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34-075-20652

Well Details

Well ID: 34-075-20652
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Country: United States
State: Ohio
County: Holmes
Municipality: Ripley Township
Operator Name: COLUMBIA GAS TRANSMISSION LLC
Well Pad ID:
Farm/Lease Name: DAYE OTHA
License Status: Storage Well
License Date:
Spud Date: 1954-07-16
Spud Drilling Contractor: CO TOOLS
Final Drill Date: 1954-08-31
Well Total Depth: 3383.00 ft
Configuration: Vertical
Latitude: 40.620000
Longitude: -82.050000

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1954-07-16 GL=1180.3, STOR
Completed 1954-08-31 GL=1180.3, STOR
Reached Total Depth 1954-08-31 GL=1180.3, STOR
Change of Owner 2011-09-07 Operator changed from 9998, HISTORIC OWNER to 22, COLUMBIA GAS TRANSMISSION
Record Last Modified 2013-03-11 GL=1180.3, STOR

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
2012-06-07 H2O 0 245 Bbl 244000 Universal Well Services Inc. 20# per Mgal crosslinked gel job with 20% N2 assist

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1020612515 2013-3-8 0:00:0 SO No Violations
-112484048 2018-7-26 0:00: SO No Violations 0.50
-1405258299 2014-5-5 0:00:0 SO No Violations
-1933949009 2015-1-15 0:00: SO No Violations
-514595404 2012-3-20 0:00: SO No Violations
0112484048 2018-07-26 Storage Well No Violations On the day of my inspection I found this to be a storage well. There were no problems noted at the time of the inspection. The well is properly identified.
0148720400 2012-04-16 Work Over Reconditioning No Violations The grout in the surface casing stayed up. Installing the well head and swabbing down the 3-1/2 tubing, to spot acid. They will rig down and move off.
0253050429 2012-03-23 Work Over Reconditioning No Violations Pulled 8-5/8 casing. Perforated 5-1/2 casing from 928 t0 930 and squeezed 310 sx class A cement. No circulation and no returns, will grout. Cement tagged at 140.
0514595404 2012-03-20 Storage Well No Violations Well will be worked over with in the week.
0540146671 2012-03-26 Work Over Reconditioning No Violations Drilling out cement plug over squeeze perfs.
0581413585 2016-04-18 Storage Well No Violations This is a storage well. There were no problems noted at the time of the inspection. There is no tank.
0836195308 2017-01-26 Storage Well No Violations This is a storage well. There were no problems note at the time of the inspection. There is no tank.
1020612515 2013-03-08 Storage Well No Violations This is a storage well. There were no problems noted at the time of the inspection. There is no tank.
1171205005 2020-1-30 0:00: SO No Violations 0.50
1342609495 2012-07-17 Preliminary Restoration No Violations This location has been graded, seeded and mulched. There is sparse growth due to the drought. It is not yet back on line.
1405258299 2014-05-05 Storage Well No Violations This is a storage well. There were no problems noted at the time of the inspection. There is no tank.
148720400 2012-4-16 0:00: WR No Violations
1933949009 2015-01-15 Storage Well No Violations This is a storage well. There were no problems noted at the time of the inspection. There is no tank.
2014912167 2012-04-12 Work Over Reconditioning No Violations Drilling 10 of new hole. Will run and cement 3-1/2 tubing tomorrow.
2070106663 2019-02-27 Storage Well No Violations On the day of my inspection I found this to be a storage well. There were no problems noted at the time of the inspection. The well is properly identified.
2133777042 2012-04-13 Work Over Reconditioning No Violations Washed in last joint of 3-1/2 tubing and Universal cemented with 70 sacks of Class A cement. Grouted 5-1/2 surface casing back to surface. See casing ticket for details.
253050429 2012-3-23 0:00: WR No Violations
540146671 2012-3-26 0:00: WR No Violations
581413585 2016-4-18 0:00: SO No Violations
836195308 2017-1-26 0:00: SO No Violations

For data sources see[4]

References