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34-099-21305

Well Details

Well ID: 34-099-21305
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Country: United States
State: Ohio
County: Mahoning
Municipality: Smith Township
Operator Name: DART OIL COMPANY
Well Pad ID:
Farm/Lease Name: CATTELL UNIT
License Status: Producing
License Date: 1980-10-29
Spud Date:
Spud Drilling Contractor:
Final Drill Date: 1980-11-24
Well Total Depth: 0.00 ft
Configuration: Vertical
Latitude: 40.920000
Longitude: -80.990000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1980-10-29 470 DART OIL CO GeoDate 10/29/80
Oil and Gas 1980-10-29 Issued Date 10/29/80 Expired Date Acres 0041000 Tool Type RTF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000
Completed 1980-11-24 PERMIT EXPIRED
Reached Total Depth 1980-11-24 PERMIT EXPIRED
Completion Report Received 1981-01-14 PERMIT EXPIRED
Record Last Modified 2014-01-08 PERMIT EXPIRED

For data sources see[2]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 DART OIL COMPANY 1770.00 940.00 0
1985 DART OIL COMPANY 1699.00 809.00 0
1986 DART OIL COMPANY 1377.00 544.00 363
1987 DART OIL COMPANY 1216.00 627.00 214
1988 DART OIL COMPANY 997.00 449.00 256
1989 DART OIL COMPANY 675.00 301.00 204
1990 DART OIL COMPANY 746.00 493.00 256
1991 DART OIL COMPANY 7977.00 2291.00 237
1992 DART OIL COMPANY 9104.00 1911.00 227
1993 DART OIL COMPANY 7636.00 1761.00 218
1994 DART OIL COMPANY 6501.00 1449.00 155
1995 DART OIL COMPANY 6025.00 1487.00 194
1996 DART OIL COMPANY 5226.00 1164.00 157
1997 DART OIL COMPANY 3396.00 1266.00 160
1998 DART OIL COMPANY 2716.00 939.00 137
1999 DART OIL COMPANY 3167.00 1119.00 114
2000 DART OIL COMPANY 3352.00 1056.00 163
2001 DART OIL COMPANY 3607.00 897.00 110
2002 DART OIL COMPANY 4254.00 863.00 115
2003 DART OIL COMPANY 4116.00 845.00 98
2004 DART OIL COMPANY 3869.00 888.00 112
2005 DART OIL COMPANY 3644.00 6453.00 116
2006 DART OIL & GAS CORP 3257.00 804.00 113
2007 DART OIL COMPANY 2859.00 574.00 75
2008 DART OIL & GAS CORP 119.00 0.00 60
2009 DART OIL & GAS CORP 0.00 0.00 0
2011 DART OIL COMPANY 0.00 0.00 0
2012 DART OIL COMPANY 0.00 124.00 38
2013 DART OIL COMPANY 448.00 270.00 346
2014 DART OIL COMPANY 0.00 217.00 365
2015 DART OIL COMPANY 0.00 212.00 307
2016 DART OIL COMPANY 0.00 195.00 307
2017 DART OIL COMPANY 0.00 288.00 307
2018 DART OIL COMPANY 0.00 182.00 335

For data sources see[3] [4]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 DART OIL COMPANY Brine 0 0
1985 DART OIL COMPANY Brine 80 0
1986 DART OIL COMPANY Brine 53 363
1987 DART OIL COMPANY Brine 19 214
1988 DART OIL COMPANY Brine 32 256
1989 DART OIL COMPANY Brine 0 204
1990 DART OIL COMPANY Brine 74 256
1991 DART OIL COMPANY Brine 165 237
1992 DART OIL COMPANY Brine 145 227
1993 DART OIL COMPANY Brine 163 218
1994 DART OIL COMPANY Brine 116 155
1995 DART OIL COMPANY Brine 131 194
1996 DART OIL COMPANY Brine 132 157
1997 DART OIL COMPANY Brine 215 160
1998 DART OIL COMPANY Brine 210 137
1999 DART OIL COMPANY Brine 119 114
2000 DART OIL COMPANY Brine 209 163
2001 DART OIL COMPANY Brine 78 110
2002 DART OIL COMPANY Brine 78 115
2003 DART OIL COMPANY Brine 53 98
2004 DART OIL COMPANY Brine 94 112
2005 DART OIL COMPANY Brine 76 116
2006 DART OIL & GAS CORP Brine 115 113
2007 DART OIL COMPANY Brine 126 75
2008 DART OIL & GAS CORP Brine 0 60
2009 DART OIL & GAS CORP Brine 0 0
2011 DART OIL COMPANY Brine 0 0
2012 DART OIL COMPANY Brine 82 38
2013 DART OIL COMPANY Brine 88 346
2014 DART OIL COMPANY Brine 59 365
2015 DART OIL COMPANY Brine 43 307
2016 DART OIL COMPANY Brine 110 307
2017 DART OIL COMPANY Brine 35 307
2018 DART OIL COMPANY Brine 0 335

For data sources see[5] [6]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1243919773 2012-3-13 0:00: PW No Violations
-147680523 2012-12-6 0:00: PW No Violations 1.00
-93452657 2012-3-13 0:00: PW No Violations
0093452657 2012-03-13 Production Wells Violations Noted I received a call from Phil Sharp (330-938-0441) on the evening of March 12, 2012 requesting an inspection of a well on his property that he reported as being incapable of production. On the day of my inspection I conducted a status check at the site and found that the well was equipped with a pumping unit and there was evidence of the well being recently serviced. The soil was disturbed around the well head and excavating equipment remained at the site. The well head was bubbling gas in two places and there were pools of oil/brine contamination around the casing. The tank battery consisted of one 210 barrel stock tank, one 100 barrel brine storage tank, one separator and a dike. Proper identification was posted on the tank battery and the dike was overgrown with weedy vegetation. The chart was dated 07-16-2009, and the ODNR database revealed that no record of production has been filed since 2009. I tried to reach Dart Oil (303-355-8341) by phone on March 15, 2012, with no success.
0147680523 2012-12-06 Production Wells No Violations I performed a fellow up inspection on the above location the tank battery consist of 1-210 barrel tank, 1- 100 barrel tank and a horizontal separator. The dike has been rebuilt and is in compliance. The well is equipped with a pumping unit and a electric motor. All violation have been cleared at this time
1243919773 2012-03-13 Production Wells No Violations FOLLOW UP TO NOV # -93452657 I received a call from Phil Sharp (330-938-0441) on the evening of March 12, 2012 requesting an inspection of a well on his property that he reported as being incapable of production. On the day of my inspection I conducted a status check at the site and found that the well was equipped with a pumping unit and there was evidence of the well being recently serviced. The soil was disturbed around the well head and excavating equipment remained at the site. The well head was bubbling gas in two places and there were pools of oil/brine contamination around the casing. The tank battery consisted of one 210 barrel stock tank, one 100 barrel brine storage tank, one separator and a dike. Proper identification was posted on the tank battery and the dike was overgrown with weedy vegetation. The chart was dated 07-16-2009, and the ODNR database revealed that no record of production has been filed since 2009. I tried to reach Dart Oil (303-355-8341) by phone on March 15, 2012, with no success.
1335378255 2012-04-19 Production Wells Violations Noted I received a call from on 3/29/2012 from Bob Timmerman (330-779-9801) of Dart Oil ensuring me that they are working to get this well in production. We discussed the violations and the actions that need to be taken to bring this well into compliance. On the day of my inspection I found that the soil had been graded and a dike had been constructed around the pumping unit. A new electric box had also been installed. The pumping unit showed no signs of actually pumping and the well head was still leaking. The tank battery was still overgrown with weeds and a new chart had been installed, which showed no recorded production. This NOV continues.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0093452657 US-OH-130685 2012-03-15 Nonproduction; well shall be plugged or placed in temporary inactive status
0093452657 US-OH-130686 2012-03-15 Defective casing, leaking well
0093452657 US-OH-130687 2012-03-15 Statement of annual production not filed
1335378255 US-OH-109654 2012-04-25 Nonproduction; well shall be plugged or placed in temporary inactive status
1335378255 US-OH-109655 2012-04-25 Defective casing, leaking well
1335378255 US-OH-109656 2012-04-25 Statement of annual production not filed

For data sources see[7]

References