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34-067-20531

Well Details

Well ID: 34-067-20531
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Country: United States
State: Ohio
County: Harrison
Municipality: Moorefield Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: DUNLAP HARVEY L & SHIRLEY
License Status: Final Restoration
License Date: 2013-05-02
Spud Date: 1982-04-12
Spud Drilling Contractor:
Final Drill Date: 1982-04-19
Well Total Depth: 6345.00 ft
Configuration: Vertical
Latitude: 40.200000
Longitude: -81.220000

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1982-03-16 2143 CARLESS RESOURCES INC GeoDate 3/16/82
Oil and Gas 1982-03-16 Issued Date 3/17/82 Expired Date 9/13/82 Acres 0040000 Tool Type RTA Proposed Formation CLINTON Proposed Depth 06345 Proposed Drill Depth 06345
Original Spud 1982-04-12 IP. A.F.
Completed 1982-04-19 IP. A.F.
Reached Total Depth 1982-04-19 IP. A.F.
Completion Report Received 1982-10-01 IP. A.F.
Change of Owner 1998-06-15 Operator changed from 2143, CARLESS RESOURCES INC to 1388, NORTH COAST ENERGY INC
Change of Owner 2009-12-14 Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC
APP 2013-05-02 Proposed Formations:CLINOTN, Issued Date:5/2/2013, Expired Date:5/2/2015 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2013-11-20 IP. A.F.
Construction Permit Expires 2015-05-02 IP. A.F.
Record Last Modified 2017-02-15 IP. A.F.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 6160 6225 2
6160 6225 2
6160 6225 2

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
Not Treated 0 0 50000 FRAC: FLUID, 50M SAND, 500G ACID

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1986 ZILKHA ENERGY INC 0.00 367.00 231
1987 SHERMAN MICHAEL 0.00 437.00 276
1990 CARLESS RESOURCES INC 0.00 278.00 365
1992 CARLESS RESOURCES INC 0.00 271.00 365
1993 CARLESS RESOURCES INC 0.00 288.00 365
1994 CARLESS RESOURCES INC 0.00 274.00 365
1995 CARLESS RESOURCES INC 0.00 99.00 365
1996 CARLESS RESOURCES INC 0.00 190.00 365
1997 CARLESS RESOURCES INC 0.00 0.00 365
1998 EXCO - NORTH COAST ENERGY INC 0.00 191.00 365
1999 EXCO - NORTH COAST ENERGY INC 0.00 0.00 365
2000 EXCO - NORTH COAST ENERGY INC 0.00 99.00 365
2001 EXCO - NORTH COAST ENERGY INC 0.00 0.00 180
2002 EXCO - NORTH COAST ENERGY INC 0.00 0.00 365
2003 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2004 EXCO - NORTH COAST ENERGY INC 0.00 263.00 365
2005 EXCO - NORTH COAST ENERGY INC 0.00 171.00 365
2006 EXCO - NORTH COAST ENERGY INC 0.00 55.00 365
2007 EXCO - NORTH COAST ENERGY INC 0.00 103.00 365
2008 EXCO - NORTH COAST ENERGY INC 0.00 0.00 366
2009 EXCO - NORTH COAST ENERGY INC 0.00 0.00 0
2010 ENERVEST OPERATING LLC 0.00 0.00 0
2011 ENERVEST OPERATING LLC 0.00 0.00 0
2012 ENERVEST OPERATING LLC 0.00 0.00 0
2013 ENERVEST OPERATING LLC 0.00 0.00 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1986 ZILKHA ENERGY INC Brine 372 231
1987 SHERMAN MICHAEL Brine 324 276
1990 CARLESS RESOURCES INC Brine 0 365
1992 CARLESS RESOURCES INC Brine 0 365
1993 CARLESS RESOURCES INC Brine 0 365
1994 CARLESS RESOURCES INC Brine 53 365
1995 CARLESS RESOURCES INC Brine 31 365
1996 CARLESS RESOURCES INC Brine 53 365
1997 CARLESS RESOURCES INC Brine 0 365
1998 EXCO - NORTH COAST ENERGY INC Brine 42 365
1999 EXCO - NORTH COAST ENERGY INC Brine 70 365
2000 EXCO - NORTH COAST ENERGY INC Brine 61 365
2001 EXCO - NORTH COAST ENERGY INC Brine 52 180
2002 EXCO - NORTH COAST ENERGY INC Brine 0 365
2003 EXCO - NORTH COAST ENERGY INC Brine 0 0
2004 EXCO - NORTH COAST ENERGY INC Brine 114 365
2005 EXCO - NORTH COAST ENERGY INC Brine 0 365
2006 EXCO - NORTH COAST ENERGY INC Brine 100 365
2007 EXCO - NORTH COAST ENERGY INC Brine 0 365
2008 EXCO - NORTH COAST ENERGY INC Brine 0 366
2009 EXCO - NORTH COAST ENERGY INC Brine 0 0
2010 ENERVEST OPERATING LLC Brine 0 0
2011 ENERVEST OPERATING LLC Brine 0
2012 ENERVEST OPERATING LLC Brine 0 0
2013 ENERVEST OPERATING LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
-1636108571 2013-12-19 0:00 PB No Violations 1.50
-2046594771 2013-9-17 0:00: PW No Violations 2.50
-490251213 2013-11-19 0:00 PB No Violations 4.00
-950551418 2013-11-20 0:00 PB No Violations
0286629085 2016-06-17 Final Restoration No Violations On the day of my inspection, I found that the final restoration has been complete. The site passed final restoration according to ORC 1509.072(B).
0490251213 2013-11-19 Plug / Plug Back No Violations I am on site today to plug this well and Chipco could not get 4 -1/2 inch casing to rip. On site while they went thru 3 blades and went after more. Did not witness any plugs today.
0697371033 2013-11-21 Plug / Plug Back No Violations Today I am on site to check the well for leaks. I did not find any leaks. The well has been cut off and can be covered over. I am also waiting to meet Little Bit for the cement ticket but he did not arrive.
0950551418 2013-11-20 Plug / Plug Back No Violations Chipco Well Service has Appalachian Wire line service on site to shoot the 4-1/2 inch diameter casing off. Was able to shoot off at 1660 ft. Chipco pulled one joint of casing out and then, wait on cement trucks. They were scheduled for 8:30 am.
1384955577 2013-11-19 Plug / Plug Back No Violations I am on site today to finish plugging this well to surface. The bottom plug and the Big Lime plug have been set. They tried to rip the 4-1/2 inch diameter casing and were not able to get a rip. Chipco Well service went thru 5 new blades and did not get the casing to rip. Next I advised that casing would have to be shot off .
1546112570 2013-11-12 Plug / Plug Back No Violations I am on site today to plug this well to surface. Chipco well service was to start plugging today but had to cancel the job today because they are not ready to plug.
1636108571 2013-12-19 Plug / Plug Back No Violations On the day of my inspection I witnessed that the well has been plugged and all equipment has been removed. Compliance issue has been resolved.
2046594771 2013-09-17 Production Wells Violations Noted

- 210bbl tanks. There was no domestic gas, pumping unit, flow line, separator, sales line, valves were closed on wellhead and no well identification. The well has not had any production the last 5 calendar years. The owner shall produce this well within 30 days or the well shall be plugged within 90 days. If the well is placed in production proper identification shall be posted. Spoke with Tim McConaha Enervest Energy at 330-877-6747 and he stated that the well is on their plugging list and a permit has been issued.

286629085 2016-6-17 0:00: FR No Violations 1.00
697371033 2013-11-21 0:00 PB No Violations 1.50

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
2046594771 US-OH-120836 2014-04-23 Well shall be plugged

For data sources see[9]

References