1996 VIKING RESOURCES LLC Brine 0 0
1997 VIKING RESOURCES LLC Brine 30 0
1998 VIKING RESOURCES LLC Brine 40 365
2000 RESOURCE AMERICA INC Brine 0 365
2001 VIKING RESOURCES LLC Brine 0 365
2002 VIKING RESOURCES LLC Brine 0 365
2003 VIKING RESOURCES LLC Brine 0 365
2004 VIKING RESOURCES LLC Brine 0 365
2005 VIKING RESOURCES LLC Brine 0 365
2006 VIKING RESOURCES LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1307809763 2006-3-7 0:00:0 PW No Violations 0.50
-216283182 2007-10-2 0:00: PW No Violations 1.00
-378708997 2008-1-7 0:00:0 PW No Violations 1.00
-745858972 2007-8-8 0:00:0 PW No Violations 2.00
000PL11299 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0216283182 2007-10-02 Production Wells No Violations Called by Terry Whitehair to advise company and landowner, Mike Kamisky, has reached an agreement on price for wells. Mike Kamisky is purchasing wells and 210 barrel tank will be removed. Sun, 70 degrees.
0378708997 2008-01-07 Production Wells No Violations Well was sold to landowner Mike Kaminsky. 210 barrel tank was removed. Well is in production. Cloudy, 60 degrees.
0745858972 2007-08-08 Production Wells Violations Noted Called by landowner Mike Kaminsky. Atlas America is not working with landowner on well problems. 210 barrel tank has holes rusted through at top and oil is leaking from holes. Threads on separator is leaking oil. No production has been reported since 2005. Gas line on south end of well leading in woods is washed out and line has been taped. Repair gas line and bury before line breaks. Belt guard on pump jack needs installed. Bull plug all open valves on separator.
1307809763 2006-03-07 Production Wells No Violations Well in production equipped with pump jack, rods and tubing. 2-210 barrel tanks and separator with concrete vault in battery. Sun, 30 degrees.
PL11299 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0745858972 US-OH-128472 2007-08-09 Failure to properly bury pipeline
0745858972 US-OH-128473 2007-08-09 General Safety
0745858972 US-OH-128474 2007-08-09 Well shall be plugged

For data sources see[9]

References