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Well ID: 34-073-21021 | Loading map...
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Country: United States | |
State: Ohio | |
County: Hocking | |
Municipality: Washington Township | |
Operator Name: POLING ALBERT | |
Well Pad ID: | |
Farm/Lease Name: HERRON JOHN & MAY HEIRS | |
License Status: Producing | |
License Date: 1962-10-19 | |
Spud Date: 1962-10-02 | |
Spud Drilling Contractor: | |
Final Drill Date: 1962-11-22 | |
Well Total Depth: 2775.00 ft | |
Configuration: Vertical | |
Latitude: 39.470000 | |
Longitude: -82.410000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1801-01-02 | 283 POLING ALBERT |
Oil and Gas | 1802-01-01 | |
Original Spud | 1962-10-02 | |
Completed | 1962-11-22 | |
Reached Total Depth | 1962-11-22 | |
Record Last Modified | 2013-10-03 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 850 Bbl | 28000 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2001 | POLING ALBERT | 0.00 | 396.00 | 261 |
2002 | POLING ALBERT | 0.00 | 318.00 | 365 |
2003 | POLING ALBERT | 0.00 | 380.00 | 365 |
2004 | POLING ALBERT | 0.00 | 336.00 | 365 |
2012 | POLING ALBERT | 0.00 | 0.00 | 90 |
2013 | POLING ALBERT | 0.00 | 0.00 | 0 |
2014 | POLING ALBERT | 0.00 | 35.00 | 62 |
2016 | POLING ALBERT | 0.00 | 31.00 | 160 |
2017 | POLING ALBERT | 0.00 | 65.00 | 120 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2001 | POLING ALBERT | Brine | 0 | 261 |
2002 | POLING ALBERT | Brine | 0 | 365 |
2003 | POLING ALBERT | Brine | 0 | 365 |
2004 | POLING ALBERT | Brine | 0 | 365 |
2012 | POLING ALBERT | Brine | 0 | 90 |
2013 | POLING ALBERT | Brine | 0 | 0 |
2014 | POLING ALBERT | Brine | 0 | 62 |
2016 | POLING ALBERT | Brine | 0 | 160 |
2017 | POLING ALBERT | Brine | 0 | 120 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-1029751789 | 2013-1-9 0:00:0 | PW | No Violations | 1.00 |
-115974230 | 2018-5-29 0:00: | PW | No Violations | 0.30 |
-1253056888 | 2013-3-27 0:00: | PW | No Violations | 1.50 |
-1267589780 | 2016-6-27 0:00: | PW | No Violations | 3.50 |
-1733614142 | 2013-3-27 0:00: | PW | No Violations | 1.00 |
-1995084286 | 2017-12-22 0:00 | PW | No Violations | 1.00 |
0115974230 | 2018-05-29 | Production Wells | No Violations | My inspection revealed the status of the well has not changed during my last inspection. The main beam is twisted and the horse head is laying on the ground. The motor to run the pumping unit is missing. I called well owner Mr. Albert Poling at 12:20 PM but was unable to leave a message. The well reported 65 barrels of oil for reporting year 2017. New pictures were taken during my inspection. |
0305759791 | 2013-11-06 | Production Wells | No Violations | Compliance notice follow up. The well is still in disrepair. The well is not capable of production. The well is missing the horse head and the main beam is twisted. |
0330996325 | 2013-01-09 | Production Wells | No Violations | FOLLOW UP TO NOV # -1029751789 Well is equipped with a pumping unit and electric motor. The horse head and bridle are missing from the pumping unit, and the walking beam is twisted with the counter-weights still on it. The arms are also disconnected from the gear box. There is no identification posted on the well. Production has not been reported since 2003. I spoke to Mr. Albert Poling on 1/10/13 at 9:28 am. We discussed the issues with this well and he may consider putting it in temporary inactive status. I told him that production reports needed submitted for this well. I also told him that identification needs posted on this well. I gave him Patty Nicklauss number at the Columbus office so that he could acquire the forms needed. |
1014074114 | 2005-02-01 | Production Wells | No Violations | No violations. NEW LAT & LONG |
1029751789 | 2013-01-09 | Production Wells | Violations Noted | Well is equipped with a pumping unit and electric motor. The horse head and bridle are missing from the pumping unit, and the walking beam is twisted with the counter-weights still on it. The arms are also disconnected from the gear box. There is no identification posted on the well. Production has not been reported since 2003. I spoke to Mr. Albert Poling on 1/10/13 at 9:28 am. We discussed the issues with this well and he may consider putting it in temporary inactive status. I told him that production reports needed submitted for this well. I also told him that identification needs posted on this well. I gave him Patty Nicklauss number at the Columbus office so that he could acquire the forms needed. |
1253056888 | 2013-03-27 | Production Wells | No Violations | No attempt has been made by company to gain compliance. Spoke with Mr. Albert Poling, and his daughters boyfriend Jason. Inspector Kip Thompson and I reviewed with him the list of needed remedial actions and gave him the phone numbers for the people in Columbus he needs to talk to in order to acquire the needed forms. |
1267589780 | 2016-06-27 | Production Wells | No Violations | Compliance notice follow-up. The well consists of a pumping unit and 1-100 barrel tank. The pumping is in disrepair. The horse head is missing and the main bean is twisted. The well is not capable of production. New photographs were taken. |
1408275022 | 2014-07-24 | Production Wells | No Violations | Compliance notice follow-up. The well is still in disrepair, the horse head is missing and the main beam is twisted. No attempt has been made to gain compliance. |
1486992977 | 2017-02-13 | Production Wells | No Violations | Compliance notice follow-up. The status of the well has not changed. The horse head is missing and the main beam is twisted. The motor for the well is in a enclosure. The pulleys on the motor are rusty and without belts. No attempt has been made to gain compliance. New photographs were taken showing the condition of the well. |
1537469667 | 2018-09-20 | Production Wells | No Violations | I conducted a compliance notice follow-up inspection in regards to Inspector Andrew Thomass compliance notice issued on 1/10/2013. My inspection revealed that the well has not been plugged or placed into production. The well was in the exact same appearance as described in Mr. Thomass compliance notice. The well was not capable of production. The beam on the pumping unit was twisted and vegetation is starting to cover the pumping unit. RBDMS records show 65 barrels of oil reported for 2017. I took three photos of the well. Time of inspection: 1:40 PM. Weather: 86 degrees F, Sunny |
1555593035 | 2019-04-18 | Production Wells | No Violations | My inspection revealed that the well has not been plugged or placed into production. The well owner has not made an attempt to bring the well into compliance. The well was not capable of production. The beam on the pumping unit was twisted. RBDMS records show 65 barrels of oil reported for 2017. I took six photos of the well. I contacted Albert Poling at 3:50 PM and discussed the well with him. Time of inspection: 8:25 AM. Weather: 61 degrees F, Sunny |
1733614142 | 2013-03-27 | Production Wells | No Violations | Hocking county training with Andy Thomas. |
1995084286 | 2017-12-22 | Production Wells | No Violations | My inspection revealed the well is not in compliance. The main beam is twisted, the horse head is missing as well as the motor. The well is not capable of production. 35 barrels of oil has been reported in 2016. |
305759791 | 2013-11-6 0:00: | PW | No Violations | 1.00 |
330996325 | 2013-1-9 0:00:0 | PW | No Violations | 1.00 |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1029751789 | US-OH-100315 | 2013-02-05 | Failure to legibly identify well | |
1029751789 | US-OH-100316 | 2013-02-05 | Nonproduction; well shall be plugged or placed in temporary inactive status | |
1029751789 | US-OH-100317 | 2013-02-05 | Statement of annual production not filed |
For data sources see[8]