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34-087-20386

Well Details

Well ID: 34-087-20386
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Country: United States
State: Ohio
County: Lawrence
Municipality: Elizabeth Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: SILICA SHARON
License Status: Final Restoration
License Date: 2011-06-23
Spud Date: 1985-01-02
Spud Drilling Contractor: CLINT HURT
Final Drill Date: 1985-01-05
Well Total Depth: 3066.00 ft
Configuration: Vertical
Latitude: 38.590000
Longitude: -82.610000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1984-12-20 1089 MITCHELL ENERGY CORP GeoDate 12/20/84
Oil and Gas 1984-12-20 Issued Date 12/20/84 Expired Date 6/18/85 Acres 0080000 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 03066 Proposed Drill Depth 03066
Original Spud 1985-01-02
Reached Total Depth 1985-01-05
Completed 1985-01-06
Completion Report Received 1985-02-21
Change of Owner 1999-10-22 Operator changed from 1089, MITCHELL ENERGY CORP to 3793, ENERGY SEARCH INC
Change of Owner 2008-02-26 Operator changed from 3793, ENERGY SEARCH INC to 1388, NORTH COAST ENERGY INC
Change of Owner 2010-05-06 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
APP 2011-06-23 Proposed Formations:CLINTON, Issued Date:6/23/2011, Expired Date:6/22/2013 12:00:00 PM, Drilling unit acres:80, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2011-09-07
Construction Permit Expires 2013-06-22
Record Last Modified 2017-02-15

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 2921 2941 14
2921 2941 14
2921 2941 14

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
GEL 0 1201 Bbl 90000
ACID 3 1250 Gal 0 FRAC: H2O,SAND

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1993 MITCHELL ENERGY CORP 0.00 0.00 0
1994 MITCHELL ENERGY CORP 0.00 0.00 365
1995 MITCHELL ENERGY CORP 0.00 0.00 0
1996 MITCHELL ENERGY CORP 0.00 0.00 0
1997 MITCHELL ENERGY CORP 0.00 0.00 0
1998 MITCHELL ENERGY CORP 0.00 0.00 0
1999 MITCHELL ENERGY CORP 0.00 0.00 0
2000 ENERGY SEARCH INC 0.00 0.00 365
2009 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2010 ENERVEST OPERATING LLC 0.00 0.00 0
2011 ENERVEST OPERATING LLC 0.00 0.00 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1993 MITCHELL ENERGY CORP Brine 0 0
1994 MITCHELL ENERGY CORP Brine 0 365
1995 MITCHELL ENERGY CORP Brine 0 0
1996 MITCHELL ENERGY CORP Brine 0 0
1997 MITCHELL ENERGY CORP Brine 0 0
1998 MITCHELL ENERGY CORP Brine 0 0
1999 MITCHELL ENERGY CORP Brine 0 0
2000 ENERGY SEARCH INC Brine 365
2009 EXCO - NORTH COAST ENERGY INC Brine 0 0
2010 EXCO - NORTH COAST ENERGY INC Brine 0 0
2011 ENERVEST OPERATING LLC Brine 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1339511601 2011-9-8 0:00:0 PB No Violations
-1447231620 2011-1-6 0:00:0 PW No Violations
-1478744534 2014-4-23 0:00: FR No Violations 4.00
-1879383919 2004-6-10 0:00: PW No Violations
-1934702103 2014-4-23 0:00: FR No Violations 0.30
-2030018038 2011-1-10 0:00: PW No Violations
-349676956 2011-9-7 0:00:0 PB No Violations
000PL14102 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0130295856 2011-02-08 Production Wells No Violations Good identification. Well is disconnected from production equipment. No production line has been ran to the well site. Well is equipped with 4.5 by 2 swedge and valve. Took pictures.
0349676956 2011-09-07 Plug / Plug Back No Violations Chipco was unable to rip 4.5 casing below Lime plug zone. Appalachian wire line was brought in to perf the 4.5 casing in Lime for plug. 10 shots. Tubing ran to 2216. Pumped plug through tubing had good circulation. Pulled tubing and ripped 4.5 casing at 1442 Berea plug pumped through 4.5casing had good circulation. 100 in and 100 out of bottom of surface casing plug had circulation. 160 to surface plug. Cement stayed at surface. 4.5 casing had 4 centralizers and 1 cement basket on the end of the casing. Pit was pumped out into water truck.
0381833421 2011-01-10 Production Wells No Violations Good Identification. Gas leak has been fixed. No LEL reading on the gas meter. Wellhead is equipped with 4 1/2 collar with 4 1/2 by 2 swedge with 2 ball valve (closed) 2 bull plug with 1/4 nipple with 1/4 ball valve (closed) with old gauge.
0908677447 2011-01-11 Administrative Inspection No Violations Talked to Tim McConaha Re: Compliance notice for idle well. Tim was not sure if they will place the well on Temporary abandonment status or plug the well.
0957596393 2011-01-07 Production Wells No Violations Good identification. Wellhead is equipped with 4 1/2 collar with 4 1/2 by 2 swedge with 2 ball valve (closed) 2 bull plug with 1/4 nipple with 1/4 ball valve (closed) with old gauge. Wellhead is leaking small amount of gas from below 4 1/2 collar at ground level. I called and told Jim Ross Jim said he will have it fixed this weekend.
1011727253 2011-09-02 Plug / Plug Back No Violations Tag TOC plug @ 2579. Free point on 4.5 @ 2287. Attempting to rip 4.5. Pit liner is in good condition.
1294757191 2011-01-06 Production Wells Violations Noted Wellhead leaking gas. Tubing was removed in summer and a pup joint was left in the well. I talked to Jim Ross (Enervest Contractor) and he is going to the site today to fix the leak.
130295856 2011-2-8 0:00:0 PW No Violations
1339511601 2011-09-08 Plug / Plug Back No Violations Witnessed pit being closed. Cement is at 3 from surface. Rig is moving off location.
1447231620 2011-01-06 Production Wells No Violations Jim Ross was able to reduce the gas flow. They are going to remove the wellhead and install a 4 1/2 by 2 swedge with a valve.
1478744534 2014-04-23 Final Restoration No Violations Upon inspection, it was observed that all production equipment had been removed from this site, and all previously disturbed land surfaces had been stabilized with a permanent vegetative cover. This satisfies the requirements for the final restoration.
1879383919 2004-06-10 Production Wells No Violations Disconnected; camera battery died so no picture.
1934702103 2014-04-23 Final Restoration No Violations Restoration relieved by inspector LJ Parkins.
2020911644 2010-05-17 Production Wells No Violations Inspected well with Scott Means USFS. 4.5 wellhead at ground level, with 2 tubing in well. 2 valve on tubing and a 2 tee with bull plugs and needle valves. Not connected to production equipment. 2 line with meter housing and equipment. Chart and meter have been removed.
2030018038 2011-01-10 Production Wells Violations Noted Wellhead is equipped with 4 1/2 collar with 4 1/2 by 2 swedge with 2 ball valve (closed) 2 bull plug with 1/4 nipple with 1/4 ball valve (closed) with old gauge. Good identification. Well is not connected to production equipment. Well is not connected to a production line. Well has never been in production since drilled in 1985. 1509.062 (A) (1) The owner of a well that has not been completed, A well that has not produced within one year after completion, or an existing well that has no reported production for two consecutive reporting periods as reported in accordance with section 1509.11 of the Revised Code shall plug the well in accordance with section 1509.12 of the Revised Code, obtain temporary inactive status for the well in accordance with this section.
381833421 2011-1-10 0:00: PW No Violations
908677447 2011-1-11 0:00: AM No Violations
957596393 2011-1-7 0:00:0 PW No Violations
PL14102 PL No Violations

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1294757191 US-OH-108301 2011-01-11 Well insufficiently equipped to prevent escape of oil and gas
2030018038 US-OH-120637 2011-01-11 Well shall be plugged
2030018038 US-OH-120638 2011-01-11 Nonproduction; well shall be plugged or placed in temporary inactive status

For data sources see[9]

References