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Well ID: 34-073-20246 | Loading map...
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Country: United States | |
State: Ohio | |
County: Hocking | |
Municipality: Benton Township | |
Operator Name: COLUMBIA GAS TRANSMISSION LLC | |
Well Pad ID: | |
Farm/Lease Name: STATE OF OHIO | |
License Status: Final Restoration | |
License Date: 2011-10-12 | |
Spud Date: 1950-05-03 | |
Spud Drilling Contractor: | |
Final Drill Date: 1950-06-06 | |
Well Total Depth: 2452.00 ft | |
Configuration: Vertical | |
Latitude: 39.440000 | |
Longitude: -82.560000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1950-05-03 | |
Completed | 1950-06-06 | |
Reached Total Depth | 1950-06-06 | |
APP | 2011-10-12 | Proposed Formations:CLINTON, Issued Date:10/12/2011, Expired Date:10/11/2013 12:00:00 PM, Drilling unit acres:7396, Proposed Well Type:SO, Proposed Well Class: |
Plugged/Abandoned | 2011-12-08 | |
Record Last Modified | 2013-03-14 | |
Construction Permit Expires | 2013-10-11 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0573102565 | 2011-12-07 | Plug / Plug Back | No Violations | Witnessed plug being pumped on top of the bottom plug. |
0753620977 | 2012-05-10 | Final Restoration | No Violations | Final restoration meets 1509.072 requirements. Stone was left on the lease road as per instruction from The Ohio Division of Forestry. |
0983135903 | 2011-12-06 | Plug / Plug Back | No Violations | Bottom hole plug was tagged at 1605ft. 7 inch casing was free-pointed at 1500 ft. |
1323983318 | 2011-12-05 | Plug / Plug Back | No Violations | Company drilled through composite plug to reach total depth. Bottom plug was pumped through drill pipe. 75 sacks were pumped, they pulled 13 joints, 75 more sacks were pumped, then 16 joints were pulled and they reverse circulated. |
1324042656 | 2011-12-08 | Plug / Plug Back | No Violations | Cement was tagged at 980 ft. Two attempts were made to cut and pull the surface casing. The first was at 700 ft., and it would not pull, and the second at 433 ft. When company attempted to pull the second time, the casing parted at about 10 ft. Drill pipe was then set at 845 ft., then cement was pumped to surface. Drill pipe was pulled and cement fell back. Well was topped off, and cement stayed. |
1616733128 | 2011-11-22 | Plug / Plug Back | No Violations | Witnessed the setting of composite plug. The plug was set at 2391. The purpose of this plug is to keep the well safe while service rig is setting up and getting ready to plug the well. Composite plug will be drilled out. Log was also ran on well by Baker Hughes. |
573102565 | 2011-12-7 0:00: | PB | No Violations | 3.00 |
753620977 | 2012-5-10 0:00: | FR | No Violations | 1.50 |
983135903 | 2011-12-6 0:00: | PB | No Violations | 1.50 |
For data sources see[3]