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34-099-20881

Well Details

Well ID: 34-099-20881
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Country: United States
State: Ohio
County: Mahoning
Municipality: Ellsworth Township
Operator Name: CUBICK KAREL L
Well Pad ID:
Farm/Lease Name: HENDRICKS
License Status: Domestic Well
License Date: 1976-12-29
Spud Date: 1977-04-11
Spud Drilling Contractor: PERKINS DRLG
Final Drill Date: 1977-04-18
Well Total Depth: 5380.00 ft
Configuration: Vertical
Latitude: 40.990000
Longitude: -80.840000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1976-12-29 504 UNITED PETROLEUM CORP GeoDate 12/29/76
Original Spud 1977-04-11 WELL DRILLED & COMPLETED..NO PRODUCTION DATA REPORTED. CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM D & L ENERGY INC. #2651 TO OWNER ON 11/30/2015 CM.
Completed 1977-04-18 WELL DRILLED & COMPLETED..NO PRODUCTION DATA REPORTED. CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM D & L ENERGY INC. #2651 TO OWNER ON 11/30/2015 CM.
Reached Total Depth 1977-04-18 WELL DRILLED & COMPLETED..NO PRODUCTION DATA REPORTED. CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM D & L ENERGY INC. #2651 TO OWNER ON 11/30/2015 CM.
Completion Report Received 1977-11-17 WELL DRILLED & COMPLETED..NO PRODUCTION DATA REPORTED. CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM D & L ENERGY INC. #2651 TO OWNER ON 11/30/2015 CM.
Construction Permit Expires 1977-12-29 WELL DRILLED & COMPLETED..NO PRODUCTION DATA REPORTED. CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM D & L ENERGY INC. #2651 TO OWNER ON 11/30/2015 CM.
Change of Owner 2003-01-13 Operator changed from 504, UNITED PETROLEUM CORP to 2651, D & L ENERGY INC
Change of Owner 2015-11-30 Operator changed from 2651, D & L ENERGY INC to 9591, CUBICK KAREL L
Record Last Modified 2017-02-15 WELL DRILLED & COMPLETED..NO PRODUCTION DATA REPORTED. CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM D & L ENERGY INC. #2651 TO OWNER ON 11/30/2015 CM.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2002-09-25 5210 5253 18
5210 5253 18
5210 5253 18

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 46000 Gal 50000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2011 D & L ENERGY INC 0.00 0.00 0
2014 D & L ENERGY INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2011 D & L ENERGY INC Brine 0
2014 D & L ENERGY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0907849435 2015-10-27 Exempt Well Pre Transfer No Violations I was on site with DOGRM inspector - John Fleming to conduct an inspection of this well. The wellhead consisted of the 8 and 5/8 inch casing with a 4.5 inch casing with a gate valve plumbed into a Swage, then into a two inch line with a regulator and drip bottle. The well is being used for domestic use only and is approximately 1450 feet from a dwelling. The production equipment has been removed from the site. The wellhead location was stable. The access was stable and driveable. I contacted the landowner with regards to adding signage to the wellhead. The domestic transfer may proceed.
1426877494 2015-03-19 Production Wells No Violations I performed a status check on the above location. The well is equipped with 4.5 casing . This well is equipped with a domestic homeowner hook-up. No records of production.
907849435 2015-10-27 0:00 EX No Violations

For data sources see[9]

References