X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-099-20735

Well Details

Well ID: 34-099-20735
Loading map...
Country: United States
State: Ohio
County: Mahoning
Municipality: Ellsworth Township
Operator Name: D & L ENERGY INC
Well Pad ID:
Farm/Lease Name: RENOUF
License Status: Final Restoration
License Date: 2016-01-08
Spud Date: 1976-09-21
Spud Drilling Contractor: PERKINS DRLG
Final Drill Date: 1976-09-28
Well Total Depth: 5354.00 ft
Configuration: Vertical
Latitude: 41.010000
Longitude: -80.890000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1976-08-20 504 UNITED PETROLEUM CORP GeoDate 8/20/76
Original Spud 1976-09-21 DRILLED & COMPLETED..NO PRODUCTION DATA REPORTED. CHANGED STATUS FROM PA TO FR PER FACILITY REPORT DATED 5/16/2017 FROM JOHN FLEMING F_REST_PASS ON 5/17/2017 CM.
Completed 1976-09-28 DRILLED & COMPLETED..NO PRODUCTION DATA REPORTED. CHANGED STATUS FROM PA TO FR PER FACILITY REPORT DATED 5/16/2017 FROM JOHN FLEMING F_REST_PASS ON 5/17/2017 CM.
Reached Total Depth 1976-09-28 DRILLED & COMPLETED..NO PRODUCTION DATA REPORTED. CHANGED STATUS FROM PA TO FR PER FACILITY REPORT DATED 5/16/2017 FROM JOHN FLEMING F_REST_PASS ON 5/17/2017 CM.
Completion Report Received 1977-02-17 DRILLED & COMPLETED..NO PRODUCTION DATA REPORTED. CHANGED STATUS FROM PA TO FR PER FACILITY REPORT DATED 5/16/2017 FROM JOHN FLEMING F_REST_PASS ON 5/17/2017 CM.
Change of Owner 2003-01-13 Operator changed from 504, UNITED PETROLEUM CORP to 2651, D & L ENERGY INC
APP 2016-01-08 Proposed Formations:QUEENSTON, Issued Date:1/8/2016, Expired Date:1/7/2018 12:00:00 PM, Drilling unit acres:113, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2016-03-21 DRILLED & COMPLETED..NO PRODUCTION DATA REPORTED. CHANGED STATUS FROM PA TO FR PER FACILITY REPORT DATED 5/16/2017 FROM JOHN FLEMING F_REST_PASS ON 5/17/2017 CM.
Record Last Modified 2017-05-17 DRILLED & COMPLETED..NO PRODUCTION DATA REPORTED. CHANGED STATUS FROM PA TO FR PER FACILITY REPORT DATED 5/16/2017 FROM JOHN FLEMING F_REST_PASS ON 5/17/2017 CM.
Construction Permit Expires 2018-01-07 DRILLED & COMPLETED..NO PRODUCTION DATA REPORTED. CHANGED STATUS FROM PA TO FR PER FACILITY REPORT DATED 5/16/2017 FROM JOHN FLEMING F_REST_PASS ON 5/17/2017 CM.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2002-09-25 5148 5202 20
5148 5202 20
5148 5202 20

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1350 Bbl 0

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2011 D & L ENERGY INC 0.00 0.00 0
2014 D & L ENERGY INC 0.00 0.00 0
2016 D & L ENERGY INC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2011 D & L ENERGY INC Brine 0
2014 D & L ENERGY INC Brine 0 0
2016 D & L ENERGY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1668823634 2016-3-9 0:00:0 PB No Violations 4.00
-546413862 2015-3-13 0:00: PW No Violations 0.70
0546413862 2015-03-13 Production Wells Violations Noted I was on location for a status check. During my inspection, I found the well not in production. The wells 4.5 inch casing is reduced with a 4.5 inch by 2 inch swage, 2 inch Tee and 2 inch bull plug. One side of the 2 inch Tee is missing a plug. There is no production equipment associated with the well. There is no identification posted. Access to the well is the landowners driveway. The only reported annual production by D & L was zero in 2011. The well shall be plugged by 9/4/2015. Photo were taken and are available upon request.
1454339980 2016-01-13 Administrative Inspection No Violations Jeff Moore from Moores Well Service is the plugging contractor for the bankruptcy settlement of the D&L wells and myself went to the residence and talked to Tracy Dearst to explain that we needed to enter the property to plug this well. She denied us access until she had proof. I called Mark Vantyne and explained this to him.
1466011009 2016-03-08 Plug / Plug Back No Violations Moore Well Service is moving on this location to start plugging operations on the above well. Rig is over the well at this time they are laying 2 steel line to be used in the plugging operations one for pumping and the other line for circulation to a 400 barrel tank. A cementing equipment will be off of location.
1467726766 2016-03-21 Administrative Inspection No Violations I was on location to witness the plugging of this well. Moore Well Service and Petroset Cementing were the contractors on location performing the plugging operations. There was a Compliance Notice (-546413862) issued on 3/13/2015. This notice can be closed at this time.
1494945224 2017-05-16 Final Restoration No Violations I performed a final restoration inspection on the above location. There was no production equipment or pipeline installed. The area that was used to enter into the location and the location of the well has been restored and vegetation has been established. Final Restoration is passed.
1668823634 2016-03-09 Plug / Plug Back No Violations Moore Well Service started running 2-3/8 tubing in the well to pump the bottom plug at 750 they encountered a blockage. They will be moving there power swivel on location to drill out the blockage.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0546413862 US-OH-126009 2016-07-26 9-9-05(A)10 Failure to legibly identify well
0546413862 US-OH-126010 2015-05-04 Well shall be plugged
0546413862 US-OH-126011 2016-07-26 NONEC Statement of annual production not filed

For data sources see[9]

References