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Well ID: 34-075-21484 | Loading map...
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Country: United States | |
State: Ohio | |
County: Holmes | |
Municipality: Richland Township | |
Operator Name: JOHN F WILLIAMS OIL FIELD SER | |
Well Pad ID: | |
Farm/Lease Name: MALDON HAWKINS | |
License Status: Final Restoration | |
License Date: 2013-05-22 | |
Spud Date: 1982-07-03 | |
Spud Drilling Contractor: | |
Final Drill Date: 1972-08-05 | |
Well Total Depth: 3176.00 ft | |
Configuration: Vertical | |
Latitude: 40.460000 | |
Longitude: -82.070000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Completed | 1972-08-05 | RE-ISSUE 6-29-72 |
Reached Total Depth | 1972-08-05 | RE-ISSUE 6-29-72 |
Original Spud | 1982-07-03 | RE-ISSUE 6-29-72 |
APP | 2009-09-11 | Proposed Formations:CLINTON, Issued Date:9/11/2009, Expired Date:9/11/2010 6:00:00 AM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2013-05-17 | RE-ISSUE 6-29-72 |
APP | 2013-05-22 | Proposed Formations:CLINTON, Issued Date:5/22/2013, Expired Date:5/22/2015 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Record Last Modified | 2014-07-25 | RE-ISSUE 6-29-72 |
Construction Permit Expires | 2015-05-22 | RE-ISSUE 6-29-72 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 3120 | 3148 | 0 |
3120 | 3148 | 0 | |
3120 | 3148 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2050 Bbl | 40000 | |||
ACID | 0 | 500 Gal | 0 | MUD |
For data sources see[4]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0041266886 | 2013-05-09 | Plug / Plug Back | No Violations | Set the 8 precast plug in the 8 seat at 350. Washed in 1 T of clay and the well filled up. Rigged down and moved off. Left clay on location to fill the hole. It will require daily filling until it is full. |
0384953111 | 2013-05-07 | Plug / Plug Back | No Violations | Tagged bottom at 3075 which is above the perforations. Washed in 3 tons of clay. Ripped the casing at 2707 and pulled 19 joints of casing before washing in 2 more tons of clay for the bottom plug. |
0548939919 | 2013-05-21 | Final Restoration | No Violations | The clay has been buried and the location is back to original grade. There is no seed or mulch. |
0869983985 | 2013-05-12 | Plug / Plug Back | No Violations | Checked the top plug. It has dropped each day and has been filled up again by the operator. |
1074335221 | 2013-05-16 | Plug / Plug Back | No Violations | The top plug dropped 20. The casing was filled back to the surface and monitored for 30 minutes. The plug is still dropping. The plug will be checked later and refilled if necessary. |
1344106519 | 2013-05-20 | Plug / Plug Back | No Violations | The 10 casing was cut off at 4 below ground level and a plate with the permit number welded on the top. The leftover clay will be buried, the limestone removed and the location put back to final grade. |
1368094977 | 2013-05-08 | Plug / Plug Back | No Violations | Displaced 8 bbls of oil out of the hole while washing in clay for the balance of the bottom plug. Pulled the balance of the 4-1/2 casing. Bridged the 8 hole at 725 and washed in 3 tons of clay. Pulled the 8-5/8 casing. Washed in 2 tons of clay for the Berea plug . |
1395087946 | 2014-03-13 | Final Restoration | No Violations | Final Restoration is passed |
384953111 | 2013-5-7 0:00:0 | PB | No Violations | |
41266886 | 2013-5-9 0:00:0 | PB | No Violations | |
548939919 | 2013-5-21 0:00: | FR | No Violations | |
869983985 | 2013-5-12 0:00: | PB | No Violations |
For data sources see[9]