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Well ID: 34-075-21096 | Loading map...
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Country: United States | |
State: Ohio | |
County: Holmes | |
Municipality: Monroe Township | |
Operator Name: COLUMBIA GAS TRANSMISSION LLC | |
Well Pad ID: | |
Farm/Lease Name: WILLIAMS OTIS & ETHEL | |
License Status: Final Restoration | |
License Date: 2013-02-01 | |
Spud Date: 1959-10-13 | |
Spud Drilling Contractor: | |
Final Drill Date: 1959-11-21 | |
Well Total Depth: 3391.00 ft | |
Configuration: Vertical | |
Latitude: 40.590000 | |
Longitude: -82.000000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1959-10-13 | LOG TYPE-NUCLEAR LOG-PERFORATE |
Completed | 1959-11-21 | LOG TYPE-NUCLEAR LOG-PERFORATE |
Reached Total Depth | 1959-11-21 | LOG TYPE-NUCLEAR LOG-PERFORATE |
Change of Owner | 2011-09-07 | Operator changed from 9998, HISTORIC OWNER to 22, COLUMBIA GAS TRANSMISSION |
APP | 2013-02-01 | Proposed Formations:CLINTON, Issued Date:2/1/2013, Expired Date:2/1/2015 12:00:00 PM, Drilling unit acres:52, Proposed Well Type:SO, Proposed Well Class: |
Plugged/Abandoned | 2013-02-18 | LOG TYPE-NUCLEAR LOG-PERFORATE |
Record Last Modified | 2014-07-25 | LOG TYPE-NUCLEAR LOG-PERFORATE |
Construction Permit Expires | 2015-02-01 | LOG TYPE-NUCLEAR LOG-PERFORATE |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
Not Treated | 0 | 850 Bbl | 42000 | R.P. 72 HRS. |
For data sources see[3]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1291443143 | 2013-2-13 0:00: | PB | No Violations | |
-2080395021 | 2013-4-15 0:00: | FR | No Violations | |
-415383909 | 2013-3-7 0:00:0 | FR | No Violations | |
0264561710 | 2013-05-20 | Final Restoration | No Violations | The location has been put to final grade and seeded and mulched. There is good growth on the location. Final restoration passed. |
0277289426 | 2012-09-13 | Storage Well | No Violations | There were no problems noted at the time of the inspection. |
0415383909 | 2013-03-07 | Final Restoration | No Violations | The pit has been emptied and closed and the location has been roughed in. |
1291443143 | 2013-02-13 | Plug / Plug Back | No Violations | Ran tubing to 3338. Petroset spotted a 40 sx cement plug from 3338 to 2838. Pulled 20 joints and reversed out. No cement returned. Pulled the balance of the tubing. See the plugging record for further details. |
1360239174 | 2013-02-06 | Plug / Plug Back | No Violations | A dozer has been moved on location but no other activity has been started. It is anticipated that a rig will move in on 2/11/13. |
1360325859 | 2013-02-07 | Plug / Plug Back | No Violations | A new road has been cut in to the well. A location has been cut around the well to set up the plugging rig. The well head has been excavated and the old head cut off and replaced with a working wellhead. |
1360756125 | 2013-02-12 | Plug / Plug Back | No Violations | Finished stoning the road to location. Moved the plugging rig on and rigged up. |
1360928612 | 2013-02-14 | Plug / Plug Back | No Violations | Baker Hughes ran a free point survey and parted the casing at 2850. The pipe was free but circulation was not obtained. Several joints of casing were pulled, circulation was obtained and Petroset Cementing spotted a 350 cement plug from 2610 to 2260. The casing was pulled out of this plug and another 500 plug was spotted from 2190 to 1690. The balance of the casing was pulled out of the well. The rig shut down for the night. See the plugging record for more details. |
1361361247 | 2013-02-15 | Plug / Plug Back | No Violations | Pulled the 8-5/8 casing. Ran 2-3/8 EUE tubing into the hole and tagged the cement at 1700. Shut down for the night. |
2080395021 | 2013-04-15 | Final Restoration | No Violations | The location has been put to final grade. There is no vegation growth. |
264561710 | 2013-5-20 0:00: | FR | No Violations | |
277289426 | 2012-9-13 0:00: | SO | No Violations |
For data sources see[4]