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Well ID: 34-067-21444 | Loading map...
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Country: United States | |
State: Ohio | |
County: Harrison | |
Municipality: Nottingham Township | |
Operator Name: AMERICAN ENERGY UTICA LLC | |
Well Pad ID: US-OH-001232 | |
Farm/Lease Name: CORDER E NTG HR | |
License Status: Plugged and Abandoned | |
License Date: 2015-04-13 | |
Spud Date: 2015-03-28 | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 40.260000 | |
Longitude: -81.130000 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2015-02-17 | Proposed Formations:UTICA THRU POINT PLEASANT, Issued Date:2/17/2015, Expired Date:2/16/2017 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:STRT |
APP | 2015-04-13 | Proposed Formations:UTICA THRU POINT PLEASANT, Issued Date:4/13/2015, Expired Date:4/12/2017 12:00:00 PM, Drilling unit acres:434.454, Proposed Well Type:OG, Proposed Well Class:EOUT |
Plugged/Abandoned | 2015-05-08 | |
Change of Owner | 2015-08-19 | Operator changed from 9193, AMERICAN ENERGY UTICA LLC to 9520, ASCENT RESOURCES UTICA LLC |
Change of Owner | 2015-08-24 | Operator changed from 9520, ASCENT RESOURCES UTICA LLC to 9193, AMERICAN ENERGY UTICA LLC - WELL TRANSFERRED TO ASCENT RESOURCES UTICA LLC IN ERROR LH WELL 8/24/2015 CM. |
Record Last Modified | 2017-02-16 | |
Construction Permit Expires | 2017-04-12 |
For data sources see[2]
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
-2024196680 | 2017-11-6 0:00: | PL | No Violations | 1.00 |
0052220810 | 2015-06-26 | Plug / Plug Back | No Violations | Upon arrival on location I found the crew runnig pipe into the wellbore to start plugging the well. The previous plug was tagged at 4306 feet. We will pull up to a depth of 4256 feet and will set a 500 foot plug there. Pulled drill pipe up to a depth of 2176 feet and set a 500 foot plug there. Drill pipe was then pulled to a depth of 300 feet, a 250 foot plug was set there and the last 50 feet was topped off. Circulated good cement to surface. |
1429797747 | 2015-04-23 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I was accompanied by James and Cowboy. The site looks in order and I see no issues with site construction or containment at this time. The rig has not yet started to drill, |
1430228662 | 2015-04-28 | Drill / Deepen / Reopen | No Violations | On the day of my inspection I found the crew drilling ahead at a depth of 4890 feet. There are no issues at this time. |
1430407716 | 2015-04-24 | Casing String Witnessed | No Violations
-Tex Pumping, LLC pumped 620sk of Class H cement at 15.6ppg, 1.20 yield, 2% CaCl2, 0.2% X-Air, and 0.25lbs/sk of Cello Flake. O-Tex displaced cement with 56bbl of fresh water. Plug was bumped, 13bbl of cement returned to surface weighing 15.5ppg. | |
1431092850 | 2015-05-08 | Plug / Plug Back | No Violations | Up on arrival on location I found that the crew had lost 1000 feet of the drilling assembly in the wellbore. The top of the fish being at a depth of 5512. A cement plug will be set from 5450 feet to 4250 feet. Once the cement plug is set the crew will run a scrapper into the wellbore to make sure the casing is free of cement. A retrievable bridge plug will be set in the wellbore and a night cap will be installed for safety and the rig will skid ahead to drill another well, then they will come back to this well and complete the well. |
1435301965 | 2015-06-25 | Plug / Plug Back | No Violations | Upon arrival on location it was determined that the plugging was not going to take place for a period of time, and I left location |
2024196680 | 2017-11-06 | Preliminary Restoration | No Violations | On the day of my inspection I found this well to have been plugged. Previous inspection reports indicate that tools were lost while drilling and well was plugged. The pad has 3 producing wells on it so a final restoration cannot be completed. |
52220810 | 2015-6-26 0:00: | PB | No Violations |
For data sources see[3]