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34-075-20681

Well Details

Well ID: 34-075-20681
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Country: United States
State: Ohio
County: Holmes
Municipality: Ripley Township
Operator Name: COLUMBIA GAS TRANSMISSION LLC
Well Pad ID:
Farm/Lease Name: FRANKS CARL D
License Status: Storage Well
License Date:
Spud Date: 1954-12-04
Spud Drilling Contractor: CO TOOLS
Final Drill Date: 1955-01-26
Well Total Depth: 3392.00 ft
Configuration: Vertical
Latitude: 40.610000
Longitude: -82.040000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1954-12-04 GL=1170.3, STORAGE
Completed 1955-01-26 GL=1170.3, STORAGE
Reached Total Depth 1955-01-26 GL=1170.3, STORAGE
Change of Owner 2011-09-07 Operator changed from 9998, HISTORIC OWNER to 22, COLUMBIA GAS TRANSMISSION
Record Last Modified 2012-06-07 GL=1170.3, STORAGE

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2012-05-29 H2O 0 242 Bbl 24000 Universal Well Services Inc. 20# per Mgal crosslinked gel job with 20% N2 assist

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1780266771 2012-7-12 0:00: PL No Violations
-1867117342 2017-1-25 0:00: SO No Violations
-2141017714 2018-2-13 0:00: SO No Violations 0.30
-244371890 2016-2-23 0:00: SO No Violations
-553105569 2012-3-20 0:00: WR No Violations
-609172331 2014-1-23 0:00: SO No Violations
-732262662 2012-3-19 0:00: WR No Violations
-813596944 2013-3-12 0:00: SO No Violations
-916066884 2012-5-29 0:00: WR No Violations
0114844175 2012-05-17 Work Over Reconditioning No Violations The pit has been emptied and filled in and the location roughed in . The frac is set up for May 29, 2012.
0244371890 2016-02-23 Storage Well No Violations This is a storage well. There were no problems noted at the time of the inspection. There is no tank.
0294407006 2012-03-13 Work Over Reconditioning No Violations Cemented 3.5 liner thru 2-3/8 drill pipe.
0553105569 2012-03-20 Work Over Reconditioning No Violations Grouted 7 casing back to surface with 40 Sx of Class A cement. Stayed up.
0609172331 2014-01-23 Storage Well No Violations This is a storage well. There were no problems noted at the time of the inspection. There is no tank.
0625841583 2015-01-13 Storage Well No Violations This is a storage well. There were no problems noted at the time of the inspection. There is no tank.
0732262662 2012-03-19 Work Over Reconditioning No Violations Drilling out 7 wiper plug. Will circulate sand off retrievable plug and retrieve the plug. Grout surface casing 3/20/12.
0769067987 2019-01-29 Storage Well No Violations On the day of my inspection I found this to be a storage well. There were no problems noted at the time of the inspection. The well is properly identified.
0813596944 2013-03-12 Storage Well No Violations This is a storage well. There were no problems noted at the time of the inspection. There is no tank.
0916066884 2012-05-29 Work Over Reconditioning No Violations The well was fractured this date. See the treatment record for the details.
114844175 2012-5-17 0:00: WR No Violations
1331897246 2012-03-15 Work Over Reconditioning No Violations The rig ran 20 joints of 7 casing to 1033. They set a Baker 7 plug at 965 and perforated with 4 shots at 935. Petroset cemented with 260 sacks of regular Class A cement with 3% CaCl2. They ran 15 barrels of gel ahead of the cement. Circulation achieved but there were no cement returns to surface.
1454634898 2020-1-14 0:00: SO No Violations 0.30
1780266771 2012-07-12 Preliminary Restoration No Violations The location has been graded seeded and mulched. Due to the lack of rain, there is little grass growth at this time. There is a horizontal flowback tank on location. The well is not yet back on line.
1867117342 2017-01-25 Storage Well No Violations This is a storage well. There were no problems noted at the time of the inspection. There is no tank.
2141017714 2018-02-13 Storage Well No Violations On the day of my inspection I found this to be a storage well. There were no problems noted at the time of the inspection. The well is properly identified.
294407006 2012-3-13 0:00: WR No Violations
625841583 2015-1-13 0:00: SO No Violations
769067987 2019-1-29 0:00: SO No Violations 0.30

For data sources see[4]

References