X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

34-099-20629

Well Details

Well ID: 34-099-20629
Loading map...
Country: United States
State: Ohio
County: Mahoning
Municipality: Canfield Township
Operator Name: HISTORIC OWNER
Well Pad ID:
Farm/Lease Name: AFC CORP
License Status: Orphan Well - Ready
License Date: 1976-03-24
Spud Date: 1976-03-27
Spud Drilling Contractor: ARMSTRONG DRLG
Final Drill Date: 1976-04-01
Well Total Depth: 5600.00 ft
Configuration: Vertical
Latitude: 40.990000
Longitude: -80.750000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1976-03-27 IP.A.F. 1.555MMCFG Orphan Well Case #2016 10 044
Completed 1976-04-01 IP.A.F. 1.555MMCFG Orphan Well Case #2016 10 044
Reached Total Depth 1976-04-01 IP.A.F. 1.555MMCFG Orphan Well Case #2016 10 044
Completion Report Received 1976-05-12 IP.A.F. 1.555MMCFG Orphan Well Case #2016 10 044
Changed to Orphan Well Ready 2016-10-01 Changed Well To Orphan Ready
Record Last Modified 2019-03-25 IP.A.F. 1.555MMCFG Orphan Well Case #2016 10 044

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2002-09-30 5420 5542 25
5420 5542 25
5420 5542 25

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 86000 Gal 75000 226.5M SCF NITROGEN ASSIST
ACID 0 600 Gal 0

For data sources see[4]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1011068953 2008-12-30 0:00 PW No Violations
-1048148460 2008-8-19 0:00: PW No Violations
1011068953 2008-12-30 Production Wells No Violations Continued from 8/19/08. I GPSd the well. 8/19/08--- I received a call from Mr. Nick Rulli(cell 330-518-7930)home(330-538-9725) about this well. He owns the property and wanted it plugged. I checked RBDMS and found no information on this well. I called Erica Freeman at the Columbus office to ask her about the operator. She also had no information. I called Andy Koval from North Coast because North Coast had a well east of the AFC 1. I checked in the computer on the GPS program. The Lat. Long for the well is seen above. He couldnt find well. I GPSd the tank battery. I called Mr. Scott Wilkes(330-252-4560). He knows the operator. He wants to buy the well and plug it. I told Mr. Wilkes to call Mr. Rulli and see if between the two of you that the well can be plugged. I will call back later. Even though Mr. Wilkes is trying to find out more about this well. This well has 5600 of 4 1/2 casing and 5430 of 2 3/8 tubing. The well was spudded on 3/27/76. The gas was used to heat the work office.
1048148460 2008-08-19 Production Wells No Violations I received a call from Mr. Nick Rulli(cell 330-518-7930)home(330-538-9725) about this well. He owns the property and wanted it plugged. I checked RBDMS and found no information on this well. I called Erica Freeman at the Columbus office to ask her about the operator. She also had no information. I called Andy Koval from North Coast because North Coast had a well east of the AFC 1. I checked in the computer on the GPS program. The Lat. Long for the well is seen above. He couldnt find well. I will have to wait for fall to locate the well. I GPSd the tank battery. I called Mr. Scott Wilkes(330-252-4560). He knows the operator. He wants to buy the well and plug it. I told Mr. Wilkes to call Mr. Rulli and see if between the two of you that the well can be plugged. I will call back later. Even though Mr. Wilkes is trying to find out more about this well. This well has 5600 of 4 1/2 casing and 5430 of 2 3/8 tubing. The well was spudded on 3/27/76. The gas was used to heat the work office.
1248091896 2009-07-17 Production Wells No Violations I called Gas Acquisition and talked to Kelly Jones. I left a message about this well. The answering service said Kelly Jones will be in on Monday, 7/20/09. This case continues.
1321654693 2009-08-18 Production Wells No Violations I called Randy Huffman from Gas Acquisition about this well. The problem with plugging this well is Gas Acquisition owns the land around the well but another landowner owns the land that Gas Acquisition has to cross to plug. Gas Acquisition is still working on this problem.
1359395252 2013-01-08 Orphan No Violations On 1/8/2013. I received a call from Tony Jasko about the above well. He has been trying to get in contact ( phone messages) with the landowner Judith Raber but has not had a response back. I also left a message for Judith Raber on 1/24/2013, with no response. After talking with Tom Hill about this, he has talked with Erica Freeman about the ownership Form 9 but there is no Form 9 on file. The well has one 100 barrel tank and one horizontal separator. The well has 2.375 tubing with 4.5 casing.
1437145713 2015-07-17 Production Wells No Violations I performed an Inspection on the above location. The well is equipped with 2.375 tubing. The valves on the wellhead are shut at this time. There is a leak at the wellhead unknown location but could hear it. The tank battery is equipped with one 100 barrel tank and one vertical separator. There has been no reported production on this well. There are no ID signs post at wellhead or at the tank battery. This well is located next to a natural drain that runs north and south of this location.
1466523321 2016-06-20 Orphan No Violations The Division of Oil and Gas received a non productive well complaint in 2008 from the prior landowner, Mr. Rulli. The well was permitted to AFC Corporation and drilled in 1976. AFC Corporation went into bankruptcy and was dissolved with a transfer of assets to AFC Company in 1986. A Division of Oil and Gas Change of Owner form was NOT filed transferring the well from AFC Corporation to AFC Company. The Ohio Secretary of State cancelled AFC Companys Articles of Incorporation on 04/05/2011. Division of Oil and Gas records show that production records have not been filed for over 27 years and that insurance is not current. The Division of Oil and Gas currently has this well listed with a Historical Producer status. A $5,000. bond was posted in 1976 and the Divisions Bonding section will attempt to retrieve the Bond. The current landowner, Mr. Joel Matthews, has also contacted the Division of Oil and Gas requesting this well be plugged due to years of non production. Division of Oil and Gas files show this is a Rotary drilled well and is equipped with 765 of 8 5/8 casing, cemented with 225 sacks of cement; 5600 of 4 1/2 casing, cemented with 150 sacks of 50/50 pos-mix and 5430 of 2 3/8 tubing. My inspection today found the well is located in a hay field. There is not a lease road to the well. The well is equipped with 2 3/8 tubing. The tubing valve is closed. The well is equipped with a 4 1/2 well head on visible 4 1/2 casing. The tubing and 4 1/2 casing both have production lines tied into the flowline. The valves are closed on the tubing and the 4 1/2 casing production lines. The flowline is buried. The 8 5/8 casing head is buried and gas is leaking through the ground above the buried 8 5/8 well head. A cut off steel line with a shut valve is coming from the ground near the well head, this line is possibly connected to the 8 5/8 casing. My Sperian gas detector showed 100% LEL and 0 ppm H2S in the area above the buried 8 5/8 casing head. There is not a domestic lin
1486409939 2017-02-06 Production Wells No Violations I performed an Inspection on the above location. The well is equipped with 2.375 tubing. The valves on the wellhead are shut at this time. The tank battery is equipped with one 100 barrel tank and one vertical separator. There has been no reported production on this well. There are no ID signs posted at wellhead or at the tank battery. This well is located next to a natural drain that runs north and south of this location. On my last inspection ( 7/17/2015 ) there was a leak at the wellhead. At the time of this inspection I coud not hear or detect a leak at the wellhead.
1497362388 2017-06-09 Orphan No Violations Todays inspection is being conducted to check the condition of the well. Mr. Matthews, the landowner, was met on location. The tank battery is overgrown and cannot be inspected due to the gate being rusted shut. The well is still leaking gas from beneath the ground surface right at the well. A gas odor is evident near the well. My Sperian gas meter quickly detected 70% LEL/0 ppm H2S/1.85 CH4 approximately 6 inches above the ground level at the well before the meter was removed to preserve the sensor. The well has visible 2 3/8 inch diameter tubing. The tubing valve is closed. The well has a 4 1/2 inch diameter well head on visible 4 1/2 inch diameter casing. The tubing and 4 1/2 inch casing both have production lines tied into the flowline. The valves are closed on the tubing and the 4 1/2 inch casing production lines. The flowline is buried. The 8 5/8 inch diameter casing head is buried. A disconnected steel line with a shut valve is coming from the ground near the well head, this line is possibly connected to the 8 5/8 inch casing. Mr. Matthews has requested that the well be plugged by the Orphan Well program. The Enforcement section is currently reviewing if bond revocation is possible.
1507732580 2017-10-04 Production Wells No Violations I was on location to follow-up on Chiefs Order 2017-308 ( Order to Plug the well. ) The well remains on location and is equipped with 2 tubing no action has been taken to plug the well. The tank battery is equipped with one 100 barrel tank and one horizontal separator. No ID signs are posted. The tank battery is overgrown with heavy vegetation. AFC Corp. has not plugged the well in compliance with Order NO 2017-308.
2119218816 2018-02-22 Orphan No Violations My inspection found no changes since my last inspection.

For data sources see[5]

References