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Well ID: 34-067-21573 | Loading map...
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Country: United States | |
State: Ohio | |
County: Harrison | |
Municipality: Nottingham Township | |
Operator Name: GULFPORT ENERGY CORPORATION | |
Well Pad ID: US-OH-001184 | |
Farm/Lease Name: LUYSTER 210213 | |
License Status: Drilling | |
License Date: 2019-01-03 | |
Spud Date: 2019-01-08 | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: 110.00 ft | |
Configuration: Horizontal | |
Latitude: 40.230000 | |
Longitude: -81.200000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2019-01-03 | Proposed Formations:UTICA/POINT PLEASANT, Issued Date:1/3/2019, Expired Date:1/2/2021 12:00:00 PM, Drilling unit acres:552.149, Proposed Well Type:OG, Proposed Well Class:POOL |
Record Last Modified | 2019-01-10 | |
Construction Permit Expires | 2021-01-02 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-545354204 | 2019-1-9 0:00:0 | CS | No Violations | 2.00 |
0545354204 | 2019-01-09 | Casing String Witnessed | No Violations | On the day of my inspection we witnessed Lightning Energy had augured a 36 inch diameter hole to 110 feet. 110 feet of 26 inch diameter conductor casing was run. Hole had water at 20 feet from surface prior to cementing. Lightning was onsite with 550 sacks of class A cement. Cement weighed with mudscale at 15.6 ppg and yield of 1.18. Cement additives include 3% cacl and .25 lb/sack celloflake. 75 percent excess ran. Cement was displaced to 100 feet with 64 barrels of fresh water. 17 barrels of cement returned to surface. |
For data sources see[3]