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34-099-20745

Well Details

Well ID: 34-099-20745
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Country: United States
State: Ohio
County: Mahoning
Municipality: Ellsworth Township
Operator Name: GRISWOLD RONALD D
Well Pad ID:
Farm/Lease Name: STEEL PLANT MAINTENANCE INC
License Status: Domestic Well
License Date: 1976-08-23
Spud Date: 1976-12-10
Spud Drilling Contractor: PERKINS DRLG
Final Drill Date: 1976-12-15
Well Total Depth: 5259.00 ft
Configuration: Vertical
Latitude: 41.040000
Longitude: -80.890000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1976-08-23 504 UNITED PETROLEUM CORP GeoDate 8/23/76
Original Spud 1976-12-10 CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM D & L ENERGY INC. #2651 TO OWNER ON 11/30/2015 CM.
Completed 1976-12-15 CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM D & L ENERGY INC. #2651 TO OWNER ON 11/30/2015 CM.
Reached Total Depth 1976-12-15 CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM D & L ENERGY INC. #2651 TO OWNER ON 11/30/2015 CM.
Construction Permit Expires 1977-08-23 CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM D & L ENERGY INC. #2651 TO OWNER ON 11/30/2015 CM.
Completion Report Received 1978-03-20 CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM D & L ENERGY INC. #2651 TO OWNER ON 11/30/2015 CM.
Change of Owner 2003-01-13 Operator changed from 504, UNITED PETROLEUM CORP to 2651, D & L ENERGY INC
Change of Owner 2015-11-30 Operator changed from 2651, D & L ENERGY INC to 9590, GRISWOLD RONALD D
Record Last Modified 2017-02-15 CHANGED STATUS OF WELL FROM PR TO DM PER TRANSFER FROM D & L ENERGY INC. #2651 TO OWNER ON 11/30/2015 CM.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5092 5134 0
5092 5134 0
5092 5134 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 24000 Gal 50000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2011 D & L ENERGY INC 0.00 0.00 0
2014 D & L ENERGY INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2011 D & L ENERGY INC Brine 0
2014 D & L ENERGY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1385331842 2015-10-27 Exempt Well Pre Transfer No Violations I was on site with DOGRM inspector - John Fleming to inspect this well. The wellhead consisted of the 8 and 5/8 inch casing with the 4.5 inch casing plumbed into a Swage then into a two inch line with three regulators and a drip bottle. The pressure gauge on the well read 1000 psi. The well is being used for domestic use only and is approximately 800 feet from the nearest dwelling. The production equipment has been removed. The wellhead and tank battery locations were stable. The lease access was stable and driveable. I was not able to speak with the landowner at the time of this inspection. The landowner will be contacted regarding the signage that still needs added to the well. The domestic transfer may proceed.
1427204078 2015-03-11 Production Wells Violations Noted I was on location for a status check. During my inspection, I found the well not in production. The wells 4.5 inch casing had been reduced using a 4.5 inch by 2 inch swage, then further reduced to a 1 inch domestic gas line with a 3 inch drip tank. The main ball valve on the 4.5 inch casing was in the open position. There is an oil residue all over the 4.5 inch and 8.625 inch casings. There is no identification posted. There is no production equipment associated with the well. The lease road is in stable condition. The only annual production filed by D & L was zero in 2011. The leak causing the oil residue needs repaired and cleaned. Photos were taken and are available upon request.
1467221373 2016-03-11 Plug / Plug Back No Violations I was on location with DOGRM Inspector Shannon Mullins, to inspect this well for Exempt Well Pre Transfer. At the time of our inspection. There was no environmental issues at that time. There was a Compliance Notice Issued (1427204078) on 3/11/2015. The Compliance Notice can be closed at this time. The well was transfer to the landowner.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1427204078 US-OH-112458 2015-05-04 Well insufficiently equipped to prevent escape of oil and gas
1427204078 US-OH-112459 2015-05-04 Failure to legibly identify well

For data sources see[9]

References