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34-073-21021

Well Details

Well ID: 34-073-21021
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Country: United States
State: Ohio
County: Hocking
Municipality: Washington Township
Operator Name: POLING ALBERT
Well Pad ID:
Farm/Lease Name: HERRON JOHN & MAY HEIRS
License Status: Producing
License Date: 1962-10-19
Spud Date: 1962-10-02
Spud Drilling Contractor:
Final Drill Date: 1962-11-22
Well Total Depth: 2775.00 ft
Configuration: Vertical
Latitude: 39.470000
Longitude: -82.410000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1801-01-02 283 POLING ALBERT
Oil and Gas 1802-01-01
Original Spud 1962-10-02
Completed 1962-11-22
Reached Total Depth 1962-11-22
Record Last Modified 2013-10-03

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 850 Bbl 28000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2001 POLING ALBERT 0.00 396.00 261
2002 POLING ALBERT 0.00 318.00 365
2003 POLING ALBERT 0.00 380.00 365
2004 POLING ALBERT 0.00 336.00 365
2012 POLING ALBERT 0.00 0.00 90
2013 POLING ALBERT 0.00 0.00 0
2014 POLING ALBERT 0.00 35.00 62
2016 POLING ALBERT 0.00 31.00 160
2017 POLING ALBERT 0.00 65.00 120

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2001 POLING ALBERT Brine 0 261
2002 POLING ALBERT Brine 0 365
2003 POLING ALBERT Brine 0 365
2004 POLING ALBERT Brine 0 365
2012 POLING ALBERT Brine 0 90
2013 POLING ALBERT Brine 0 0
2014 POLING ALBERT Brine 0 62
2016 POLING ALBERT Brine 0 160
2017 POLING ALBERT Brine 0 120

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1029751789 2013-1-9 0:00:0 PW No Violations 1.00
-115974230 2018-5-29 0:00: PW No Violations 0.30
-1253056888 2013-3-27 0:00: PW No Violations 1.50
-1267589780 2016-6-27 0:00: PW No Violations 3.50
-1733614142 2013-3-27 0:00: PW No Violations 1.00
-1995084286 2017-12-22 0:00 PW No Violations 1.00
0115974230 2018-05-29 Production Wells No Violations My inspection revealed the status of the well has not changed during my last inspection. The main beam is twisted and the horse head is laying on the ground. The motor to run the pumping unit is missing. I called well owner Mr. Albert Poling at 12:20 PM but was unable to leave a message. The well reported 65 barrels of oil for reporting year 2017. New pictures were taken during my inspection.
0305759791 2013-11-06 Production Wells No Violations Compliance notice follow up. The well is still in disrepair. The well is not capable of production. The well is missing the horse head and the main beam is twisted.
0330996325 2013-01-09 Production Wells No Violations FOLLOW UP TO NOV # -1029751789 Well is equipped with a pumping unit and electric motor. The horse head and bridle are missing from the pumping unit, and the walking beam is twisted with the counter-weights still on it. The arms are also disconnected from the gear box. There is no identification posted on the well. Production has not been reported since 2003. I spoke to Mr. Albert Poling on 1/10/13 at 9:28 am. We discussed the issues with this well and he may consider putting it in temporary inactive status. I told him that production reports needed submitted for this well. I also told him that identification needs posted on this well. I gave him Patty Nicklauss number at the Columbus office so that he could acquire the forms needed.
1014074114 2005-02-01 Production Wells No Violations No violations. NEW LAT & LONG
1029751789 2013-01-09 Production Wells Violations Noted Well is equipped with a pumping unit and electric motor. The horse head and bridle are missing from the pumping unit, and the walking beam is twisted with the counter-weights still on it. The arms are also disconnected from the gear box. There is no identification posted on the well. Production has not been reported since 2003. I spoke to Mr. Albert Poling on 1/10/13 at 9:28 am. We discussed the issues with this well and he may consider putting it in temporary inactive status. I told him that production reports needed submitted for this well. I also told him that identification needs posted on this well. I gave him Patty Nicklauss number at the Columbus office so that he could acquire the forms needed.
1253056888 2013-03-27 Production Wells No Violations No attempt has been made by company to gain compliance. Spoke with Mr. Albert Poling, and his daughters boyfriend Jason. Inspector Kip Thompson and I reviewed with him the list of needed remedial actions and gave him the phone numbers for the people in Columbus he needs to talk to in order to acquire the needed forms.
1267589780 2016-06-27 Production Wells No Violations Compliance notice follow-up. The well consists of a pumping unit and 1-100 barrel tank. The pumping is in disrepair. The horse head is missing and the main bean is twisted. The well is not capable of production. New photographs were taken.
1408275022 2014-07-24 Production Wells No Violations Compliance notice follow-up. The well is still in disrepair, the horse head is missing and the main beam is twisted. No attempt has been made to gain compliance.
1486992977 2017-02-13 Production Wells No Violations Compliance notice follow-up. The status of the well has not changed. The horse head is missing and the main beam is twisted. The motor for the well is in a enclosure. The pulleys on the motor are rusty and without belts. No attempt has been made to gain compliance. New photographs were taken showing the condition of the well.
1537469667 2018-09-20 Production Wells No Violations I conducted a compliance notice follow-up inspection in regards to Inspector Andrew Thomass compliance notice issued on 1/10/2013. My inspection revealed that the well has not been plugged or placed into production. The well was in the exact same appearance as described in Mr. Thomass compliance notice. The well was not capable of production. The beam on the pumping unit was twisted and vegetation is starting to cover the pumping unit. RBDMS records show 65 barrels of oil reported for 2017. I took three photos of the well. Time of inspection: 1:40 PM. Weather: 86 degrees F, Sunny
1555593035 2019-04-18 Production Wells No Violations My inspection revealed that the well has not been plugged or placed into production. The well owner has not made an attempt to bring the well into compliance. The well was not capable of production. The beam on the pumping unit was twisted. RBDMS records show 65 barrels of oil reported for 2017. I took six photos of the well. I contacted Albert Poling at 3:50 PM and discussed the well with him. Time of inspection: 8:25 AM. Weather: 61 degrees F, Sunny
1733614142 2013-03-27 Production Wells No Violations Hocking county training with Andy Thomas.
1995084286 2017-12-22 Production Wells No Violations My inspection revealed the well is not in compliance. The main beam is twisted, the horse head is missing as well as the motor. The well is not capable of production. 35 barrels of oil has been reported in 2016.
305759791 2013-11-6 0:00: PW No Violations 1.00
330996325 2013-1-9 0:00:0 PW No Violations 1.00

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1029751789 US-OH-100315 2013-02-05 Failure to legibly identify well
1029751789 US-OH-100316 2013-02-05 Nonproduction; well shall be plugged or placed in temporary inactive status
1029751789 US-OH-100317 2013-02-05 Statement of annual production not filed

For data sources see[8]

References